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Well ID: 34-167-60385 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Aurelius Township | |
Operator Name: TRIAD HUNTER LLC | |
Well Pad ID: | |
Farm/Lease Name: MCBRIDE/GILDOW | |
License Status: Final Restoration | |
License Date: 2018-10-24 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.610000 | |
Longitude: -81.430000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Change of Owner | 2003-09-12 | Operator changed from 2060, FEICK C R to 7517, PIERSOL OIL AND GAS |
Change of Owner | 2006-03-20 | Operator changed from 7517, PIERSOL OIL AND GAS to 2348, TRIAD RESOURCES INC |
Change of Owner | 2010-03-24 | Operator changed from 2348, TRIAD RESOURCES INC to 8610, TRIAD HUNTER LLC |
APP | 2018-10-24 | Proposed Formations:BEREA SAND, Issued Date:10/24/2018, Expired Date:10/23/2020 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-12-07 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Record Last Modified | 2019-05-10 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Construction Permit Expires | 2020-10-23 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | FEICK C R | 0.00 | 109.00 | 365 |
1999 | FEICK C R | 0.00 | 55.00 | 365 |
2000 | FEICK C R | 0.00 | 55.00 | 365 |
2001 | FEICK C R | 0.00 | 104.00 | 365 |
2002 | FEICK C R | 0.00 | 51.00 | 365 |
2003 | FEICK C R | 0.00 | 106.00 | 365 |
2004 | PIERSOL OIL AND GAS | 0.00 | 51.00 | 365 |
2005 | PIERSOL OIL AND GAS | 0.00 | 0.00 | 365 |
2006 | TRIAD RESOURCES INC | 0.00 | 0.00 | 365 |
2007 | TRIAD RESOURCES INC | 0.00 | 0.00 | 365 |
2008 | TRIAD RESOURCES INC | 0.00 | 0.00 | 365 |
2009 | TRIAD RESOURCES INC | 0.00 | 0.00 | 365 |
2010 | TRIAD RESOURCES INC | 0.00 | 0.00 | 365 |
2011 | TRIAD HUNTER LLC | 0.00 | 0.00 | 365 |
2012 | TRIAD HUNTER LLC | 0.00 | 0.00 | 366 |
2017 | TRIAD HUNTER LLC | 0.00 | 0.00 | 0 |
2018 | TRIAD HUNTER LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | FEICK C R | Brine | 0 | 365 |
1999 | FEICK C R | Brine | 0 | 365 |
2000 | FEICK C R | Brine | 0 | 365 |
2001 | FEICK C R | Brine | 0 | 365 |
2002 | FEICK C R | Brine | 0 | 365 |
2003 | FEICK C R | Brine | 0 | 365 |
2004 | PIERSOL OIL AND GAS | Brine | 0 | 365 |
2005 | PIERSOL OIL AND GAS | Brine | 0 | 365 |
2006 | TRIAD RESOURCES INC | Brine | 0 | 365 |
2007 | TRIAD RESOURCES INC | Brine | 0 | 365 |
2008 | TRIAD RESOURCES INC | Brine | 0 | 365 |
2009 | TRIAD RESOURCES INC | Brine | 0 | 365 |
2010 | TRIAD RESOURCES INC | Brine | 0 | 365 |
2011 | TRIAD HUNTER LLC | Brine | 0 | 365 |
2012 | TRIAD HUNTER LLC | Brine | 0 | 366 |
2017 | TRIAD HUNTER LLC | Brine | 0 | 0 |
2018 | TRIAD HUNTER LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1303743950 | 2016-3-14 0:00: | PW | No Violations | 1.00 |
-1373947707 | 2017-6-30 0:00: | PW | No Violations | |
-1505836959 | 2009-4-30 0:00: | PW | No Violations | |
-1653321367 | 2016-11-3 0:00: | PW | No Violations | 0.10 |
-1965767084 | 2016-3-30 0:00: | AM | No Violations | 0.20 |
-232227191 | 2018-1-16 0:00: | AD | No Violations | |
-292358074 | 2018-12-3 0:00: | PB | No Violations | 6.00 |
0232227191 | 2018-01-16 | Annular Disposal | No Violations | The inspection this day revealed that this well is equipped with a 4 1/2 inch diameter production casing. The valves are closed on the wellhead. The well is idle at this time and no attempts have been made to get this well into compliance. |
0292358074 | 2018-12-03 | Plug / Plug Back | No Violations | I was on location today to witness the plugging activities on this well. Timco has there wireline truck out here today so they can shoot the bottom joint off so we can set a bottom plug because there is a packer hung on the tubing up hole. The casing is crooked in the hole and the tubing is also crooked. The wireline truck could not get past 1058 feet. We ended up sending the wireline crew out for the day so the rig crew could work on cleaning up the tubing. |
0410440267 | 2018-12-05 | Plug / Plug Back | No Violations | I was back on location today to witness the plugging of this well. Today the wireline crew was able to get down to 1230 feet. They shot the tubing off there so we could set the bottom plug. Formation Cementing came out to the well today to pump the cement plug. A 45 sack class A plug was pumped to cover the bottom plug. The wireline crew then ran back in the well to shoot the tubing off again at 798 feet. The cement crew will come back out tomorrow to finish plugging this well. |
0579839487 | 2007-01-30 | Production Wells | No Violations | Inspection this day found well not in production - jack sitting off to side, rods out of hole, has recently been worked on, tank has good IDs, fair to poor dike. |
1303743950 | 2016-03-14 | Production Wells | Violations Noted | Upon inspection, it was observed that this well is idle and incapable of production. The well is open to the atmosphere and consists of 6.625 casing and 2.375 tubing. The rods are pulled from the well and are stacked beside the well along with the pumping unit. The tank battery consists of a 100 bbl production tank inside an earthen dike. RBDMS records indicate that the well has not produced oil or gas since 2004. The well shall be plugged and abandoned. Triad Hunter LLC shall submit a written plugging schedule within 30 days to Inspector Lynn Parkins at 5880 Memory Rd. Zanesville, OH 43701 and plug the well within 180 days. Triad Hunter LLC will be notified if the plugging schedule is approved or denied. |
1373947707 | 2017-06-30 | Production Wells | No Violations | The inspection this day revealed that this well is equipped with a 4 1/2 inch diameter production casing. There are rods and a pumping unit near the well but are off the wellhead at the time of inspection. I call Austin Clark to speak to him about this well and ask if Triad still planned to put this well into production. He informed me it was still on the list to do in 2017 and would speak to Bob Handschumaker and have him call or e-mail me to let me know more information on the well. The well is idle at the time of inspection and the issues on this well have not been resolved. |
1483251407 | 2019-8-14 0:00: | FR | No Violations | 0.50 |
1505836959 | 2009-04-30 | Production Wells | No Violations | Inspection this day found well with jack producing, tank has good IDs, good dike, no gas meter. |
1543504249 | 2018-11-29 | Plug / Plug Back | No Violations | I was on location today to witness the plugging activities on this well. Today the rig crew worked on getting setup and made sure we could get to the bottom to set the bottom plug. The 2 inch diameter tubing is hung in the well. They will have to shoot the bottom joint off to pump the bottom plug. The rig crew is shutting down until next week. |
1653321367 | 2016-11-03 | Production Wells | No Violations | ODNR Division of Oil and Gas supervisors Dan Goins and Eric Conrad, and I met with Triad Hunter representatives Austin Clark, Mike Horan, and Bob Handschumaker. We discussed the violation issues with this well and a timeline in which these violations shall be put back within compliance. Triad stated that they plan to put this well back in production. |
1771198768 | 2018-12-07 | Plug / Plug Back | No Violations | I was back on location today to witness the plugging of this well. The tubing was shot off at 798 feet. Formation Cementing was back out on location today to pump the plug down this well. We cemented the 4.5 inch diameter casing from 798 feet to surface using 133 sacks of Class A cement. We pumped a 450 foot plug then pulled 450 feet of tubing out of the well then finished with a 350 foot plug. The cement stayed at the surface when we finished pumping it. This well is now plugged. |
1965767084 | 2016-03-30 | Administrative Inspection | No Violations | Met at Barlow Office with Supervisor Dan Goins and Triad-Hunter representatives Ben Smeltzer and Bob Handschumaker to discuss compliance issues at this well. Triad-Hunter is in the process of evaluating this well for potential to produce or if it needs plugged and abandoned. |
410440267 | 2018-12-5 0:00: | PB | No Violations | 6.00 |
579839487 | 2007-1-30 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1303743950 | US-OH-108565 | 2016-03-16 | Well shall be plugged |
For data sources see[7]