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Well ID: 34-167-29622 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Barlow Township | |
Operator Name: HANGER MARVIN | |
Well Pad ID: | |
Farm/Lease Name: HANGER (WOODRUFF) | |
License Status: Producing | |
License Date: 2006-11-27 | |
Spud Date: 2006-12-03 | |
Spud Drilling Contractor: FALCON DRLG | |
Final Drill Date: 2010-11-03 | |
Well Total Depth: 1345.00 ft | |
Configuration: Vertical | |
Latitude: 39.440000 | |
Longitude: -81.640000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-11-27 | Proposed Formations:MAXTON, Issued Date:11/27/2006, Expired Date:11/27/2007 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Construction Permit Expires | 2007-11-27 | |
Change of Owner | 2009-11-30 | Operator changed from 3045, SUNNY SHORES OF OHIO INC to 8583, HANGER MARVIN |
Reached Total Depth | 2010-11-03 | |
Completion Report Received | 2010-11-15 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | SUNNY SHORES OF OHIO INC | 0.00 | 0.00 | 0 |
2008 | SUNNY SHORES OF OHIO INC | 0.00 | 0.00 | 0 |
2013 | HANGER MARVIN | 560.00 | 0.00 | 365 |
2014 | HANGER MARVIN | 415.00 | 0.00 | 365 |
2015 | HANGER MARVIN | 397.00 | 0.00 | 365 |
2016 | HANGER MARVIN | 290.00 | 0.00 | 365 |
2017 | HANGER MARVIN | 300.00 | 0.00 | 365 |
2018 | HANGER MARVIN | 158.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | SUNNY SHORES OF OHIO INC | Brine | 0 | 0 |
2008 | SUNNY SHORES OF OHIO INC | Brine | 0 | 0 |
2013 | HANGER MARVIN | Brine | 0 | 365 |
2014 | HANGER MARVIN | Brine | 0 | 365 |
2015 | HANGER MARVIN | Brine | 0 | 365 |
2016 | HANGER MARVIN | Brine | 0 | 365 |
2017 | HANGER MARVIN | Brine | 0 | 365 |
2018 | HANGER MARVIN | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-141219021 | 2010-7-26 0:00: | PW | No Violations | 1.50 |
-1700214129 | 2010-9-3 0:00:0 | AM | No Violations | 0.20 |
-1866729090 | 2010-8-23 0:00: | DD | No Violations | 1.00 |
-1975805995 | 2009-1-20 0:00: | PW | No Violations | |
-2010729188 | 2009-4-1 0:00:0 | AM | No Violations | |
-288145649 | 2008-9-19 0:00: | PW | No Violations | |
-620102989 | 2008-11-3 0:00: | PW | No Violations | |
-847829137 | 2008-9-8 0:00:0 | CT | No Violations | |
-955638170 | 2008-7-21 0:00: | PL | No Violations | |
0141219021 | 2010-07-26 | Production Wells | No Violations
- will keep me informed. | |
0288145649 | 2008-09-19 | Production Wells | No Violations | Just talked to Pete Monueau, pumper - he said rig has been on well, now producing, has run tubing and turned into line, but says needs rods, jack to make any gas. I did field inspection and found well is NOT producing, valves closed, still no IDs. |
0620102989 | 2008-11-03 | Production Wells | No Violations | No change. Well still not in production, no reclamation, no IDs at all. Ready for C. O.s. Pictures. |
0847829137 | 2008-09-08 | Completion Testing | No Violations | Bobby Andersons rig on location this day swabbing well - ran tubing last week and trying to get well into production. Looks like it will need rods and pump jack - drilled too deep, they say. |
0955638170 | 2008-07-21 | Preliminary Restoration | Violations Noted | Inspection this day found well drilled 12/06 is hooked to sales line, valve open but well only has 4.5 casing in it. Location has been smoothed out, all debris removed but still needs seeded and mulched. Cannot pass PRD today. 9/19/2008- Just talked to Pete and he said well was producing, have ran tubing but he says it will need rods and jack - but is now turned into line. I went and checked and it is NOT producing, valves closed, no IDs. 11/3 - No change - valve completely shut now, no IDs or restoration. Restoration is not complete. Location needs seeded and mulched, ground smoothed (edge starting to form considerable slip). Post IDs. Failure to comply may result in bond forfeiture. 7/10- Well logged, too deep, making water, will have to plug bottom off. 12/10 - well capable of producing - landowner is satified with reclamation - will continue to watch slip. |
0956064106 | 2007-07-19 | Preliminary Restoration | No Violations | Location not cleaned up - well not producing. Will talk to Pete, then if no results, write NOVs. |
1246982864 | 2009-07-07 | Administrative Inspection | No Violations | Talked with Mark Epler, pumper. He says they have pulled the pump in McDougal well so Terry Sampson can have gas over the winter. Cant get ahead of Jim Ray to find out where he can go to get work done. He says they have to worked on the 3 new wells they committed to having completed by 7/31 - last night 1st day service rig has worked. Expects to have this well finished by 7/31, Jim very slow to pay/respond by phone and that makes it hard to get work done. Called back later this day to say Jim had called him back and were getting the pump work done. |
1700214129 | 2010-09-03 | Administrative Inspection | No Violations | Bobby Anderson called to say they still cant get down the hole with his service rig, working up a new plan. |
1866729090 | 2010-08-23 | Drill / Deepen / Reopen | No Violations | Inspection this day found service rig on location, setting a temporary plug on bottom to try and seal off water. Crew put gunny sack in well, pushed it down to 1310 then several buckets of river gravel on top of it - believes will seal off water. Today, gravel is stuck up the hole and they are going for bigger, heavier tools to push it down, water standing 300 in hole. Talked to Bobby about remaining violations and how to resolve, other Sunny Shores wells and who would take them over. |
1919628759 | 2009-06-01 | Production Wells | No Violations | Inspection this day with Supervisor Stonerock found well still not producing. Well tied into sales line but valves shut at wells, line only continues a few feet before ending. No IDs, tank not hooked up, slip on lease road is getting alittle worse. Lease road to well so wet and untravelable that cant drive in. |
1975805995 | 2009-01-20 | Production Wells | Violations Noted | Added idle well to list of violations. Plug or produce. Post IDs. Failure to comply may result in bond forfeiture. Well now capable of producing. Good IDs. |
1976476221 | 2008-09-19 | Production Wells | No Violations | Called Pete and he said well was turned into line. Went to well and checked and it is NOT turned into line, valves shut, Pete says needs rods, jack. Still no IDs. |
2010729188 | 2009-04-01 | Administrative Inspection | No Violations | Met with Sunny Shores owner Jim Ray regarding the numberous NOVs and pending C.O.s. He present letter stating his plans for completion of all 4 wells, said the royalty owners would be caught up soon, and has hired another person to operate the field from Ohio - also a new pumper. Jim made numerous commitments and we will be monitoring to see that he executes them. Also present was Jay Cheslock. |
2122944420 | 2008-11-03 | Production Wells | No Violations | Inspection found no change. Valves completely shut. No IDs or reclamation has been done. Flow line goes staight uphill and ties into another well. |
956064106 | 2007-7-19 0:00: | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0955638170 | US-OH-130909 | 2008-07-22 | Failure to restore land surface within 9 mos. (CHANGE) (REPLACE) | |
0955638170 | US-OH-130910 | 2008-07-22 | Failure to legibly identify well | |
1975805995 | US-OH-119967 | 2009-01-20 | Failure to legibly identify well | |
1975805995 | US-OH-119968 | 2009-01-20 | Well shall be plugged |
For data sources see[8]