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Well ID: 37-005-28081 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Cowanshannock Township | |
Operator Name: BLX INC | |
Well Pad ID: | |
Farm/Lease Name: ARTHUR B STROUPE 1 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2005-06-15 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.830576 | |
Longitude: -79.325853 |
Date | Event |
---|---|
2005-06-15 | New Permit Application |
2006-01-04 | Performed Spud Operation |
2006-01-12 | Drilling Completion |
2006-03-03 | NEWLY DRILLED |
2006-03-06 | Perforation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2006 | BLX INC | 4740.00 | 161 | 0.00 | 0 | 0.00 | 0 |
2007 | BLX INC | 5113.00 | 271 | 0.00 | 0 | 0.00 | 0 |
2008 | BLX INC | 4568.00 | 299 | 0.00 | 0 | 0.00 | 0 |
2009 | BLX INC | 4182.00 | 293 | 0.00 | 0 | 0.00 | 0 |
2010 | BLX INC | 2,664.50 | 191 | 0.00 | 0 | 0.00 | 0 |
2011 | BLX INC | 4,349.00 | 279 | 0.00 | 0 | 0.00 | 0 |
2012 | BLX INC | 3,434.00 | 258 | 0.00 | 0 | 0.00 | 0 |
2013 | BLX INC | 3,066.00 | 239 | 0.00 | 0 | 0.00 | 0 |
2014 | BLX INC | 2,695.00 | 171 | 0.00 | 0 | 0.00 | 0 |
2015 | BLX INC | 2,662.00 | 143 | 0.00 | 0 | 0.00 | 0 |
2016 | BLX INC | 2,441.00 | 114 | 0.00 | 0 | 0.00 | 0 |
2017 | BLX INC | 2,222.00 | 272 | 0.00 | 0 | 0.00 | 0 |
2018 | BLX INC | 2,132.00 | 276 | 0.00 | 0 | 0.00 | 0 |
2019 | BLX INC | 1,927.00 | 203 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | BLX INC | Produced Fluid | 28.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1506603 | Primary Facility | 2006-01-10 | Drilling/Alteration | No Violations Noted | Well spudded 1/6/06 by Whipstock,Pit ok,E&S ok |
1506605 | Primary Facility | 2006-01-06 | Drilling/Alteration | No Violations Noted | Rig moving on location.Pit ok,E&S ok |
1973854 | Primary Facility | 2011-05-18 | Routine/Complete Inspection | No Violations Noted | |
2028792 | Primary Facility | 2011-12-21 | Routine/Complete Inspection | No Violations Noted | Producing gas. Tag, tank, e&s ok. |
2264088 | Primary Facility | 2014-04-18 | Routine/Complete Inspection | No Violations Noted | Well appeared to be equipped for production. Brine tanks located onsite and they appeared to be in sound condition. There was no observed accelerated erosion or sedimentation in relation to the site or access road. |
2666231 | Primary Facility | 2017-12-01 | Routine/Complete Inspection | No Violations Noted | This well is tagged and in production. The annulus is shut. The well head casing, equipment and grounded 100 bbl fiberglass tank look ok. |
2760641 | Primary Facility | 2018-08-06 | Routine/Complete Inspection | No Violations Noted | This well is tagged and in production. The annulus is shut. The well head casing, piping, equipment and grounded 100 bbl fiberglass fluid collection tank look ok. |
For data sources see[7]