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Well ID: 34-167-29742 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Barlow Township | |
Operator Name: ANDERSON BOBBY B | |
Well Pad ID: | |
Farm/Lease Name: NELSON UNIT | |
License Status: Producing | |
License Date: 2014-05-13 | |
Spud Date: 2014-06-09 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 2014-06-18 | |
Well Total Depth: 869.00 ft | |
Configuration: Vertical | |
Latitude: 39.430000 | |
Longitude: -81.640000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-05-13 | Proposed Formations:COW RUN, Issued Date:5/13/2014, Expired Date:5/12/2016 12:00:00 PM, Drilling unit acres:8.7, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2014-06-18 | |
Completion Report Received | 2015-01-14 | |
Construction Permit Expires | 2016-05-12 | |
Record Last Modified | 2017-10-23 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2014-08-04 | GEL | 0 | 45 Lbs | 0 | OTHER | This well is open hole completion and was shot with 45 lbs of Dyno Nobel Gelled Shot to stimulate oil and gas production. The shots were placed from 867' to 845'. 15' of wire line was left in the hole and will be fished out. |
2014-10-02 | GEL | 0 | 45 Lbs | 0 | OTHER | Well was shot with 36 sticks of SPO900 gelled expolosives from 812-827'. Jet Wireline Services was the contractor who shot this well for Mr. Bobby Anderson. |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | ANDERSON BOBBY B | 0.00 | 0.00 | 85 |
2015 | ANDERSON BOBBY B | 0.00 | 8.00 | 85 |
2016 | ANDERSON BOBBY B | 0.00 | 8.00 | 85 |
2017 | ANDERSON BOBBY B | 0.00 | 0.00 | 85 |
2018 | ANDERSON BOBBY B | 0.00 | 0.00 | 85 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | ANDERSON BOBBY B | Brine | 0 | 85 |
2015 | ANDERSON BOBBY B | Brine | 0 | 85 |
2016 | ANDERSON BOBBY B | Brine | 0 | 85 |
2017 | ANDERSON BOBBY B | Brine | 0 | 85 |
2018 | ANDERSON BOBBY B | Brine | 0 | 85 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1516090382 | 2014-6-18 0:00: | CS | No Violations | 3.00 |
-1844062473 | 2014-6-13 0:00: | DD | No Violations | 7.00 |
-1896479921 | 2014-8-4 0:00:0 | DD | No Violations | 6.00 |
-1943150484 | 2014-10-1 0:00: | AM | No Violations | 0.10 |
0143022138 | 2016-01-19 | Production Wells | No Violations | Upon inspection, it was observed that the drilling rig has been removed from the location and a 100 bbl production tank has been set within an earthen dike. The well is in production and consists of 7 surface casing, 4.5 production casing, and 2 production tubing. Due to snowy conditions, I was unable to determine whether the preliminary restoration for the location is satisfactory. I will return to the location this spring to evaluate the preliminary restoration. I was accompanied on this inspection by DOGRM Geologist Jake Glascock. |
1217922092 | 2014-06-10 | Drill / Deepen / Reopen | No Violations | Drive pipe has been set in hole. 21 ft. of 9.875 in. hole was drilled and suitable bedrock was found. A 25 ft. joint of 9.625 in pipe was driven in the hole. 4 ft is sticking above ground. Spoke with Mr. Bobby Anderson on site. Accompanied by Inspector LJ Parkins. |
136044169 | 2020-6-19 0:00: | PL | No Violations | 0.30 |
1401832112 | 2014-06-03 | Drill / Deepen / Reopen | No Violations | The location has been built and the drilling rig is in place. I spoke with Mr. Ben Anderson on site. We discussed the placement of the pit with the contractors. We also discussed the casing program and cement. |
143022138 | 2016-1-19 0:00: | PW | No Violations | 1.00 |
1471251103 | 2014-06-09 | Drill / Deepen / Reopen | No Violations | Drilling rig is stood up and there is one piece of drill pipe with the drill bit on it. The pit was dug, but had no liner in it. Drilling had not been started due to their air compressor being down. I spoke with Mr. Bobby Anderson over the phone. |
1516090382 | 2014-06-18 | Casing String Witnessed | No Violations | Witnessed the cementing of the production string on this well. 769 ft. of 4.5 in. casing was ran in 868 ft. of 6.25 in. hole. Good circulation was achieved and kept throughout the job. After the plug landed the pipe was tested at 750 psi. and it passed. |
1844062473 | 2014-06-13 | Drill / Deepen / Reopen | No Violations | Witnessed the running and cementing of 300 of 7 surface casing. Good circulation was witnessed and the hole was conditioned with cottonseed hulls as LCM. Cement was run with a 2% mixture of calcium chloride. Good cement returnns were witnessed at the surface. The cement dropped approximately 1 in the first 10 minutes after cementing. Formation Cementing topped off the cement back to surface and it stayed. A pressure test will be performed on Monday, 6/16/2014. |
1896479921 | 2014-08-04 | Drill / Deepen / Reopen | No Violations | Visited this well location to witness well logging and stimulation activities. Timco Well Services was on location to run a gamma/neutron log to find which zones to perforate. A cement bond log was also run to verify the top of cement (TOC). TOC was found to be at 345 below surface. The well was shot from 867 to 845 with 45 lbs of Dyno Nobel RDX/PETN gelled wireline explosives. 15 of wire was left in the well and will be fished out by Mr. Bobby Andersons service rig. |
1943150484 | 2014-10-01 | Administrative Inspection | No Violations | Mr. Bobby Anderson contacted me via phone call at 2:00 pm and informed me that he has scheduled JT Well Surveys to log this well and shoot it at 10:30 am on 10/2/2014. This will be the second attempt at shooting this well to stimulate production. |
2008593260 | 2014-06-16 | Drill / Deepen / Reopen | No Violations | Witnessed pressure testing of the 7 surface casing that was ran and cemented on 6/13/2014. The pressure test commenced at 9:42 a.m. at 350 p.s.i. and ended at 10:12 a.m. at 310 p.s.i. There was a slight leak on the 2 valve on the cement head, which accounted for most of the drop in pressure. The pressure test was considered satisfactory and the O.K. was given to continue deepening. |
For data sources see[8]