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37-007-20113

Well Details

Well ID: 37-007-20113
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Country: United States
State: Pennsylvania
County: Beaver
Municipality: Economy Borough
Operator Name: DC LAND MANAGEMENT LLC
Well Pad ID:
Farm/Lease Name: BIGRIGG 14
License Status: Inactive
Spud Date: 1983-05-10
Permit Date: 1982-06-24
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.651863
Longitude: -80.211890

For data sources see[1][2][3]

Well History

Date Event
1982-06-24 New Permit Application
1983-05-10 Performed Spud Operation
1983-05-23 Drilling Completion
1984-09-26 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1994 TEVEBAUGH MGMT CO 0.00 0 13.71 365 0.00 0
2000 TEVEBAUGH MGMT CO 38.29 365 10.33 365 0.00 0
2001 TEVEBAUGH MGMT CO 29.65 365 5.29 365 0.00 0
2002 TEVEBAUGH MGMT CO 38.69 365 0.00 0 0.00 0
2005 BIALY GAS PRODUCTION LLC 20.98 152 0.00 0 0.00 0
2006 BIALY GAS PRODUCTION LLC 0.00 0 0.00 0 0.00 0
2008 BIALY GAS PRODUCTION LLC 0.00 0 6.62 365 0.00 0
2009 BIALY GAS PRODUCTION LLC 0.00 0 0.00 0 0.00 0
2010 BIALY GAS PRODUCTION LLC 0.00 0 0.00 0 0.00 0
2014 DC LAND MANAGEMENT LLC 0.00 0 0.00 0 0.00 0
2015 DC LAND MANAGEMENT LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
210182 Primary Facility 1988-02-03 Routine/Complete Inspection No Violations Noted
2815908 Primary Facility 2018-12-13 Routine/Complete Inspection No Violations Noted Operator has applied for inactive status. The casing is cemented and the well is intact. There is a need for some surface work not related to the well itself. The base of the jack could be updated and gas lines need repairs. The operator has stock piled new 2" plastic gas line as well as culvert pipe to improve access.

For data sources see[6]

References