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37-005-29880

Well Details

Well ID: 37-005-29880
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Wayne Township
Operator Name: US ENERGY EXPLORATION CORP
Well Pad ID:
Farm/Lease Name: CLOWSER 1
License Status: ACTIVE
Spud Date:
Permit Date: 2008-06-23
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.869795
Longitude: -79.242078

For data sources see[1][2][3]

Well History

Date Event
2008-06-23 New Permit Application
2008-07-29 Performed Spud Operation
2008-08-12 Drilling Completion
2008-08-19 Perforation
2009-03-25 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 US ENERGY EXPLORATION CORP 1457.00 60 0.00 0 0.00 0
2009 US ENERGY EXPLORATION CORP 6244.00 360 0.00 0 0.00 0
2010 US ENERGY EXPLORATION CORP 2,518.00 360 0.00 0 0.00 0
2011 US ENERGY EXPLORATION CORP 1,298.00 360 0.00 0 0.00 0
2012 US ENERGY EXPLORATION CORP 960.00 360 0.00 0 0.00 0
2013 US ENERGY EXPLORATION CORP 1,108.00 360 0.00 0 0.00 0
2014 US ENERGY EXPLORATION CORP 526.00 365 0.00 0 0.00 0
2015 US ENERGY EXPLORATION CORP 480.00 365 0.00 0 0.00 0
2016 US ENERGY EXPLORATION CORP 203.00 240 0.00 0 0.00 0
2017 US ENERGY EXPLORATION CORP 204.00 305 0.00 0 0.00 0
2018 US ENERGY EXPLORATION CORP 230.00 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1716174 Primary Facility 2008-06-16 Routine/Complete Inspection No Violations Noted site not made/waiver ok
1727942 Primary Facility 2008-08-05 Drilling/Alteration No Violations Noted Spudded 7/31/08. Rig shut down @ time of inspection. Pit/freeboard/E&S controls OK.
1816056 Primary Facility 2009-07-28 Site Restoration No Violations Noted Drilling was completed on 08/12/08. Well appeared to be equipped for production at the time of the inspection. Brine tank located onsite and appeared to be in sound condition. Well-site had been regraded and the vegetative cover met the 70% uniform coverage criteria.
2846947 Primary Facility 2019-03-01 Administrative/File Review No Violations Noted

For data sources see[6]

References