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Well ID: 34-169-22865 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Green Township | |
Operator Name: MORMACK IND INC | |
Well Pad ID: | |
Farm/Lease Name: MARTY HAMMEL UNIT | |
License Status: Final Restoration | |
License Date: 2009-10-01 | |
Spud Date: 2009-12-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-08-27 | |
Well Total Depth: 3568.00 ft | |
Configuration: Vertical | |
Latitude: 40.900000 | |
Longitude: -81.840000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-06-19 | 217 MORMACK IND INC GeoDate 6/19/81 |
Original Spud | 1981-07-16 | |
Completed | 1981-08-27 | |
Reached Total Depth | 1981-08-27 | |
APP | 2009-10-01 | Proposed Formations:CLINTON, Issued Date:10/1/2009, Expired Date:10/1/2010 6:00:00 AM, Drilling unit acres:75, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2009-12-15 | |
Construction Permit Expires | 2010-10-01 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3426 | 3509 | 19 |
3426 | 3509 | 19 | |
3426 | 3509 | 19 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2000 Bbl | 25000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MORMACK IND INC | 4058.00 | 0.00 | 0 |
1985 | MORMACK IND INC | 2400.00 | 0.00 | 0 |
1986 | MORMACK IND INC | 2580.00 | 0.00 | 365 |
1987 | MORMACK IND INC | 1707.00 | 0.00 | 365 |
1988 | MORMACK IND INC | 2082.00 | 67.00 | 365 |
1989 | MORMACK IND INC | 1548.00 | 0.00 | 365 |
1990 | MORMACK IND INC | 1390.00 | 0.00 | 365 |
1991 | MORMACK IND INC | 1582.00 | 0.00 | 365 |
1993 | MORMACK IND INC | 868.00 | 0.00 | 365 |
1994 | MORMACK IND INC | 1010.00 | 0.00 | 365 |
1995 | MORMACK IND INC | 792.00 | 0.00 | 365 |
1998 | MORMACK IND INC | 611.00 | 0.00 | 365 |
1999 | MORMACK IND INC | 589.00 | 0.00 | 365 |
2000 | MORMACK IND INC | 508.00 | 0.00 | 365 |
2001 | MORMACK IND INC | 514.00 | 0.00 | 365 |
2002 | MORMACK IND INC | 404.00 | 63.00 | 365 |
2003 | MORMACK IND INC | 402.00 | 0.00 | 365 |
2004 | MORMACK IND INC | 305.00 | 0.00 | 365 |
2005 | MORMACK IND INC | 233.00 | 45.00 | 365 |
2006 | MORMACK IND INC | 267.00 | 0.00 | 365 |
2007 | MORMACK IND INC | 198.00 | 0.00 | 365 |
2008 | MORMACK IND INC | 0.00 | 0.00 | 365 |
2009 | MORMACK IND INC | 0.00 | 0.00 | 365 |
2010 | MORMACK IND INC | 123.00 | 17.00 | 365 |
2011 | MORMACK IND INC | 0.00 | 0.00 | 0 |
2012 | MORMACK IND INC | 0.00 | 0.00 | 366 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MORMACK IND INC | Brine | 35 | 0 |
1985 | MORMACK IND INC | Brine | 65 | 0 |
1986 | MORMACK IND INC | Brine | 35 | 365 |
1987 | MORMACK IND INC | Brine | 0 | 365 |
1988 | MORMACK IND INC | Brine | 35 | 365 |
1989 | MORMACK IND INC | Brine | 0 | 365 |
1990 | MORMACK IND INC | Brine | 0 | 365 |
1991 | MORMACK IND INC | Brine | 0 | 365 |
1993 | MORMACK IND INC | Brine | 0 | 365 |
1994 | MORMACK IND INC | Brine | 35 | 365 |
1995 | MORMACK IND INC | Brine | 0 | 365 |
1998 | MORMACK IND INC | Brine | 0 | 365 |
1999 | MORMACK IND INC | Brine | 0 | 365 |
2000 | MORMACK IND INC | Brine | 56 | 365 |
2001 | MORMACK IND INC | Brine | 0 | 365 |
2002 | MORMACK IND INC | Brine | 30 | 365 |
2003 | MORMACK IND INC | Brine | 0 | 365 |
2004 | MORMACK IND INC | Brine | 0 | 365 |
2005 | MORMACK IND INC | Brine | 30 | 365 |
2006 | MORMACK IND INC | Brine | 0 | 365 |
2007 | MORMACK IND INC | Brine | 0 | 365 |
2008 | MORMACK IND INC | Brine | 150 | 365 |
2009 | MORMACK IND INC | Brine | 20 | 365 |
2010 | MORMACK IND INC | Brine | 86 | 365 |
2011 | MORMACK IND INC | Brine | 0 | |
2012 | MORMACK IND INC | Brine | 0 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1762111944 | 2009-12-14 0:00 | PB | No Violations | 6.00 |
-20124018 | 2009-12-9 0:00: | PB | No Violations | 8.00 |
-232545182 | 2009-12-8 0:00: | PB | No Violations | 4.50 |
-556653141 | 2010-11-19 0:00 | FR | No Violations | 0.70 |
-755967263 | 2010-2-4 0:00:0 | FR | No Violations | 1.00 |
0000PL1098 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0020124018 | 2009-12-09 | Plug / Plug Back | No Violations | Try and rip 4 inch casing and could not get a telegraph - got all the way up to 2160 ft and still no telegraph , at that time I advised to blind rip and see what happens.After they knocked on it for over 1 hour and next tried to pull casing.What happened was the 8 inch casing came with it.That means the 8 inch is in two and has been leaking around casing and dirt and rust has built up so that a telegraph could not be heard.Next pumped the 8 inch full of freshwate out of the stream and the casing fell.Could not get the two casing apart so advised rip another set of holes in two more spots and set 300 ft plug thru tubing.That will hold the 4 inch and next pull the 8 inch out . |
0232545182 | 2009-12-08 | Plug / Plug Back | No Violations | Set bottom plug thru tubing from 3500 ft to 3300 ft. |
0556653141 | 2010-11-19 | Final Restoration | No Violations | Meets requirements for restoration final |
0755967263 | 2010-02-04 | Final Restoration | No Violations | Pipe cut off do not see any leaks but there is plenty of snow .Pits are closed |
0991465924 | 2009-12-15 | Plug / Plug Back | No Violations | Grout to surface today from 550 to o ft with 9 sk grout . |
1557814327 | 2009-12-21 | Plug / Plug Back | No Violations | Check plug for leaks and found no leaks.Cement is at surface and pipe can be cut off.Pits are closed. |
1762111944 | 2009-12-14 | Plug / Plug Back | No Violations | Set 2 nd plug from 2100 to1800ft thru 1 1/2 tubing. Next try and rip at 780 ft and set precast cement plug on seat .Fill up around plug with clay and fill up to 550 ft with clay. |
991465924 | 2009-12-15 0:00 | PB | No Violations | 6.00 |
PL1098 | PL | No Violations |
For data sources see[9]