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Well ID: 37-005-20376 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Redbank Township | |
Operator Name: XTO ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: IDA MCGREGOR 2 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 1960-05-05 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.924420 | |
Longitude: -79.215766 |
Date | Event |
---|---|
1960-12-08 | Performed Spud Operation |
1961-02-15 | Drilling Completion |
1962-01-01 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | PEOPLES TWP LLC | 2494.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1992 | PEOPLES TWP LLC | 2,382.00 | 366 | 0.00 | 0 | 0.00 | 0 |
1993 | PEOPLES TWP LLC | 2,072.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | PEOPLES TWP LLC | 2011 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | PEOPLES TWP LLC | 1842 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | PEOPLES TWP LLC | 1377 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | PEOPLES TWP LLC | 1158 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | PEOPLES TWP LLC | 467 | 366 | 0.00 | 0 | 0.00 | 0 |
2001 | PEOPLES TWP LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2002 | PEOPLES TWP LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | PEOPLES TWP LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | PEOPLES TWP LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2005 | PEOPLES TWP LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | TW PHILLIPS GAS SUPPLY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | TW PHILLIPS GAS SUPPLY CORP | 1.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | TW PHILLIPS GAS SUPPLY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | TW PHILLIPS GAS SUPPLY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | TW PHILLIPS GAS SUPPLY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2000 | PEOPLES TWP LLC | Brine | 5.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2016 | XTO ENERGY INC | Servicing Fluid | 730.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW009 |
2017 | XTO ENERGY INC | Servicing Fluid | 440.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW009 |
2017 | XTO ENERGY INC | Servicing Fluid | 13.24 Tons | RESIDUAL WASTE PROCESSING FACILITY | 101674 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2487229 | Primary Facility | 2016-05-23 | Routine/Complete Inspection | Pending | Well tagged-shut in. Sales meter pulled. Management has scheduled meeting with operator to discuss inactive status/plugging of this well. Follow up inspection-report to be issued. |
2503684 | Primary Facility | 2016-07-19 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Rig crew ran a camera in and determined that the tubing was rotted off @ 262'. In the process of running an overshot to attempt to grab tubing and back it off @ time of inspection. All equipment on site looked ok. |
2507273 | Primary Facility | 2016-07-21 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Rig crew attempting to get overshot on to 2 3/8" tubing in well bore @ time of inspection in order to unscrew tubing and retrieve from well bore. All equipment on site looked ok. |
2508465 | Primary Facility | 2016-08-03 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Rig tagged top of 2 3/8" tubing @ 305' after pulling last 43' section of tubing that would come free. The old bent-rotted 7" casing is hanging up the Rig's tools preventing them from getting over 2 3/8" tubing to unscrew and pull free section. Still trying to get on tubing @ time of this inspection. All equipment on site looked ok. |
2510096 | Primary Facility | 2016-08-04 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Rig could not get past rotted 7" casing to get to and retrieve 2 3/8" tubing. Moved service Rig off and waiting for a larger cable tool Rig to move in and retrieve enough 7" to get to tubing. All equipment on site looked ok. |
2520604 | Primary Facility | 2016-09-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Operator back on site with cable tool Rig-ran camera to 219'-noted bent 7"@53'-top of 2 3/8" tubing noted @ 304'. The Rig was at 230' running a 4 11/16" casing swage at the time of inspection. All equipment on site looked ok. |
2522586 | Primary Facility | 2016-09-26 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Service Rig has pulled 39' of 6 1/4" casing so far at time of inspection. Witnessed crew run the camera down hole ahead of the next casing fishing trip. All equipment looked ok. |
2524158 | Primary Facility | 2016-09-28 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | The plugging Rig ran an 8" swage to 35'-retooled and ran in to 44' and was putting a trip spear on to try and run in to get hold of the 2 3/8" production tubing at the time of this inspection. All equipment on site looked ok. |
2524880 | Primary Facility | 2016-10-04 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | The plugging Rig is still trying to get through the old 7" casing at 39' and was putting on a 6 1/4" bull dog spear to run back in at the time of this inspection. All equipment on site looked ok. |
2528539 | Primary Facility | 2016-10-17 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | The cable tool plugging Rig was shut down waiting on a special drilling bit to arrive at the time of this inspection. The forward plan is to drill over the short section of bent casing stuck in the hole and then pull it out. All equipment on site looked ok. |
2605970 | Primary Facility | 2017-06-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | The operator was moving a service rig and equipment back on to this well to finish the plugging operation at the time of this inspection. All equipment on site looked ok. |
For data sources see[7]