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37-005-00756

Well Details

Well ID: 37-005-00756
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Wayne Township
Operator Name: EQT PROD CO
Well Pad ID:
Farm/Lease Name: W D MCINTYRE
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.842626
Longitude: -79.350243

For data sources see[1][2][3]

Well History

Date Event
1940-10-11 Drilling Completion
1986-01-01 Old Well
2018-07-20 Begin Plugging
2018-08-07 Finished Plugging
2019-06-14 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1986 APOLLO GAS CO 1,339.00 359 0.00 0 0.00 0
1987 APOLLO GAS CO 1,138.00 361 0.00 0 0.00 0
1988 APOLLO GAS CO 1,262.00 365 0.00 0 0.00 0
1989 APOLLO GAS CO 917.00 362 0.00 0 0.00 0
1991 APOLLO GAS CO 813.00 365 0.00 0 0.00 0
1997 CARNEGIE PROD CO 0.00 0 0.00 0 0.00 0
1998 CARNEGIE PROD CO 0.00 0 0.00 0 0.00 0
1999 CARNEGIE PROD CO 0.00 0 0.00 0 0.00 0
2000 EQUITRANS INC 0.00 0 0.00 0 0.00 0
2001 EQUITABLE PROD EASTERN STATES EXPLORATION INC 0.00 0 0.00 0 0.00 0
2003 EQT PROD CO 0.00 0 0.00 0 0.00 0
2004 EQT PROD CO 0.00 0 0.00 0 0.00 0
2005 EQT PROD CO 0.00 0 0.00 0 0.00 0
2006 EQT PROD CO 0.00 0 0.00 0 0.00 0
2007 EQT PROD CO 0.00 0 0.00 0 0.00 0
2008 EQT PROD CO 0.00 0 0.00 0 0.00 0
2009 EQT PROD CO 0.00 0 0.00 0 0.00 0
2010 EQT PROD CO 0.00 0 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0
2012 EQT PROD CO 0.00 0 0.00 0 0.00 0
2013 EQT PROD CO 0.00 0 0.00 0 0.00 0
2014 EQT PROD CO 0.00 0 0.00 0 0.00 0
2015 EQT PROD CO 0.00 0 0.00 0 0.00 0
2016 EQT PROD CO 0.00 0 0.00 0 0.00 0
2017 EQT PROD CO 0.00 0 0.00 0 0.00 0
2018 EQT PROD CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
209193 Primary Facility 1989-02-15 Routine/Complete Inspection No Violations Noted E&S OK; NO TANK
217783 Primary Facility 1996-05-03 Routine/Complete Inspection No Violations Noted OPERATING; IN LINE
2756761 Primary Facility 2018-07-26 Plugging(Includes Plugged/Mined Through) No Violations Noted The rig had some difficulty getting down through the packer on the 3" tubing string but finally breached the packer and obtained a TD of 2069' at which point the well bore appears to be collapsed and attempts to gain more depth utilizing a work string of 1 1/2" tubing through the 3" tubing was not successful. The risk of getting the work string stuck was too great to continue. This approved attainable total depth is below all gas shows except the lowest one and as the bond log on the 3" shows good bond in several places and the 3" cannot be pulled after an attempt to pull was made and only 1/8" of stretch was noted in the tubing the forward plan is to cement the bottom and perf and squeeze cement with 5 shots per every 100' up through the 3" until the free point is reached at approximately 800' or a bit higher where the collar will be shot off and the 3" will be pulled from the free point and the well can be cemented and finished from that point.

For data sources see[6]

References