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Well ID: 34-167-29697 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Muskingum Township | |
Operator Name: OLD SOUTH OIL LLC | |
Well Pad ID: | |
Farm/Lease Name: T. LOVE ETAL | |
License Status: Producing | |
License Date: 2010-10-22 | |
Spud Date: 2010-11-14 | |
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC | |
Final Drill Date: 2010-11-17 | |
Well Total Depth: 1800.00 ft | |
Configuration: Vertical | |
Latitude: 39.470000 | |
Longitude: -81.490000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2010-10-22 | Proposed Formations:BEREA, Issued Date:10/22/2010, Expired Date:10/21/2012 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2010-11-17 | |
Completion Report Received | 2011-01-20 | |
Construction Permit Expires | 2012-10-21 | |
Change of Owner | 2019-05-22 | Operator changed from 7582, KROLL ENERGY LLC to 8390, OLD SOUTH OIL LLC |
Record Last Modified | 2019-05-22 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-05-11 | 1710 | 1718 | 20 |
1710 | 1718 | 20 | |
1710 | 1718 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2010-12-02 | H2O | 20 | 74356 Gal | 40000 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | KROLL ENERGY LLC | 3000.00 | 52.00 | 365 |
2012 | KROLL ENERGY LLC | 2284.00 | 35.00 | 366 |
2013 | KROLL ENERGY LLC | 2200.00 | 0.00 | 365 |
2014 | KROLL ENERGY LLC | 1379.00 | 10.00 | 365 |
2015 | KROLL ENERGY LLC | 1324.00 | 0.00 | 365 |
2016 | KROLL ENERGY LLC | 1200.00 | 0.00 | 365 |
2017 | KROLL ENERGY LLC | 1017.00 | 9.00 | 365 |
2018 | KROLL ENERGY LLC | 983.00 | 11.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | KROLL ENERGY LLC | Brine | 0 | 365 |
2012 | KROLL ENERGY LLC | Brine | 0 | 366 |
2013 | KROLL ENERGY LLC | Brine | 0 | 365 |
2014 | KROLL ENERGY LLC | Brine | 0 | 365 |
2015 | KROLL ENERGY LLC | Brine | 0 | 365 |
2016 | KROLL ENERGY LLC | Brine | 5 | 365 |
2017 | KROLL ENERGY LLC | Brine | 20 | 365 |
2018 | KROLL ENERGY LLC | Brine | 11 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2043372933 | 2010-12-2 0:00: | CT | No Violations | 1.50 |
0068049412 | 2011-06-01 | Preliminary Restoration | No Violations | Inspection this day found well with jack - service rig on location this day running tubing back in. Good IDs at well, tank is big 210 bbl with good IDs, current chart in meter. Reclamation has been done, farmer in this day discing and planting. |
1290004203 | 2010-11-17 | Completion Testing | No Violations | Inspection this morning found Formation cementing 4.5 casing - plug didnt want to latch but finally set and appears good cement job. Drilled 1800 of hole, set 1794 of 4.5 casing. |
2043372933 | 2010-12-02 | Completion Testing | No Violations | Called this day to witness frac of Berea sand - Producers Services on location, fracing with 2000 bbl water and 40,000 sand. Well broke down at 1289 and treated slightly lower. Flow back water will be moved to next well and mixed with fresh for next frac, then Select will eventually haul away. 1st 2 wells are ready to pump - got very little water back and no sand came back. |
68049412 | 2011-6-1 0:00:0 | PL | No Violations | 0.70 |
For data sources see[9]