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Well ID: 34-169-21612 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: East Union Township | |
Operator Name: ODOT-PR | |
Well Pad ID: | |
Farm/Lease Name: WALTZ EVERETT | |
License Status: Final Restoration | |
License Date: 2004-09-03 | |
Spud Date: 1971-01-04 | |
Spud Drilling Contractor: ROSS WELL SERVICE | |
Final Drill Date: 1971-02-11 | |
Well Total Depth: 3704.00 ft | |
Configuration: Vertical | |
Latitude: 40.800000 | |
Longitude: -81.810000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-12-18 | 2200 SMITH MANAGEMENT INC GeoDate 12/18/70 |
Original Spud | 1971-01-04 | |
Completed | 1971-02-11 | |
Reached Total Depth | 1971-02-11 | |
Completion Report Received | 1971-03-04 | |
CO | 1993-04-20 | 2180 PONDEROSA CONSULT SER INC GeoDate 12/18/70 |
APP | 2004-09-03 | Proposed Formations:CLINTON, Issued Date:9/3/2004, Expired Date:9/3/2005 6:00:00 AM, Drilling unit acres:79.6, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2004-10-08 | |
Construction Permit Expires | 2005-09-03 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2000 Bbl | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1600707107 | 2004-10-18 0:00 | PB | No Violations | 1.50 |
-1645700414 | 2004-10-8 0:00: | PB | No Violations | 6.50 |
-437086348 | 2004-10-7 0:00: | PB | No Violations | 3.50 |
0437086348 | 2004-10-07 | Plug / Plug Back | No Violations | Rip 4 inch at 2700ft. Set bridge plug at 2650 ft. and fill with 4.5 tons clay.Return later and found all 4 inch out and pulling 8 inch next. |
0592938085 | 2007-01-11 | Final Restoration | No Violations | Meets requirements for restoration final . |
1299006499 | 2004-09-24 | Plug / Plug Back | No Violations | Check for rig again today and did not find rig.Contact Altier Brothers and found that rig is delayed on another plug. |
1521995339 | 2004-10-06 | Plug / Plug Back | No Violations | Set 4 tons clay on bottom 3714 to 3200 ft. |
1591262186 | 2004-09-23 | Plug / Plug Back | No Violations | Rig was to have moved in today and check on rig status.Did not find rig today ? |
1600707107 | 2004-10-18 | Plug / Plug Back | No Violations | Pits are closed and pipe has been cut off below ground level. No leaks noted |
1645700414 | 2004-10-08 | Plug / Plug Back | No Violations | Had to run tubing in hole to set the rest of plugs on cement.The tubing got stuck and after working it pulled out and check bottom joint.Cut slots in bottom joint and ran back in to 990 ft.Set cement plug from 990 ft. to 600 ft. Set next plug at 400 ft. to 0ft. Had cement drop down hole.W/O cement to set up and top off again and this time it held at surface.Cement remained at surface and did not drop off after job was complete. |
592938085 | 2007-1-11 0:00: | FR | No Violations | 0.70 |
For data sources see[8]