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Well ID: 34-167-29629 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Aurelius Township | |
Operator Name: GENESIS RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: B & N COAL/MM | |
License Status: Producing | |
License Date: 2006-12-20 | |
Spud Date: 2007-04-03 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 2007-04-09 | |
Well Total Depth: 2100.00 ft | |
Configuration: Vertical | |
Latitude: 39.590000 | |
Longitude: -81.420000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-12-20 | Proposed Formations:BEREA-GORDON, Issued Date:12/20/2006, Expired Date:12/20/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2007-04-09 | |
Reached Total Depth | 2007-04-09 | |
Completion Report Received | 2007-07-17 | |
Construction Permit Expires | 2007-12-20 | |
Change of Owner | 2015-07-10 | Operator changed from 6288, ALLIANCE PETROLEUM CORPORATION to 9086, GENESIS RESOURCES LLC |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2007-10-31 | 1636 | 1684 | 10 |
2007-10-31 | 1538 | 1546 | 20 |
1538 | 1546 | 20 | |
1636 | 1684 | 10 | |
1758 | 1804 | 10 | |
1889 | 1937 | 20 | |
1538 | 1546 | 20 | |
2007-10-31 | 1889 | 1937 | 20 |
2007-10-31 | 1758 | 1804 | 10 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2000 Gal | 0 | GANTZ, THIRTY FOOT, & GORDON SANDS WERE INVOLVED IN THIS FRAC TREATMENT. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | ALLIANCE PETROLEUM CORPORATION | 1027.00 | 14.00 | 365 |
2013 | ALLIANCE PETROLEUM CORPORATION | 1169.00 | 28.00 | 365 |
2014 | ALLIANCE PETROLEUM CORPORATION | 931.00 | 6.00 | 365 |
2015 | ALLIANCE PETROLEUM CORPORATION | 595.00 | 8.00 | 181 |
2016 | GENESIS RESOURCES LLC | 1098.00 | 6.00 | 298 |
2017 | GENESIS RESOURCES LLC | 895.00 | 0.00 | 301 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 365 |
2013 | ALLIANCE PETROLEUM CORPORATION | Brine | 10 | 365 |
2014 | ALLIANCE PETROLEUM CORPORATION | Brine | 9 | 365 |
2015 | GENESIS RESOURCES LLC | Brine | 0 | 184 |
2016 | GENESIS RESOURCES LLC | Brine | 0 | 298 |
2017 | GENESIS RESOURCES LLC | Brine | 0 | 301 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1368049347 | 2007-8-24 0:00: | PL | No Violations | |
-1718684839 | 2009-9-16 0:00: | PW | No Violations | |
-1781379572 | 2017-4-11 0:00: | PW | No Violations | 1.20 |
-2061066357 | 2020-8-26 0:00: | PW | No Violations | 0.40 |
-907720118 | 2017-1-25 0:00: | PW | No Violations | 1.00 |
0201587502 | 2017-01-12 | Production Wells | No Violations | The gas leak at the wellhead was corrected, however no work on the brine scald was completed at the date and time of this inspection. |
0340655864 | 2016-12-27 | Administrative Inspection | No Violations | Called company to notify them of compliance notice and explain my findings. They said they would start right away cleaining up the spill. |
0512527107 | 2017-01-27 | Production Wells | No Violations | Follow up on this well found that the 2 inch was still leaking. I again called Andrew and this time I explained that I would wait here till someone came to fix the leak. He called back and said that his pumper was in West Virginia and couldnt get there until near 3. |
0907720118 | 2017-01-25 | Production Wells | No Violations | This follow up inspection found that the gas leaking from the 1/4 inch pipe at the well-head was corrected. However the brine contamination in the dike and outside the dike was still untouched. The 2 inch diameter pipe where a plug is screwed into the tee was found to be actively leaking. I called Andrew with Genesis Resources to find out what was going on. He said that the pumper stated it was cleaned up. I informed him that it wasnt and that the pipe was actively leaking. He said that he would get someone on it right now. |
0994956221 | 2016-12-27 | Production Wells | Violations Noted | When I pulled off the road I could smell natural gas. As I neared the well I could hear the leak as well as smell it stronger. Inspection of the well found a plug to be leaking in the end of a 1/4 valve. Inspection of the tank battery found 2-210 barrel tanks and 2 small 40 barrel plastic tanks. The dike also contained 2 separators. The lower corner of the dike by a tank drain contained water. The soil in this area looked different. This was by the tank labeled 995. This water was noted on the outside of the dike going toward the road ditch. There was a swath of ground approximately 18 wide void of vegetation where the water from the dike was running. A field test of this water with Quantabs maxed out the low range ones inside and outside the dike. I then tested with high range Quantabs from Lot # 4430 which also maxed out. These high level Quantabs tested to 6171 PPM chlorides at 8.6. Pictures were taken. Gas leak needs corrected, brine contaminated soils need removed and disposed of in a proper manner. Uncontaminated soil will be needed to replace contaminated soil removed and location needs seeded and mulched to establish vegetation. |
1368049347 | 2007-08-24 | Preliminary Restoration | No Violations | Inspection this day found well producing with jack, tanks for 6 wells, has good IDs, good dike, current chart in meter, location has been reclaimed, grass growing, lookds good! |
1525710543 | 2018-05-01 | Production Wells | No Violations | I am accompanied by Regional Supervisor Dan Goins. Our inspection found the well is equipped with a pumping unit. The pumping unit has no motor or engine. The tank battery is equipped with two 210 barrel tanks, two 50 barrel plastic tanks, two separators and two orifice meters. |
1718684839 | 2009-09-16 | Production Wells | No Violations | Inspection this day found well producing with jack, tank has ID sticker but no info - call secretary and asked her to get some better pens for the pumpers, current chart in meter, good dike. |
1781379572 | 2017-04-11 | Production Wells | No Violations | Violations have been resolved. Site is remediated and gas leak has been fixed. |
201587502 | 2017-1-12 0:00: | PW | No Violations | 1.50 |
340655864 | 2016-12-27 0:00 | AM | No Violations | 0.30 |
512527107 | 2017-1-27 0:00: | PW | No Violations | 1.50 |
994956221 | 2016-12-27 0:00 | PW | No Violations | 2.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0994956221 | US-OH-131417 | 2017-01-06 | 9-1-07 | Well operation causing pollution and contamination |
0994956221 | US-OH-131418 | 2017-01-06 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
0994956221 | US-OH-131419 | 2017-01-06 | NONE(B) | Dike or pit not able to prevent escape of brine or other wastes |
0994956221 | US-OH-131420 | 2017-01-06 | NONE[C] | Failure to keep dike or pit free of brine or other wastes |
For data sources see[9]