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Well ID: 37-005-28571 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Dayton Borough | |
Operator Name: US ENERGY EXPLORATION CORP | |
Well Pad ID: | |
Farm/Lease Name: R MILLER 1 | |
License Status: | |
Spud Date: | |
Permit Date: 2006-03-01 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.877817 | |
Longitude: -79.244095 |
Date | Event |
---|---|
2006-03-01 | New Permit Application |
2006-03-01 | Performed Spud Operation |
2009-09-28 | New Permit Application |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | US ENERGY EXPLORATION CORP | 2,535.00 | 360 | 0.00 | 0 | 0.00 | 0 |
2009 | US ENERGY EXPLORATION CORP | 1,487.00 | 360 | 0.00 | 0 | 0.00 | 0 |
2010 | US ENERGY EXPLORATION CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | US ENERGY EXPLORATION CORP | 1,811.00 | 360 | 0.00 | 0 | 0.00 | 0 |
2012 | US ENERGY EXPLORATION CORP | 892.00 | 360 | 0.00 | 0 | 0.00 | 0 |
2013 | US ENERGY EXPLORATION CORP | 1,273.00 | 360 | 0.00 | 0 | 0.00 | 0 |
2014 | US ENERGY EXPLORATION CORP | 1,015.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | US ENERGY EXPLORATION CORP | 1,337.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | US ENERGY EXPLORATION CORP | 791.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | US ENERGY EXPLORATION CORP | 540.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | US ENERGY EXPLORATION CORP | 347.00 | 330 | 0.00 | 0 | 0.00 | 0 |
2019 | US ENERGY EXPLORATION CORP | 584.00 | 330 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1520984 | Primary Facility | 2006-03-03 | Drilling/Alteration | No Violations Noted | WELL SPUD 3/03/06/PIK OK/E&S OK |
1699564 | Primary Facility | 2008-03-14 | Routine/Complete Inspection | No Violations Noted | |
1855827 | Primary Facility | 2010-01-13 | Routine/Complete Inspection | Pending | Noted possible issue with respect to drill cutting disposal. |
1856578 | Primary Facility | 2010-01-12 | Drilling/Alteration | No Violations Noted | drill deeper in process @ 3570ft/E&S ok/ID&pit ok |
1871980 | Primary Facility | 2010-03-17 | Routine/Complete Inspection | No Violations Noted | Drilling had been completed, well apeared to have been equipped for production at the time of the inspection. Site had been regraded. Inspection performed in conjunction with Mike Morgart to evaluate the site for evidence of the possibility of the presence of a seasonal high groundwater table that would have precluded disposal of the drill cuttings via encapsulation. No evidence was found onsite that would show this was the case. In future cases where soils information shows the possibility of a high seasonal groundwater table the operator should consider the land application of drill cuttings as outlined in 78.63 as an alternative to the encapsulation of the cuttings. |
2146345 | Primary Facility | 2013-03-08 | Routine/Complete Inspection | No Violations Noted | Well appeared to be equipped for production. Brine tank located onsite and it appeared to be in sound condition. There was no observed accelerated erosion or sedimentation in relation to the well site. |
2586303 | Primary Facility | 2017-04-24 | Routine/Complete Inspection | No Violations Noted | Well tagged-on-annulus open. Well head casing-equipment-50 bbl fiberglass tank look ok. |
For data sources see[6]