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Well ID: 34-167-29701 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Muskingum Township | |
Operator Name: OLD SOUTH OIL LLC | |
Well Pad ID: | |
Farm/Lease Name: C. LOVE | |
License Status: Producing | |
License Date: 2010-10-22 | |
Spud Date: 2010-11-10 | |
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC | |
Final Drill Date: 2010-11-12 | |
Well Total Depth: 1845.00 ft | |
Configuration: Vertical | |
Latitude: 39.470000 | |
Longitude: -81.490000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2010-10-22 | Proposed Formations:BEREA, Issued Date:10/22/2010, Expired Date:10/21/2012 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2010-11-12 | |
Completion Report Received | 2011-01-20 | |
Construction Permit Expires | 2012-10-21 | |
Change of Owner | 2019-05-22 | Operator changed from 7582, KROLL ENERGY LLC to 8390, OLD SOUTH OIL LLC |
Record Last Modified | 2019-05-22 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-05-11 | 1717 | 1725 | 20 |
1717 | 1725 | 20 | |
1717 | 1725 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2010-11-23 | H2O | 20 | 78700 Gal | 40000 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | KROLL ENERGY LLC | 289.00 | 20.00 | 365 |
2012 | KROLL ENERGY LLC | 115.00 | 0.00 | 366 |
2013 | KROLL ENERGY LLC | 115.00 | 0.00 | 365 |
2014 | KROLL ENERGY LLC | 100.00 | 0.00 | 365 |
2015 | KROLL ENERGY LLC | 30.00 | 0.00 | 365 |
2016 | KROLL ENERGY LLC | 0.00 | 0.00 | 365 |
2017 | KROLL ENERGY LLC | 0.00 | 0.00 | 365 |
2018 | KROLL ENERGY LLC | 90.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | KROLL ENERGY LLC | Brine | 0 | 365 |
2012 | KROLL ENERGY LLC | Brine | 0 | 366 |
2013 | KROLL ENERGY LLC | Brine | 0 | 365 |
2014 | KROLL ENERGY LLC | Brine | 0 | 365 |
2015 | KROLL ENERGY LLC | Brine | 0 | 365 |
2016 | KROLL ENERGY LLC | Brine | 0 | 365 |
2017 | KROLL ENERGY LLC | Brine | 0 | 365 |
2018 | KROLL ENERGY LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-432962581 | 2011-6-1 0:00:0 | PL | No Violations | 0.70 |
0432962581 | 2011-06-01 | Preliminary Restoration | No Violations | Inspection this day found casing well in production, small compressor nearby, good IDs at well, current chart in meter. Reclamation has been done, farmer in this day discing and planting. |
0728256923 | 2011-02-08 | Completion Testing | No Violations | Met with Bobby Kroll - wells have been completed, started out good and have now sealed themselves off, will produce only small amount of time and then shut down. Have been running tests on production water to see if something in frac went wrong, or if formation is plugged off and how far out from the well bore, or if formation is just depleted. Still waiting to hear from Universal well services as to a treatment to open up the formation again. |
1445211563 | 2010-11-12 | Drill / Deepen / Reopen | No Violations | Called received to say cementing 4.5 casing - arrived in time to see it circulate. No problems. |
1504648565 | 2010-11-23 | Completion Testing | No Violations | Inspection this day found well being fraced in the Berea. 40,000# sand, 2000 bbl water. |
728256923 | 2011-2-8 0:00:0 | CT | No Violations | 2.00 |
For data sources see[9]