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Well ID: 34-169-61123 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Plain Township | |
Operator Name: W H PATTEN DRILLING CO | |
Well Pad ID: | |
Farm/Lease Name: EBERHART | |
License Status: Final Restoration | |
License Date: 2012-08-09 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: 1921-02-12 | |
Well Total Depth: 3297.00 ft | |
Configuration: Vertical | |
Latitude: 40.770000 | |
Longitude: -82.030000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Completed | 1921-02-12 | |
Reached Total Depth | 1921-02-12 | |
APP | 2012-08-09 | Proposed Formations:CLINTON, Issued Date:8/9/2012, Expired Date:8/9/2014 12:00:00 PM, Drilling unit acres:106.75, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2012-11-14 | |
Construction Permit Expires | 2014-08-09 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2021-02-26 | NITR | 0 | 60 Qts | 0 | ||
0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
1999 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2000 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2001 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2002 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2003 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2004 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2005 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2006 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2007 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2008 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2009 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2010 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2011 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2012 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 366 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | W H PATTEN DRILLING CO | Brine | 110 | 365 |
1999 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2000 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2001 | W H PATTEN DRILLING CO | Brine | 75 | 365 |
2002 | W H PATTEN DRILLING CO | Brine | 90 | 365 |
2003 | W H PATTEN DRILLING CO | Brine | 60 | 365 |
2004 | W H PATTEN DRILLING CO | Brine | 55 | 365 |
2005 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2006 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2007 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2008 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2009 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2010 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2011 | W H PATTEN DRILLING CO | Brine | 0 | 365 |
2012 | W H PATTEN DRILLING CO | Brine | 0 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1056289988 | 2012-11-9 0:00: | PB | No Violations | |
-1117223160 | 2012-11-14 0:00 | PB | No Violations | |
-1188325850 | 2012-10-11 0:00 | PB | No Violations | |
-1263830514 | 2012-11-15 0:00 | FR | No Violations | |
-1568407841 | 2012-10-15 0:00 | PB | No Violations | |
-1808155897 | 2013-7-17 0:00: | FR | No Violations | 0.50 |
-183504774 | 2012-4-6 0:00:0 | PW | No Violations | 2.00 |
-2104410073 | 2012-11-1 0:00: | PB | No Violations | |
-226022772 | 2012-10-17 0:00 | PB | No Violations | |
-324056814 | 2013-7-23 0:00: | FR | No Violations | |
-829394055 | 2012-10-10 0:00 | PB | No Violations | |
-890361284 | 2013-7-17 0:00: | PB | No Violations | 0.50 |
0154008294 | 2012-10-31 | Plug / Plug Back | No Violations | They ripped the 7 casing at 1300. They had some trouble getting the pipe free as it was catching on the bottom of the 8. It finally came free and they are pulling 7 casing. |
0183504774 | 2012-04-06 | Production Wells | No Violations | FOLLOW UP TO NOV # 1334232065 I received a complaint on this well from John Corbett, 3301 Congress Road, Wooster , Ohio 44691. During my inspection, on 4/06/2012, I found the well was shut- in with zero pressure on the gauges. There is no evidence of pet |
0210930923 | 2012-04-06 | Production Wells | No Violations | FOLLOW UP TO NOV # 1334232065 I received a complaint on this well from John Corbett, 3301 Congress Road, Wooster , Ohio 44691. During my inspection, on 4/06/2012, I found the well was shut- in with zero pressure on the gauges. There is no evidence of petroleum impact around the well head or well site. There is no tank battery and proper identification has not been posted. I located the well owner using ODNR Emergency Well Locator. I contacted the well owner and noified them of this complaint. I then issued the well owner a verbal Compliance Notice. I will follow up with a written Compliance Notice to plug this well. There is no option to produce this well since it has been idle for 14 years and the well owner has removed the production equipment. |
0226022772 | 2012-10-17 | Plug / Plug Back | No Violations | Getting the casing ready to shoot off. Shooters will be on location in the morning. |
0324056814 | 2013-07-23 | Final Restoration | No Violations | There was no indication of the well, tank battery, or lease road. The location was graded and vegetation was restored. The site is now a pasture. Final restoration passes. |
0522017557 | 2012-11-05 | Plug / Plug Back | No Violations | Petroset spotted a 300 cement plug from 1254-954. See the plugging report for details. |
0548898032 | 2012-04-06 | Production Wells | No Violations | FOLLOW UP TO NOV # 2054033149 FOLLOW UP TO NOV # 1334057658 I received a complaint from John Corbertt, 3301 Congress Road, Wooster, OH. I found the well head but no tanks. No pollution or contamination evident and no production recorded, as well is shut in. It does not have any press |
0626618432 | 2012-04-06 | Production Wells | No Violations | FOLLOW UP TO NOV # -183504774 FOLLOW UP TO NOV # 1334232065 I received a complaint on this well from John Corbett, 3301 Congress Road, Wooster , Ohio 44691. During my inspection, on 4/06/2012, I found the well was shut- in with zero pressure on the gauges. There is no evidence of pet |
0829394055 | 2012-10-10 | Plug / Plug Back | No Violations | Moved a rig on and rigged it up. They are pulling rods and tubing in preparation to plug the well. |
0890361284 | 2013-07-17 | Plug / Plug Back | No Violations | With plugging of this well, NV is resolved. |
1056289988 | 2012-11-09 | Plug / Plug Back | No Violations | Petroset Cementing set cement plugs from 600-450 and from 300 - 0. No circulation even though we ran gel and hulls ahead of both plugs. Fluid level remained at 30. We will tag the cement top and grout to surface. See the plugging report for details. |
1066160940 | 2012-10-22 | Plug / Plug Back | No Violations | No activity today. Short handed. |
1117223160 | 2012-11-14 | Plug / Plug Back | No Violations | Grouted the top plug back to surface with 3 cubic yards of 9 sack grout. The grout stayed up. See the plugging report for details. |
1188325850 | 2012-10-11 | Plug / Plug Back | No Violations | The rig is pulling the 2-3/8 EUE tubing and will run 1-1/2 regular tubing back in thru which to spot a bottom cement plug. |
1263830514 | 2012-11-15 | Final Restoration | No Violations | The grout stayed up. The casing was cut off and buried. The pit has been emptied and closed. The top soil has been spread and the location is to final grade. The location was left to settle out over the winter and be seeded in the spring. |
1334057658 | 2012-04-06 | Production Wells | Violations Noted | I received a complaint from John Corbertt, 3301 Congress Road, Wooster, OH. I found the well head but no tanks. No pollution or contamination evident and no production recorded, as well is shut in. It does not have any pressure on any of the gauges. There is no identification at the well, and there are no tanks. I returned to the site on Monday (4/09/2012) and obtained a GPS reading to check the Emergency Well Locator to verify the well permit number and well owner. I contacted the well owner, advised them of the complaint and issued a verbal notice. I will follow up with a written notice. This well should be plugged and there is no option to put it in production since it has not produced since 1998 (14 years) and the operator has removed the production equipment, thus eliminating the wells ability to produce. |
1334232065 | 2012-04-06 | Production Wells | No Violations | I received a complaint on this well from John Corbett, 3301 Congress Road, Wooster , Ohio 44691. During my inspection, on 4/06/2012, I found the well was shut- in with zero pressure on the gauges. There is no evidence of petroleum impact around the well head or well site. There is no tank battery and proper identification has not been posted. I located the well owner using ODNR Emergency Well Locator. I contacted the well owner and noified them of this complaint. I then issued the well owner a verbal Compliance Notice. I will follow up with a written Compliance Notice to plug this well. There is no option to produce this well since it has been idle for 14 years and the well owner has removed the production equipment. |
1350502051 | 2012-10-12 | Plug / Plug Back | No Violations | Running 1-1/2 tubing through which to set the bottom cement plug. |
1350643734 | 2012-10-18 | Plug / Plug Back | No Violations | Tim Brown is on location to try and shoot off the 5-1/2 casing. They finally succeeded on 5th attempt and shot it off at 1900. Pulled two joints and shut down for the night. |
1352228503 | 2012-11-06 | Plug / Plug Back | No Violations | Tried to pull the 8- |
154008294 | 2012-10-31 0:00 | PB | No Violations | |
1568407841 | 2012-10-15 | Plug / Plug Back | No Violations | Petroset spotted a 60 sack bottom cement plug from 3250 to 2900. See the plugging report for details. |
1654533330 | 2012-04-06 | Production Wells | No Violations | FOLLOW UP TO NOV # 1334057658 I received a complaint from John Corbertt, 3301 Congress Road, Wooster, OH. I found the well head but no tanks. No pollution or contamination evident and no production recorded, as well is shut in. It does not have any pressure on any of the gauges. There is no identification at the well, and there are no tanks. I returned to the site on Monday (4/09/2012) and obtained a GPS reading to check the Emergency Well Locator to verify the well permit number and well owner. I contacted the well owner, advised them of the complaint and issued a verbal notice. I will follow up with a written notice. This well should be plugged and there is no option to put it in production since it has not produced since 1998 (14 years) and the operator has removed the production equipment, thus eliminating the wells ability to produce. |
1808155897 | 2013-07-17 | Final Restoration | No Violations | Appears to meet requirements for final restoration. |
2054033149 | 2012-04-06 | Production Wells | No Violations | FOLLOW UP TO NOV # 1334057658 I received a complaint from John Corbertt, 3301 Congress Road, Wooster, OH. I found the well head but no tanks. No pollution or contamination evident and no production recorded, as well is shut in. It does not have any press |
2104410073 | 2012-11-01 | Plug / Plug Back | No Violations | They pulled the balance of the 7 casing and ran tubing to approximately 1250. The rig will be down on11/2/12 and we will spot a cement plug on Monday 11/5/12. |
210930923 | 2012-4-6 0:00:0 | PW | No Violations | 2.00 |
2110509696 | 2012-10-16 | Plug / Plug Back | No Violations | Ran tibing and tagged the bottom cement plug at 2900. Pulled the tubing. |
522017557 | 2012-11-5 0:00: | PB | No Violations | |
548898032 | 2012-4-6 0:00:0 | PW | No Violations | 2.00 |
626618432 | 2012-4-6 0:00:0 | PW | No Violations | 2.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1334057658 | US-OH-109600 | 2012-04-10 | Failure to legibly identify well | |
1334057658 | US-OH-109601 | 2012-04-10 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[8]