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Well ID: 37-003-22455 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Allegheny | |
Municipality: Avalon Borough | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: SPRUCE RUN | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Undetermined | |
Conservation: No | |
Latitude: 40.505194 | |
Longitude: -80.073306 |
Date | Event |
---|---|
2017-05-01 | Begin Plugging |
2017-07-06 | Finished Plugging |
2019-06-26 | Fully Plugged |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2602637 | Primary Facility | 2017-03-31 | Follow-up Inspection | No Violations Noted | Followup to yesterday's DEP response to stray gas reported by Columbia Gas at residence, 343 Spruce Run Road, Pittsburgh (Avalon). Columbia currently purging the soil of gas, using test holes in yard near the high gas readings they found in basement wall and porch floor cracks. A 2 3/8" tubing against house next to high readings can be seen venting a significant amount of gas. Digging was done at the base of the vent pipe, revealing an elbow and lateral pipe leading away from house into yard. Test results of gas indicate it is not pipeline gas. |
2602642 | Primary Facility | 2017-04-04 | Follow-up Inspection | No Violations Noted | DEP representatives on site to meet w/ representative from Allegheny Well Service to propose how to proceed with an evaluation of the vent and how to excavate to locate the source of the stray gas/vent gas. Got consent form signed by property owner. Ran DEP metal detector, found possible source near house, but a lot of stray readings. |
2602653 | Primary Facility | 2017-04-10 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | A state emergency contract was issued to evaluate this site for remediation or plugging. The evaluation phase of the contract given to Allegheny Well Service, who subcontracted an excavation operator to dig around the vent. The vent was found to lead a few feet from the house, then lead down ~5 feet into the bottom of an overturned bucket set on top of a steel barrel. When the barrel was excavated and removed, a "cellar" about 2' in diameter, ~ 2' deep was found below the barrel with 2 3/8" tubing centered in it. It was partly filled w/ water and gas was bubbling up through the water. The tubing was not gassing. A measuring rod was lowered into cellar and went down ~12 feet before encountering obstruction. Area around well was excavated ~ 8' deep & supported. |
2602658 | Primary Facility | 2017-04-11 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Allegheny ran a wireline into the tubing, hit a solid obstruction @ 815 feet. They pumped the water out of the well cellar to a depth of 5-6 feet. the cellar had some debris, including bottles, metal and some rocks, but was basically open. No wellhead or casing was found. |
2602670 | Primary Facility | 2017-04-14 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T Service & Supply visited site to evaluate for plugging proposal & estimate. (Allegheny provided a plugging proposal & estimate also) Met w/ property owner to discuss possible course of action. |
2602683 | Primary Facility | 2017-04-27 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T vacuumed out the well cellar, redressed threads on tubing and screwed on a new collar. Tried to set 20 feet of 8" casing, but after meeting some resistance when tapped, the casing slipped down and out of sight into annulus area. Then 15" conductor was carefully set & driven into place. |
2602702 | Primary Facility | 2017-05-01 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Visited site before S&T rig mobilization. Hole was completely backfilled, replacing all of the excavated soil & rig pads were placed. Rig on site by mid morning. Ran ~600 feet of 1" tubing into 2 3/8" by 2:30 PM. Shut down for an hour due to heavy rains/storms. Tried to start back up but storms shut down operations again for the rest of the day. Borough of Avalon Public Works Supervisor visited location @ 11:30 AM to check on plugging operations. |
2602839 | Primary Facility | 2017-05-02 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T power swiveled/cleaned out wood obstruction from 830-835 feet. Penetration rate slowed considerably, so pulled string to check bit (bit is 1" collar dressed w/ carbide). |
2602840 | Primary Facility | 2017-05-04 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Rich Freese & I discussed progress of cleanout so far w/ S&T. Current depth is 838 feet. They appear to be drilling on something hard w/ 1" bit, so they plan to fabricate 1 1/2" collar w/carbide to possibly go over obstruction. Well has gassed occasionally through tubing. Well is not taking fluid. |
2602841 | Primary Facility | 2017-05-09 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T TIH w/ new 1 1/2" bit & barrel w/2 grabs. Got hold of fish but lost. TOOH, cut 3 more grabs in barrel, TIH. Current depth is 875 feet. |
2602842 | Primary Facility | 2017-05-11 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T TOOH w/ barrel, got pieces of rope in bit. Rigged up rod socket & TIH. Current depth is 898 feet. |
2602843 | Primary Facility | 2017-05-12 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | No activity @ site today. Checked well for flowback-gassing into tank. |
2602844 | Primary Facility | 2017-05-16 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T power swiveling to 880'-890', TOOH to check for rope fillup. They are getting some circulation back up the tubing. As they drill & fish out rope, they lose depth in tubing to rope rising. |
2602845 | Primary Facility | 2017-05-17 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T went in hole w/ rod socket & retrieved pieces of rope. TIH w/ bit to continue to drill/clean out rope, lost ~20 depth to rope rising in tubing. Still gassing through tubing. |
2602847 | Primary Facility | 2017-05-22 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Ran DEP camera in tubing to 700 feet-rope fillup. Ran camera into annulus, got to ~ 60 feet. Could see tubing and possibly the 8" casing that dropped, but visibility was poor. S&T TIH w/ spear. |
2602850 | Primary Facility | 2017-05-26 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | No activity @ site, so check well for flowback status. Annulus has plastic vent re-installed, extending to roofline. No detectable gas flow from tubing to tank or up ventpipe. |
2602855 | Primary Facility | 2017-05-30 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | No activity at site, shut down for holiday. Check flowback status. All well, w/ no noticeable gas/fluid flow from tubing to tank. |
2602861 | Primary Facility | 2017-06-01 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Shut down for holiday, no activity. Well is quiet, w/ no noticeable gas/fluid flow. |
2602862 | Primary Facility | 2017-06-05 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Checked site (prior to S&T arrival mid morning). No gas/fluid flowback noted. |
2602864 | Primary Facility | 2017-06-05 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T fishing w/ rod socket on tubing, got ~1 foot of rope. Will TIH using sand line & newly fabricated fishing tools. |
2602865 | Primary Facility | 2017-06-06 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T cleaned out to tubing to 1120 feet late yesterday, pulled out a single length of rope 155 feet long. Fishing efforts today have pulled the rope up to 1070 feet. They used a center spear most of the morning, pulling out chunks of rope each trip. Appeared to grab entire fish 2-3 times, moved uphole some, but could not pull out. |
2602867 | Primary Facility | 2017-06-06 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T fishing w/ rod socket on 1" tubing. |
2602869 | Primary Facility | 2017-06-08 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T TIH w/ spear/overshot on tubing, drove ~5 feet, then TOOH, got nothing. Depth: 1200' |
2602870 | Primary Facility | 2017-06-08 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T fishing w/ center spear on sand line, getting chunks of rope. |
2608099 | Primary Facility | 2017-06-13 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T pulled ~8 feet of rope yesterday. Today @ 1235 feet. TIH w/10 foot center spear on work string, TOOH w/ nothing, Put spear on tool string w/ jars on sand line, TIH, snagged some rope, stalled rig pulling, but only got rope chunks. Repeated. Well is gassing today after being dead for several days. |
2608105 | Primary Facility | 2017-06-14 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T @ 1245 feet. TIH w/ rod socket on tubing. TOOH w/ pieces of rope. TIH w/ center spear on tubing. |
2608112 | Primary Facility | 2017-06-15 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T TIH w/ center spear on tubing, got small pieces of rope. Repeated, pulled weight to 490 feet, then broke free. Went in w/ center spear on sand line, pulled fish to 290 feet then broke free, but pulled out ~4 feet of rope. Repeated, pulled out 6 feet of rope, followed by a strong blow of gas. TIH w/ center spear on sandline, back to bottom. |
2608117 | Primary Facility | 2017-06-15 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T fishing w/ center spear on sandline, pulled out ~5 foot section of rope from 1279 feet. |
2608121 | Primary Facility | 2017-06-19 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Surefire Wireline logged well: GR, CCL & CBL. Logger TD:1281'. Appears to be tight spots in annulus @ 240', 316', 358', 505' and possibly 670'-712'. Ratty tubing w/ possible holes @~900'. |
2608123 | Primary Facility | 2017-06-21 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | No activity @ site today. Work to resume tomorrow. Well is quiet, w/ no gas or water flowback. |
2608126 | Primary Facility | 2017-06-22 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Surefire cut the 2 3/8" tubing @ 1280'. S&T TIH w/ wireline, tagged obstruction @ 1281', TOOH. TIH w/ 1" tubing w/ angled end, bumped @1281', then continued downhole in annulus to 1390', hit bottom or cavings. (This will be attainable bottom.) |
2612818 | Primary Facility | 2017-06-26 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T pumped an 8 sack bottom-hole plug. TOOH w/all 1"work string. Did repairs to damage on yard from logging truck. |
2612819 | Primary Facility | 2017-06-27 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T tagged bottom-hole plug TOC @ 1340 feet. Loggers will perf tomorrow. |
2612821 | Primary Facility | 2017-06-28 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Surefire perfed 2 3/8" tubing from ~1200' to ~900', 2 shots every 50'. S&T TIH w/ tools on sandline to check hole - all clear to top of plug @ 1340', TOOH. TIH w 1" work string to 1336', could not break circulation, pulled tubing up, then able to break circulation. Pumped a 60 sack plug, w/ a calculated top of 960', based on estimated volume of annulus. Pulled workstring up to 762', circulated bottoms up w/ no cement in returns. TOOH w/ remaining 762' of 1". |
2612822 | Primary Facility | 2017-06-29 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T TIH w/ work string, tagged TOC @ 784'. Well no longer gases after setting this last plug. Will perf & pump next plug tomorrow. |
2612865 | Primary Facility | 2017-07-07 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T has moved rig off location and parked it across the street. They will be doing final work on wellhead and restoring yard next week. Columbia Gas is on site to turn gas back on & take gas readings. They will give their go-ahead to have electric turned back on. Homeowner is on site also. |
2614010 | Primary Facility | 2017-07-10 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Rig has been removed from across the street, and one of two tanks has been removed from location. No activity on site at time of inspection. |
2614045 | Primary Facility | 2017-07-10 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | S&T on site mid-morning w/ gravel (for the well conductor) & topsoil for the yard. They cut the conductor off ~2' below grade (~6" below window well), filled several feet w/ gravel and filled to top w/ cement and attached well ID tag. They returned the cement-slab step that was moved for plugging operations, then applied & leveled top soil, seeded & mulched. |
2614837 | Primary Facility | 2017-07-12 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Checked site restoration work after recent heavy rains. No ponding or washouts noted. Mulch remained in place. |
2615260 | Primary Facility | 2017-05-10 | Drilling/Alteration | No Violations Noted | S&T RETRIEVED SOME TYPE OF PACKER ASSEMBLY. WE ARE NOT SURE WHAT IT WAS USED FOR. S&T WENT BACK INTO THE TUBING WITH A SMALL BIT TO TRY AND VERIFY TD. THEY PULLED THE BIT AND WITH IT THEY FOUND PIECES OF STEEL AND ROPE. |
2615273 | Primary Facility | 2017-05-11 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | S&T IS MAKING MULTIPLE RUNS INTO THE WELL TO DETERMIN TD. THE LAST FEW RUNS, WIT A ROD SOCKET, THEY HAVE BEEN PULLING OUT PIECES OF ROPE. |
2615276 | Primary Facility | 2017-05-23 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | S&T IS FISHING ROPE SECTIONS FROM THE 2" TUBING. THEY ARE USING WIRELINE AND 1" PIPE TO RUN THIER FISHING TOOLS. THE DEPTH AT 3 PM IS 945'. |
2615365 | Primary Facility | 2017-06-30 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | SUREFIRE WIRELINE IS ON THE SITE TO CUT THE 2" TUBING AT 750' THEN PERF THIER WAY OUT OF THE TUBING. |
2615582 | Primary Facility | 2017-05-09 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | S&T, FISHING INSIDE 2" TUBING CAME OUT EMPTY. THEY RAN ANOTHER SOCKET AND HOOKED ONTO SOMETHING BUT LOST IT COMING OUT OF THE HOLE. AT 2:30 THEY BEGAN ANOTHER RUN. |
2615605 | Primary Facility | 2017-05-08 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | S&T RAN A NEW ROD SOCKET INTO THE TUBING. THE OBSTRUCTION DROPPED 35' TO A DEPTH OF 875'. GAS AND SOME FLUID CAME OUT OF THE 1" WORK STRING. |
2615619 | Primary Facility | 2017-05-22 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | THE DEP RAN A CAMERA INSIDE OF THE 2" TUBING, BUT WAS NOT ABLE TO ADVANCE TO THE BOTTOM OF THE HOLE. THE CAMERA WAS RUN OUTSIDE THE OF THE TUBING AND GOT TO 58'. NO CASING WAS EVIDENT. |
2615626 | Primary Facility | 2017-05-02 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | S&T DRILLED WITH A CARBIDE SHOE, AND RETRIEVED SPLINTERD WOOD AND PART OR A ROD STRAP. THEY ADAPTED A ROD SOCKET TO 1" PIPE AND RAN IN TO FISH. THE FIRST RUN WAS NOT SUCCESSFUL. |
2618689 | Primary Facility | 2017-07-25 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Visited site to check restoration after recent rains. The grass is growing in nicely with no signs of erosion or uneven settling. The straw mulch remains in place. |
2624375 | Primary Facility | 2017-08-07 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Reclamation of site looks good; grass is filling in & soil settling has been minimal. |
2652911 | Primary Facility | 2017-09-19 | Site Restoration | In Compliance with Policy | Visited site to check on grass growth. Generally looking good, with some thin spots. |
For data sources see[5]