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Well ID: 37-003-22512 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Pennsylvania | |
County: Allegheny | |
Municipality: Harrison Township | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: | |
License Status: | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.664681 | |
Longitude: -79.7141 |
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2724872 | Primary Facility | 2018-03-15 | Routine/Complete Inspection | No Viols - Permanently Shut Down | Abandoned gas well found during excavation work on construction site. Wellhead is intact and consists of 13" with cement in collar, 6 5/8" casing open, but sealed off, 4 1/2" casing on casing clamp, swaged to 2 3/8" tubing, valved, teed with tapped plug and needle valve, side is plugged. Well is situated on open hillside. |
2725058 | Primary Facility | 2018-05-01 | Plugging(Includes Plugged/Mined Through) | No Viols - Permanently Shut Down | Keystone Wireline logged well, found TD to be 2852', casing to 1688'. Rig TIH with work string, set two bottom hole plugs in open hole to estimated ~1700'. TOOH with work string. |
2725649 | Primary Facility | 2018-05-02 | Plugging(Includes Plugged/Mined Through) | No Viols - Permanently Shut Down | Keystone Wireline unseated packer and pulled all 1024' of the 4 1/2" casing. TIH with wireline, tagged TOC plug at 1630'. Pulled on 6 5/8" casing, but got no stretch. Ran CBL and found several deep and shallow tight spots. Rigging up to run and set CIBP in bottom of 6 5/8" casing. Will perf casing before cementing to surface. |
2726127 | Primary Facility | 2018-05-03 | Plugging(Includes Plugged/Mined Through) | No Viols - Permanently Shut Down | Keystone set CIBP in 6 5/8" casing and perforated late yesterday. The remaining cement plug to surface was pumped today. Well took cement, requiring an extra 10 sacks cement to maintain cement at surface. |
For data sources see[4]