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37-005-20376

Well Details

Well ID: 37-005-20376
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Redbank Township
Operator Name: XTO ENERGY INC
Well Pad ID:
Farm/Lease Name: IDA MCGREGOR 2
License Status: ACTIVE
Spud Date:
Permit Date: 1960-05-05
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.924420
Longitude: -79.215766

For data sources see[1][2][3]

Well History

Date Event
1960-12-08 Performed Spud Operation
1961-02-15 Drilling Completion
1962-01-01 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 PEOPLES TWP LLC 2494.00 365 0.00 0 0.00 0
1992 PEOPLES TWP LLC 2,382.00 366 0.00 0 0.00 0
1993 PEOPLES TWP LLC 2,072.00 365 0.00 0 0.00 0
1996 PEOPLES TWP LLC 2011 365 0.00 0 0.00 0
1997 PEOPLES TWP LLC 1842 365 0.00 0 0.00 0
1998 PEOPLES TWP LLC 1377 365 0.00 0 0.00 0
1999 PEOPLES TWP LLC 1158 365 0.00 0 0.00 0
2000 PEOPLES TWP LLC 467 366 0.00 0 0.00 0
2001 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2002 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2003 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2004 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2005 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2006 TW PHILLIPS GAS SUPPLY CORP 0.00 0 0.00 0 0.00 0
2007 TW PHILLIPS GAS SUPPLY CORP 1.00 365 0.00 0 0.00 0
2008 TW PHILLIPS GAS SUPPLY CORP 0.00 0 0.00 0 0.00 0
2010 TW PHILLIPS GAS SUPPLY CORP 0.00 0 0.00 0 0.00 0
2011 TW PHILLIPS GAS SUPPLY CORP 0.00 0 0.00 0 0.00 0
2012 XTO ENERGY INC 0.00 0 0.00 0 0.00 0
2013 XTO ENERGY INC 0.00 0 0.00 0 0.00 0
2014 XTO ENERGY INC 0.00 0 0.00 0 0.00 0
2015 XTO ENERGY INC 0.00 0 0.00 0 0.00 0
2016 XTO ENERGY INC 0.00 0 0.00 0 0.00 0
2017 XTO ENERGY INC 0.00 0 0.00 0 0.00 0
2018 XTO ENERGY INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2000 PEOPLES TWP LLC Brine 5.00 Bbl Brine or Industrial Waste Treatment Plt
2016 XTO ENERGY INC Servicing Fluid 730.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW009
2017 XTO ENERGY INC Servicing Fluid 440.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW009
2017 XTO ENERGY INC Servicing Fluid 13.24 Tons RESIDUAL WASTE PROCESSING FACILITY 101674

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2487229 Primary Facility 2016-05-23 Routine/Complete Inspection Pending Well tagged-shut in. Sales meter pulled. Management has scheduled meeting with operator to discuss inactive status/plugging of this well. Follow up inspection-report to be issued.
2503684 Primary Facility 2016-07-19 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig crew ran a camera in and determined that the tubing was rotted off @ 262'. In the process of running an overshot to attempt to grab tubing and back it off @ time of inspection. All equipment on site looked ok.
2507273 Primary Facility 2016-07-21 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig crew attempting to get overshot on to 2 3/8" tubing in well bore @ time of inspection in order to unscrew tubing and retrieve from well bore. All equipment on site looked ok.
2508465 Primary Facility 2016-08-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig tagged top of 2 3/8" tubing @ 305' after pulling last 43' section of tubing that would come free. The old bent-rotted 7" casing is hanging up the Rig's tools preventing them from getting over 2 3/8" tubing to unscrew and pull free section. Still trying to get on tubing @ time of this inspection. All equipment on site looked ok.
2510096 Primary Facility 2016-08-04 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig could not get past rotted 7" casing to get to and retrieve 2 3/8" tubing. Moved service Rig off and waiting for a larger cable tool Rig to move in and retrieve enough 7" to get to tubing. All equipment on site looked ok.
2520604 Primary Facility 2016-09-20 Plugging(Includes Plugged/Mined Through) No Violations Noted Operator back on site with cable tool Rig-ran camera to 219'-noted bent 7"@53'-top of 2 3/8" tubing noted @ 304'. The Rig was at 230' running a 4 11/16" casing swage at the time of inspection. All equipment on site looked ok.
2522586 Primary Facility 2016-09-26 Plugging(Includes Plugged/Mined Through) No Violations Noted Service Rig has pulled 39' of 6 1/4" casing so far at time of inspection. Witnessed crew run the camera down hole ahead of the next casing fishing trip. All equipment looked ok.
2524158 Primary Facility 2016-09-28 Plugging(Includes Plugged/Mined Through) No Violations Noted The plugging Rig ran an 8" swage to 35'-retooled and ran in to 44' and was putting a trip spear on to try and run in to get hold of the 2 3/8" production tubing at the time of this inspection. All equipment on site looked ok.
2524880 Primary Facility 2016-10-04 Plugging(Includes Plugged/Mined Through) No Violations Noted The plugging Rig is still trying to get through the old 7" casing at 39' and was putting on a 6 1/4" bull dog spear to run back in at the time of this inspection. All equipment on site looked ok.
2528539 Primary Facility 2016-10-17 Plugging(Includes Plugged/Mined Through) No Violations Noted The cable tool plugging Rig was shut down waiting on a special drilling bit to arrive at the time of this inspection. The forward plan is to drill over the short section of bent casing stuck in the hole and then pull it out. All equipment on site looked ok.
2605970 Primary Facility 2017-06-20 Plugging(Includes Plugged/Mined Through) No Violations Noted The operator was moving a service rig and equipment back on to this well to finish the plugging operation at the time of this inspection. All equipment on site looked ok.

For data sources see[7]

References