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34-167-29477

Well Details

Well ID: 34-167-29477
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Country: United States
State: Ohio
County: Washington
Municipality: Warren Township
Operator Name: HEINRICH ENTERPRISES INC DBA W
Well Pad ID:
Farm/Lease Name: SULLIVAN # 2
License Status: Producing
License Date: 2000-10-13
Spud Date: 2000-10-20
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 2000-10-29
Well Total Depth: 6318.00 ft
Configuration: Vertical
Latitude: 39.420000
Longitude: -81.510000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2000-10-13 3793 ENERGY SEARCH INC Proposed Formation CLINTON/MEDINA Issued Date 10/13/00 Expired Date 10/13/01 6:00:00 AM
Original Spud 2000-10-20 RBDMS Rec
Completed 2000-10-29 RBDMS Rec
Reached Total Depth 2000-10-29 RBDMS Rec
Completion Report Received 2001-01-22 RBDMS Rec
Construction Permit Expires 2001-10-13 RBDMS Rec
Change of Owner 2008-02-27 Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
Change of Owner 2015-11-04 Operator changed from 7578, ENERVEST OPERATING LLC to 2007, HEINRICH ENT INC/WASHINGTON OP
Record Last Modified 2015-11-04 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2001-03-23 6063 6085 21
2001-03-23 6177 6187 21
6063 6085 21
6177 6187 21
6063 6085 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1700 Bbl 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2000 ENERGY SEARCH INC 2330.00 0.00 0
2001 ENERGY SEARCH INC 17367.00 0.00 365
2002 ENERGY SEARCH INC 9382.00 0.00 365
2003 ENERGY SEARCH INC 6579.00 0.00 365
2004 ENERGY SEARCH INC 5153.00 0.00 365
2005 ENERGY SEARCH INC 2095.00 0.00 365
2006 ENERGY SEARCH INC 2222.00 0.00 365
2007 ENERGY SEARCH INC 2182.00 0.00 344
2008 EXCO - NORTH COAST ENERGY INC 1329.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 1943.00 0.00 365
2010 ENERVEST OPERATING LLC 2489.00 0.00 365
2011 ENERVEST OPERATING LLC 2202.00 0.00 0
2012 ENERVEST OPERATING LLC 2355.00 0.00 366
2013 ENERVEST OPERATING LLC 1845.00 0.00 365
2014 ENERVEST OPERATING LLC 1691.00 0.00 365
2015 ENERVEST OPERATING LLC 1160.00 0.00 273
2016 HEINRICH ENTERPRISES INC DBA W 1365.00 0.00 365
2017 HEINRICH ENTERPRISES INC DBA W 716.00 0.00 365
2018 HEINRICH ENTERPRISES INC DBA W 73.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2000 ENERGY SEARCH INC Brine 54
2001 ENERGY SEARCH INC Brine 24 365
2002 ENERGY SEARCH INC Brine 82 365
2003 ENERGY SEARCH INC Brine 82 365
2004 ENERGY SEARCH INC Brine 0 365
2005 ENERGY SEARCH INC Brine 0 365
2006 ENERGY SEARCH INC Brine 0 365
2007 ENERGY SEARCH INC Brine 0 344
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 ENERVEST OPERATING LLC Brine 0 92
2010 ENERVEST OPERATING LLC Brine 63 365
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 366
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 365
2015 ENERVEST OPERATING LLC Brine 107 273
2016 HEINRICH ENTERPRISES INC DBA W Brine 0 365
2017 HEINRICH ENTERPRISES INC DBA W Brine 0 365
2018 HEINRICH ENTERPRISES INC DBA W Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1566244116 2017-2-10 0:00: PW No Violations 1.00
-1608361063 2002-1-2 0:00:0 PL No Violations
0537569818 2017-01-04 Administrative Inspection No Violations I called and spoke with Sam Johnson about this well. I explained that the well was not eggregiously leaking but it was something that needed fixed and not to make a speacial trip but to fix it the next time he was there.
0640519776 2017-07-20 Production Wells No Violations The inspection this day revealed that this well is equipped with a 4 1/2 inch diameter production casing, 8 5/8 inch diameter surface casing, and 1 1/2 inch diameter production tubing. The valves on the wellhead are open at the time of inspection. There is a 100 barrel steel tank inside the tank battery. There are no issues to report at this time and the well is in production at the time of inspection.
1473239715 2017-01-04 Production Wells Violations Noted I was accompanied by Jake a Hydrologist for the State of Ohio and Nathan Lane Emergency Response team member as I inspected this well. I spoke with the land owner who stated they receive well gas from the well, before the inspection. The well was indeed producing house gas. The casing head was leaking it was noted because there was water around the casing head and gas was bubbling out. This was presumably caused from gas leaking around the bull plug on the casing head, but could not be seen. The tank sounded empty and there was a new chart installed in the meter. I called the company and made them aware of the leak and that it would need corrected. I did not give them a date just to do it the next time they were out there. I spoke with Sam Johnson production manager for Heirich Ent Inc/Washington OP.
1566244116 2017-02-10 Production Wells No Violations The bubbling around the 8.625 inch diameter casing head could no longer be detected. Violation is resolved.
1608361063 2002-01-02 Preliminary Restoration No Violations
537569818 2017-1-4 0:00:0 AM No Violations 0.30
640519776 2017-7-20 0:00: PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1473239715 US-OH-113584 2017-01-31 9-9-05(A)1 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[9]

References