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Well ID: 37-005-29385 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: North Buffalo Township | |
Operator Name: MDS ENERGY DEV LLC | |
Well Pad ID: | |
Farm/Lease Name: RONALD G SHAFER ET UX 2-23 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2007-07-25 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.798513 | |
Longitude: -79.582139 |
Date | Event |
---|---|
2007-07-25 | New Permit Application |
2008-01-07 | Performed Spud Operation |
2008-01-10 | Drilling Completion |
2008-05-30 | Perforation |
2008-06-05 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | MDS ENERGY LTD | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | MDS ENERGY LTD | 6609.00 | 94 | 0.00 | 0 | 0.00 | 0 |
2010 | MDS ENERGY LTD | 7,783.00 | 259 | 0.00 | 0 | 0.00 | 0 |
2011 | MDS ENERGY LTD | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | MDS ENERGY LTD | 6,712.00 | 348 | 0.00 | 0 | 0.00 | 0 |
2013 | MDS ENERGY LTD | 5,754.00 | 344 | 0.00 | 0 | 0.00 | 0 |
2014 | MDS ENERGY LTD | 4,879.00 | 342 | 0.00 | 0 | 0.00 | 0 |
2015 | MDS ENERGY DEV LLC | 3,795.00 | 332 | 0.00 | 0 | 0.00 | 0 |
2016 | MDS ENERGY DEV LLC | 3,018.00 | 234 | 0.00 | 0 | 0.00 | 0 |
2017 | MDS ENERGY DEV LLC | 3,035.00 | 250 | 0.00 | 0 | 0.00 | 0 |
2018 | MDS ENERGY DEV LLC | 3,183.00 | 272 | 0.00 | 0 | 0.00 | 0 |
2019 | MDS ENERGY DEV LLC | 2,612.00 | 250 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2008 | MDS ENERGY LTD | Brine | 135.00 Bbl | Road Spreading | |
2011 | MDS ENERGY LTD | Produced Fluid | 40.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2014 | MDS ENERGY LTD | Produced Fluid | 80.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2014 | MDS ENERGY LTD | Produced Fluid | 80 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1682698 | Primary Facility | 2008-01-14 | Drilling/Alteration | No Violations Noted | WELL DRILLED - PIT LINED, FREEBOARD, E/S OK |
1887963 | Primary Facility | 2010-05-26 | Routine/Complete Inspection | No Violations Noted | Well is equipped for production. Tag located. Brine Tank appears to be in sound condition. There are no E&S concerns at this time. |
1898421 | Primary Facility | 2010-06-25 | Routine/Complete Inspection | No Violations Noted | ID tag in meter box. Tank and E&S ok. Pumpjack on well. Producing gas. |
2042024 | Primary Facility | 2012-02-10 | Routine/Complete Inspection | No Violations Noted | Pumpjack on well. Tag, tank, e&s ok. |
2677499 | Primary Facility | 2018-01-03 | Routine/Complete Inspection | No Violations Noted | This well is tagged and in production. The annulus is shut. The well head casing, pumpjack, production equipment and grounded 100 bbl fiberglass tank look ok. |
For data sources see[7]