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Well ID: 37-003-20980 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Allegheny | |
Municipality: Forward Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: | |
Farm/Lease Name: COMBUSTION ENGINEERING INC | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 1979-01-30 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.197236 | |
Longitude: -79.899999 |
Date | Event |
---|---|
1979-01-27 | Performed Spud Operation |
1979-01-30 | New Permit Application |
1979-05-11 | Drilling Completion |
1981-01-01 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1982 | KEYSTONE RESOURCES INC | 10,000.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1983 | KEYSTONE RESOURCES INC | 8,000.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1984 | KEYSTONE RESOURCES INC | 11,000.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1985 | KEYSTONE RESOURCES INC | 1,500.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1991 | PA FUELS CORP | 11373.00 | 220 | 0.00 | 0 | 0.00 | 0 |
1994 | OIL & GAS MGMT INC | 4,219.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | OIL & GAS MGMT INC | 1234 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | OIL & GAS MGMT INC | 1610.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | OIL & GAS MGMT INC | 1985.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
213931 | Primary Facility | 1991-09-16 | Routine/Complete Inspection | No Violations Noted | NO TANK |
2547227 | Primary Facility | 2016-11-02 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | WHILE PREPARING THE SITE FOR THE PLUGGING RIG, A TRACK HOE HIT A GAS LINE. THE JOB HAS BEEN SHUT DOWN AND THE PLUGGING HAS BEEN DELAYED. |
2547232 | Primary Facility | 2016-12-01 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | BAKER HUGHES IS ON THE SITE TO CUT THE TUBING AT IT'S FREE POINT. CONTRACTOR SERVICES RIG 1 WILL GO BACK IN AND FISH THE REST OUT. |
2548225 | Primary Facility | 2016-12-28 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | A BOND LOG SHOWED TOC AT 2,025'. THE CASING WAS CUT AT 1,970'. THE RIG IS NOW PULLING THE CASING. |
2548227 | Primary Facility | 2016-12-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | RIG 1 HAS PULLED TUBING THAT WAS STUCK IN THE HOLE. THEY ARE NOW CLEANING OUT THE HOLE. THEY ARE JUST OVER 4,000'. |
2548232 | Primary Facility | 2016-12-06 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | STUCK TUBING WAS CUT AT 2,880'. NOW RUNNING WASH OVER PIPE TO FREE STUCK TUBING LEFT IN HOLE. |
For data sources see[6]