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Well ID: 34-167-28621 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Wesley Township | |
Operator Name: BROAD STREET SERV LLC | |
Well Pad ID: | |
Farm/Lease Name: YEAGER | |
License Status: Final Restoration | |
License Date: 2011-11-22 | |
Spud Date: 1988-12-24 | |
Spud Drilling Contractor: MID ATLANTC DRLG | |
Final Drill Date: 1989-01-03 | |
Well Total Depth: 5312.00 ft | |
Configuration: Vertical | |
Latitude: 39.420000 | |
Longitude: -81.800000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1988-12-15 | 45 G W F CORPORATION GeoDate 12/15/88 |
Oil and Gas | 1988-12-15 | Issued Date 12/15/88 Expired Date 12/15/89 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05312 Proposed Drill Depth 05312 |
Original Spud | 1988-12-24 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
Completed | 1989-01-03 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
Reached Total Depth | 1989-01-03 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
Completion Report Received | 1989-10-06 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
CO | 1995-08-31 | 3437 CEMCO OPERATING INC GeoDate 12/15/88 |
Change of Owner | 2001-04-09 | Operator changed from 3437, CEMCO OPERATING INC to 4350, CENTURY WELL SERVICE |
Change of Owner | 2007-10-03 | Operator changed from 4350, CENTURY WELL SERVICE to 7033, BROAD STREET ENERGY COMPANY |
Change of Owner | 2008-02-19 | Operator changed from 7033, BROAD STREET ENERGY COMPANY to 8312, BROAD STREET SERV LLC |
APP | 2011-11-22 | Proposed Formations:CLINTON/MEDINA, Issued Date:11/22/2011, Expired Date:11/21/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-10-23 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
Construction Permit Expires | 2013-11-21 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
Record Last Modified | 2015-10-01 | CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5031 | 5105 | 0 |
5031 | 5105 | 0 | |
2006-09-11 | 5073 | 5077 | 5 |
5073 | 5077 | 5 | |
5031 | 5105 | 0 | |
2006-09-11 | 5085 | 5101 | 16 |
2006-09-11 | 5165 | 5173 | 9 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
GEL | 0 | 65000 Gal | 80000 | FRAC:SAND/GEL WATER |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1989 | CEMCO OPERATING INC | 15871.00 | 0.00 | 255 |
1990 | CEMCO OPERATING INC | 4853.00 | 0.00 | 270 |
1992 | CEMCO OPERATING INC | 0.00 | 0.00 | 0 |
1994 | CEMCO OPERATING INC | 1950.00 | 0.00 | 365 |
1996 | CEMCO OPERATING INC | 0.00 | 0.00 | 0 |
1997 | CEMCO OPERATING INC | 0.00 | 0.00 | 365 |
1998 | CEMCO OPERATING INC | 0.00 | 0.00 | 365 |
1999 | CENTURY WELL SERVICE | 63.00 | 0.00 | 365 |
2000 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2001 | CEMCO OPERATING INC | 56.00 | 0.00 | 365 |
2002 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2003 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2004 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2005 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2006 | CENTURY WELL SERVICE | 0.00 | 0.00 | 365 |
2007 | BROAD STREET SERV LLC | 56.00 | 0.00 | 365 |
2008 | BROAD STREET SERV LLC | 258.00 | 0.00 | 365 |
2009 | BROAD STREET SERV LLC | 434.00 | 0.00 | 365 |
2010 | BROAD STREET SERV LLC | 101.00 | 0.00 | 365 |
2011 | BROAD STREET SERV LLC | 0.00 | 0.00 | 0 |
2012 | BROAD STREET SERV LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1989 | CEMCO OPERATING INC | Brine | 560 | 255 |
1990 | CEMCO OPERATING INC | Brine | 540 | 270 |
1992 | CEMCO OPERATING INC | Brine | 0 | 0 |
1994 | CEMCO OPERATING INC | Brine | 0 | 365 |
1996 | CEMCO OPERATING INC | Brine | 0 | 0 |
1997 | CEMCO OPERATING INC | Brine | 45 | 365 |
1998 | CEMCO OPERATING INC | Brine | 0 | 365 |
1999 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2000 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2001 | CEMCO OPERATING INC | Brine | 0 | 365 |
2002 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2003 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2004 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2005 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2006 | CENTURY WELL SERVICE | Brine | 0 | 365 |
2007 | BROAD STREET SERV LLC | Brine | 0 | 365 |
2008 | BROAD STREET SERV LLC | Brine | 50 | 365 |
2009 | BROAD STREET SERV LLC | Brine | 80 | 365 |
2010 | BROAD STREET SERV LLC | Brine | 0 | 365 |
2011 | BROAD STREET SERV LLC | Brine | 60 | 0 |
2012 | BROAD STREET SERV LLC | Brine | 120 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1203266279 | 2013-10-22 0:00 | AM | No Violations | 0.50 |
-1315370326 | 2013-10-25 0:00 | PB | No Violations | 8.00 |
-1639818049 | 2013-10-15 0:00 | PB | No Violations | 3.00 |
-1911991838 | 2011-9-6 0:00:0 | PW | No Violations | 1.00 |
-1912504316 | 2013-10-17 0:00 | AM | No Violations | |
-676661496 | 2013-10-10 0:00 | PB | No Violations | 2.00 |
-694666386 | 2004-12-27 0:00 | PW | No Violations | |
-711616392 | 2013-10-22 0:00 | PB | No Violations | 3.00 |
0633202580 | 2013-10-15 | Administrative Inspection | No Violations | I received a phone call from Mr. Ed Butler at 12:37 PM. He stated that they could not get the packer on this well to move to the bottom of the hole. They were at about 2700 ft. I told them that they needed to get to the bottom of the hole in order to set an adequate bottom hole plug. I suggested that the packer may have to be milled out. |
0655834719 | 2015-09-29 | Final Restoration | No Violations | Location has met 1509.072 B requirements. |
0676661496 | 2013-10-10 | Plug / Plug Back | No Violations | Crew was pulling tubing at the time of inspection. It was being difficult to pull. Spoke with Mr. Kenny OBrian from Broad Street and Donnie from Knox Energy. We discussed plugging procedure. |
0694666386 | 2004-12-27 | Production Wells | No Violations | Inspection this day found well shared with 8491, being metered together with current chart, not turning any production in for it but way up behind house and cant get to - may be house gas also, IDs good on 100 bbl tank, fair to good dike |
0711616392 | 2013-10-22 | Plug / Plug Back | No Violations | Witnessed the bottom hole plug being set. The bottom of the tubing was set at 4994 ft. A 30 sack plug was set at this depth. |
1015455725 | 2013-10-24 | Plug / Plug Back | No Violations | Showed up on site and no one was there. I called Mr. Donnie Strange and he stated that plugging will take place the next day. |
1203266279 | 2013-10-22 | Administrative Inspection | No Violations | Received phone call from Donnie from Knox Energy. He stated that they first tried to rip at 3800 ft, and the first telegraph they got was at 3000 ft. After consulting with Inspector Pat Shreve, I told them that they could rip there, pull the pipe, and run tubing back down to that depth and set a rip plug there to cover up the Big Lime. |
1315370326 | 2013-10-25 | Plug / Plug Back | No Violations | Witnessed the setting of the Lime plug, Berea plug, the bottom of surface plug and the surface plug. The Lime plug circulated. The others did not circulate fluid but pressure was observed on the backside during pumping. A bridge was set for the surface plug. Fluid level was 6.5 seconds down. Well was cemented from there to surface. |
1315387920 | 2011-09-06 | Production Wells | Violations Noted | Inspection this day due to complaint by landowner, Mr. Mike Whited. Says well has not produced in long time and black plastic line not buried, as required in lease, on his property. Found well standing idle, cedar tree growing up into it and could barely see well. Wellhead, casing rotted thru and sitting at angle - will need to be fixed to produce but found no odor - well not leaking. Valves shut - last annual production reported for 2010 but this is mistake - not possible well produced in 2010 and landowner verifies this. Says he has not received royalties since he moved in @2004. No IDs at well - required. Tanks have good IDs, chart in meter has no date, says it is for Yaeger #1, #2. Well needs put in production, IDs posted. |
1334653183 | 2011-11-07 | Production Wells | No Violations | Inspection this day found Broad Streets service rig set up on well. They are getting a water truck to dump water down tubing to see if well will circulate. It may have a hole in casing as the other Yaeger well does. Later in day the pump truck had to leaveand they did not get well pressure tested. |
1639818049 | 2013-10-15 | Plug / Plug Back | No Violations | It was reported to me that that there was a packer on the end of the tubing. It got caught on a hole in the casing and the tubing had to be shot off. During my visit the service rig crew was attempting to beat the packer down to the bottom of the well using the stem and jars. They were at a depth of 2100 ft. |
1911991838 | 2011-09-06 | Production Wells | No Violations | FOLLOW UP TO NOV # 1315387920 Inspection this day due to complaint by landowner, Mr. Mike Whited. Says well has not produced in long time and black plastic line not buried, as required in lease, on his property. Found well standing idle, cedar tree growing up into it and could barely see well. Wellhead, casing rotted thru and sitting at angle - will need to be fixed to produce but found no odor - well not leaking. Valves shut - last annual production reported for 2010 but this is mistake - not possible well produced in 2010 and landowner verifies this. Says he has not received royalties since he moved in @2004. No IDs at well - required. Tanks have good IDs, chart in meter has no date, says it is for Yaeger #1, #2. Well needs put in production, IDs posted. |
1912504316 | 2013-10-17 | Administrative Inspection | No Violations | Andy Thomas called and the Rig was beating on packer with jars to drive to bottom. |
633202580 | 2013-10-15 0:00 | AM | No Violations | 0.50 |
655834719 | 2015-9-29 0:00: | FR | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1315387920 | US-OH-108976 | 2011-09-07 | Failure to legibly identify well | |
1315387920 | US-OH-108977 | 2011-09-07 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]