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| Well ID: 34-167-29565 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: <County> | |
| Municipality: | |
| Operator Name: TRIAD HUNTER LLC | |
| Well Pad ID: | |
| Farm/Lease Name: REYNOLDS UNIT | |
| License Status: Final Restoration | |
| License Date: 2017-05-26 | |
| Spud Date: 2003-10-18 | |
| Spud Drilling Contractor: WARREN DRLG | |
| Final Drill Date: 2003-10-26 | |
| Well Total Depth: 6280.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.370000 | |
| Longitude: -81.290000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2003-07-16 | Proposed Formations:BIG LIME, Issued Date:7/16/2003, Expired Date:7/15/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW |
| APP | 2003-09-19 | Proposed Formations:DEVONIAN SHALE THRU LOCKPORT, Issued Date:9/19/2003, Expired Date:9/18/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW |
| Original Spud | 2003-10-18 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
| Completed | 2003-10-26 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
| Reached Total Depth | 2003-10-26 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
| Completion Report Received | 2004-03-10 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
| Change of Owner | 2010-03-24 | Operator changed from 2348, TRIAD RESOURCES INC to 8610, TRIAD HUNTER LLC |
| APP | 2017-05-26 | Proposed Formations:ORISKANY SANDSTONE/WILLIAMSPORT SANDSTONE, Issued Date:5/26/2017, Expired Date:5/26/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2017-10-16 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
| Record Last Modified | 2018-04-17 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
| Construction Permit Expires | 2019-05-26 | RBDMS Rec. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2004-05-18 | 5138 | 5142 | 16 |
| 2004-05-18 | 6095 | 6098 | 12 |
| 5138 | 5142 | 16 | |
| 6095 | 6098 | 12 | |
| 5138 | 5142 | 16 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| ACID | 15 | 2500 Gal | 0 | |||
| H2O | 15 | 2260 Bbl | 20000 | 1500 GALLONS HCL ACID |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2005 | TRIAD RESOURCES INC | 3808.00 | 420.00 | 365 |
| 2006 | TRIAD RESOURCES INC | 1694.00 | 94.00 | 365 |
| 2007 | TRIAD RESOURCES INC | 1992.00 | 128.00 | 365 |
| 2008 | TRIAD RESOURCES INC | 1252.00 | 89.00 | 365 |
| 2009 | TRIAD RESOURCES INC | 600.00 | 42.00 | 365 |
| 2010 | TRIAD RESOURCES INC | 82.00 | 10.00 | 365 |
| 2011 | TRIAD HUNTER LLC | 96.00 | 0.00 | 365 |
| 2012 | TRIAD HUNTER LLC | 36.00 | 0.00 | 366 |
| 2013 | TRIAD HUNTER LLC | 0.00 | 0.00 | 365 |
| 2014 | TRIAD HUNTER LLC | 0.00 | 0.00 | 0 |
| 2015 | TRIAD HUNTER LLC | 0.00 | 0.00 | 0 |
| 2016 | TRIAD HUNTER LLC | 0.00 | 0.00 | 0 |
| 2017 | TRIAD HUNTER LLC | 1082.00 | 113.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2005 | TRIAD RESOURCES INC | Brine | 2736 | 365 |
| 2006 | TRIAD RESOURCES INC | Brine | 0 | 365 |
| 2007 | TRIAD RESOURCES INC | Brine | 0 | 365 |
| 2008 | TRIAD RESOURCES INC | Brine | 0 | 365 |
| 2009 | TRIAD RESOURCES INC | Brine | 0 | 365 |
| 2010 | TRIAD RESOURCES INC | Brine | 0 | 365 |
| 2011 | TRIAD HUNTER LLC | Brine | 0 | 365 |
| 2012 | TRIAD HUNTER LLC | Brine | 0 | 366 |
| 2013 | TRIAD HUNTER LLC | Brine | 0 | 365 |
| 2014 | TRIAD HUNTER LLC | Brine | 0 | 0 |
| 2015 | TRIAD HUNTER LLC | Brine | 0 | 0 |
| 2016 | TRIAD HUNTER LLC | Brine | 0 | 0 |
| 2017 | TRIAD HUNTER LLC | Brine | 0 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1062797625 | 2011-9-19 0:00: | PW | No Violations | 0.50 |
| -1850735169 | 2009-4-30 0:00: | PW | No Violations | |
| -2097636114 | 2009-7-30 0:00: | PW | No Violations | |
| -2111633714 | 2017-7-5 0:00:0 | PW | No Violations | 1.00 |
| -396508704 | 2003-10-22 0:00 | DD | No Violations | |
| 0105845886 | 2016-02-08 | Production Wells | Violations Noted | Upon inspection, it was observed that this well is capable of production, but is currently idle. The well consists of a pumping unit standing over 4.5 production casing with a 4-2 swedge, 2 ball valve, and associated steel flow lines. The pumping unit is no longer in use as the rods and tubing have been pulled from the well. The tank battery consists of a 210 bbl production tank, separator, drip, and containment dike. The meter run has been pulled. Legible and correct ID information is posted on the tank. Photos were taken of the location. Production records indicate that the well has not produced oil or gas since 2012. The well shall be plugged and abandoned. Triad Hunter LLC shall submit a written plugging schedule within 30 days to Inspector Lynn Parkins at 5880 Memory Rd. Zanesville, OH 43701 and plug the well within 180 days. Triad Hunter LLC will be notified if the plugging schedule is approved or denied. |
| 0396508704 | 2003-10-22 | Drill / Deepen / Reopen | No Violations | Checked BOP to make sure would hold pressure - passed 15 minute test at 575# - 3 hours |
| 105845886 | 2016-2-8 0:00:0 | PW | No Violations | 1.50 |
| 1062797625 | 2011-09-19 | Production Wells | No Violations | Inspection this day found pumpjack not sitting on well and head has been removed. Well is tied into sales line and valves open. Proper ID at tank battery, current chart in meter, good dike. |
| 1066826683 | 2003-09-13 | Drill / Deepen / Reopen | No Violations | Test BOP to determine if will hold a blow out - |
| 1093615036 | 2004-08-27 | Preliminary Restoration | No Violations | Inspection this day found drill site reclaimed, still wet but is swampy area, grass growing, Tank along road, good IDs, good dike |
| 1242229240 | 2016-02-08 | Production Wells | No Violations | Upon inspection, it was observed that this well is capable of production, but is currently idle. The well consists of a pumping unit standing over 4.5 production casing with a 4-2 swedge, 2 ball valve, and associated steel flow lines. The pumping unit is no longer in use as the rods and tubing have been pulled from the well. The tank battery consists of a 210 bbl production tank, separator, drip, and containment dike. The meter run has been pulled. Legible and correct ID information is posted on the tank. Photos were taken of the location. |
| 1402031855 | 2020-5-21 0:00: | FR | No Violations | 0.80 |
| 1434379317 | 2015-06-15 | Production Wells | No Violations | Performed an inspection on this well in response to a landowner complaint of nonproduction. Upon inspection, it was observed that this well is capable of production, but is currently shut in. The well consists of a pumping unit standing over 4.5 casing with a 4-2 swedge, 2 ball valve, and associated steel flow lines. The motor and the horsehead/bridle have been pulled from the pumping unit and the tubing/rods have been pulled from the well. The well has not shown production since 2012. No pollution or contamination issues were observed at the well or tank battery location. The tank battery consists of a 210 bbl production tank, mechanical separator, and containment dike. Legible and correct ID information is posted on the production tank. I will contact Triad Hunter LLC and inquire about why this well is not producing and what their plans are for either producing or plugging the well. |
| 1509377816 | 2017-10-16 | Plug / Plug Back | No Violations | I was on location with Patchwork Oil and Gas of West Virginia this day to plug this well. Patch work had set a bottom hole plug on 10/13/17 without me due to time issues. The bottom hole plug was from 5446 to 4888 and Patchwork tagged the top of the plug at 4888 on 10/16/17. Patchwork then ripped pipe off at around 2385 feet and pulled 3 joints of the 4 1/2 inch diameter production casing to be at around 2216 feet. Formation was on site to set the rest of the plugs through the 4 1/2 inch diameter production casing. Formation set a Gordon Sand/Rip Plug plug (2216-200 feet), a bottom of surface plug (2700-2400 feet), a Berea Sandstone plug (1538-1320 feet), a bottom of surface plug (1864-1664 feet), and a surface plug (150-0 feet). Patchwork then pulled the 4 1/2 inch diameter production casing from the hole and the hole was topped off with cement to surface. Patchwork pulled a total of 2385 feet of 4 1/2 inch diameter production casing from the hole. This well is now plugged to surface and all violations have been resolved with this well. |
| 1850735169 | 2009-04-30 | Production Wells | No Violations | Inspection this day found well producing with jack, current chart in meter, good IDs, good dike. |
| 2097636114 | 2009-07-30 | Production Wells | No Violations | Inspection this day found service rig on well - pulling pump. Well should be back going soon. Good IDs at tank, good dike. |
| 2111633714 | 2017-07-05 | Production Wells | No Violations | The inspection this day revealed that this well is equipped with a pumping unit and a 4 to 2 inch diameter swage. The rods and tubing have been removed from this well. The valves on the wellhead are shut at the time of inspection. No production equipment was found at the site at the time of inspection. Triad currently has a permit to plug and abandon this well and plans on doing it this summer of 2017. There has been no resolution to the issue on this well and the well is idle at the time of inspection. |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0105845886 | US-OH-101112 | 2016-02-29 | Well shall be plugged |
For data sources see[9]