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Well ID: 34-169-24549 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Milton Township | |
Operator Name: MORTON SALT INC | |
Well Pad ID: | |
Farm/Lease Name: MORTON SALT (SMP #4) | |
License Status: Plugged and Abandoned | |
License Date: 2016-07-29 | |
Spud Date: 1988-03-04 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1988-03-14 | |
Well Total Depth: 2596.00 ft | |
Configuration: Vertical | |
Latitude: 40.950000 | |
Longitude: -81.790000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-10-02 | 3509 MORTON SALT/MORTON INTL GeoDate 10/2/87 |
Solution Mining | 1987-10-02 | Issued Date 10/2/87 Expired Date 10/1/88 Acres 0000000 Tool Type RTAF Proposed Formation SALINA Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1988-03-04 | CHG. FTG. & COORDS 5-14-88 |
Completed | 1988-03-14 | CHG. FTG. & COORDS 5-14-88 |
Reached Total Depth | 1988-03-14 | CHG. FTG. & COORDS 5-14-88 |
Completion Report Received | 1988-05-03 | CHG. FTG. & COORDS 5-14-88 |
Annulus Pressure Monitoring Approved | 1995-08-16 | CHG. FTG. & COORDS 5-14-88 |
Change of Owner | 2010-11-29 | Operator changed from 3509, MORTON SALT INC to 8736, MORTON SALT INC |
Last Compliance Report | 2011-07-18 | CHG. FTG. & COORDS 5-14-88 |
APP | 2016-07-29 | Proposed Formations:SALINA, Issued Date:7/29/2016, Expired Date:7/29/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class: |
Plugged/Abandoned | 2017-06-23 | CHG. FTG. & COORDS 5-14-88 |
Record Last Modified | 2017-08-18 | CHG. FTG. & COORDS 5-14-88 |
Construction Permit Expires | 2018-07-29 | CHG. FTG. & COORDS 5-14-88 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1999-09-09 | 2580 | 2590 | 0 |
2580 | 2590 | 0 | |
2580 | 2590 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1239554406 | 2017-7-18 0:00: | SM | No Violations | |
-1413500157 | 2006-7-20 0:00: | SM | No Violations | 10.70 |
-1722987586 | 2003-12-9 0:00: | SM | No Violations | |
-1763250762 | 2017-9-15 0:00: | SM | No Violations | |
-312382801 | 2015-6-12 0:00: | SM | No Violations | 0.50 |
-682345095 | 2017-7-24 0:00: | SM | No Violations | |
00000PL216 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0312382801 | 2015-06-12 | Solution Mining Project | No Violations | This well has no apparent problems at time of inspection. Signs in place and legible. |
0516255139 | 2013-10-23 | Solution Mining Project | No Violations | No violations were found at the time of inspection. |
0541454920 | 2017-11-21 | Solution Mining Project | No Violations | |
0593730780 | 2017-11-30 | Solution Mining Project | No Violations | |
0682345095 | 2017-07-24 | Solution Mining Project | No Violations | Arrived on location on 07/24/2017 to meet with Mark Kurtz with Morton Salt and check on the well. A water truck had been brought in on Friday to suck the water off of the top of the well. Cement was noted to be ~5 below ground level and was solid, however gas bubbles were clearly noted in the trace amount of water remaining on top of the cement. A flange with an open valve on it will be placed over the well to prevent additional rainwater from going downhole while also allowing gas to vent. This issue was discussed with Andrew Adgate (DOGRM UIC), who will research well construction and work with Morton Salt to determine a plan for remediation. |
0693570793 | 2005-11-04 | Solution Mining Project | No Violations | Test M.I.T. For 4 hours and test was stopped by operator becasuse of leaks. |
1210i40571 | 2002-03-27 | Solution Mining Project | No Violations | Well appears ok. Flow meter was broken. |
1210i4057195 | 2002-3-27 0:00: | SM | No Violations | |
1239554406 | 2017-07-18 | Solution Mining Project | No Violations | Performed quarterly inspection at the request of DOGRM UIC on 07/18/2017. The well was previously plugged. Cement was noted to have fallen back to an indeterminate depth, and water in the casing was noted to be bubbling. Mark Kurtz with Morton Salt was notified of this issue and will have the water sucked out of the casing in order to determine cement top so that a plan forward can be determined. No other problems were noted at the time of the inspection. |
1296678223 | 2017-08-16 | Plug / Plug Back | No Violations | Visited location on 08/16/2017 to meet with Mark Kurtz with Morton Salt to check the top plug and discuss a plan forward. No bubbles or gas were noted on the top plug at the time of the inspection. Morton Salt will continue to monitor the well. |
1413500157 | 2006-07-20 | Solution Mining Project | No Violations | Test well # 27-- # 4549 and use # 36 as Reference well --Test well passed. Reading # 1 test well -266.874- # 2 266.467-- # 3 265.709-- # 4 265.103-- # 5 265.103-- # 6 264.778-- # 7 264.764-- # 8 265.343-- # 9 266.223-- Reference well # 1 39.882-- # 2 39.480-- # 3 38.758-- # 4 38.460-- # 5 38.173-- # 6 37.825-- # 7 37.813-- # 8 265.343-- # 9 39.262-- |
1498243374 | 2017-06-23 | Plug / Plug Back | No Violations | The well was plugged with cement to surface today. Assisted inspector Allie Sherwood with plugging. |
1512137703 | 2017-12-01 | Surface Facility Construction | No Violations | |
1722987586 | 2003-12-09 | Solution Mining Project | No Violations | CHECKED ID - OK |
1763250762 | 2017-09-15 | Solution Mining Project | No Violations | Visited location on 09/15/2017 at the request of Mark Kurtz with Morton Salt, to check on the status of the well. No changes were noted from the previous inspection, nor any problems noted. |
1812252632 | 2012-09-24 | Solution Mining Project | No Violations | Identification in place. No problems noted. |
1853152970 | 2014-03-06 | Solution Mining Project | No Violations | ID in place and legible. No apparent problems. |
1871455608 | 2014-05-29 | Solution Mining Project | No Violations | Well signs in place and legible. No apparent problems at this time. |
1980616642 | 2011-07-08 | Solution Mining Project | No Violations | Arrive for MIT on well using 8 5/8 casing. Well has been blanked from going down line and has main valve open to the well. Appears to have proper isolation to conduct a proper test of integrity. Bob Browne of Morton Salt conducted the setting of the interface with water and is here for the test. The reference well used for this test is Morton Salt # 37 - Test went as planned and well passed with .023 ave. for eight hour test. |
2040095812 | 2014-10-24 | Solution Mining Project | No Violations | ID is in place. No apparent problems at time of inspection. |
516255139 | 2013-10-23 0:00 | SM | No Violations | |
541454920 | 2017-11-21 0:00 | SM | No Violations | 2.00 |
593730780 | 2017-11-30 0:00 | SM | No Violations | 1.50 |
693570793 | 2005-11-4 0:00: | SM | No Violations | 4.00 |
PL216 | PL | No Violations |
For data sources see[4]