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Well ID: 37-007-20283 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Beaver | |
Municipality: South Beaver Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: DBC | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: 2007-04-04 | |
Well Type: COMB. OIL&GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 40.730139 | |
Longitude: -80.478917 |
Date | Event |
---|---|
2007-04-04 | New Permit Application |
2007-04-23 | Performed Spud Operation |
2016-07-16 | Begin Plugging |
2016-08-11 | Finished Plugging |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2009 | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 | |
2010 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 219.00 Bbl | INJECTION DISPOSAL WELL | 34-119-28780 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 179.67 Bbl | INJECTION DISPOSAL WELL | 34-031-27241 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 179.67 Bbl | INJECTION DISPOSAL WELL | 34-031-27177 |
2016 | CHESAPEAKE APPALACHIA LLC | Fracturing Fluid Waste | 42.87 Tons | LANDFILL | 06-08438 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 179.67 Bbl | INJECTION DISPOSAL WELL | 34-031-27178 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 1,575.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 2014-184 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 706.00 Bbl | INJECTION DISPOSAL WELL | 34-157-25506 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1629615 | Primary Facility | 2007-06-08 | Drilling/Alteration | No Violations Noted | RIGGING UP. |
1638720 | Primary Facility | 2007-06-21 | Drilling/Alteration | No Violations Noted | PRE-DRILL SAFETY MEETING. TALK OVER ISSUES BEFORE START OF DRILLING. |
1640938 | Primary Facility | 2007-06-27 | Drilling/Alteration | No Violations Noted | DRILL MOUSE AND RAT HOLE. |
1641093 | Primary Facility | 2007-07-02 | Drilling/Alteration | No Violations Noted | PATTERSON DRILLING RIG 490; RAN 1073 FEET, 13 3/8 INCHES |
1641095 | Primary Facility | 2007-07-11 | Drilling/Alteration | No Violations Noted | DRILL 12 1/4 INCH HOLE @ 5057 FEET. |
1641098 | Primary Facility | 2007-07-18 | Drilling/Alteration | No Violations Noted | TRIP BIT OUT OF HOLE @ 5901 FEET. |
1641099 | Primary Facility | 2007-07-23 | Drilling/Alteration | No Violations Noted | AT 6704 FEET, TRIP OUT HOLE TO LOG WELL |
1646960 | Primary Facility | 2007-08-07 | Drilling/Alteration | No Violations Noted | T.O.H. WITH 8 1/2 INCH BIT. 9069 FEET DEPTH. |
1651692 | Primary Facility | 2007-09-05 | Drilling/Alteration | No Violations Noted | SET UP TO RUN CEMENT. |
1651693 | Primary Facility | 2007-09-06 | Drilling/Alteration | No Violations Noted | TRIP D.P. OUT OF HOLE - EMERALD TOOL (HALCO) LOGGING. |
1671693 | Primary Facility | 2007-11-21 | Drilling/Alteration | No Violations Noted | SWABBING WELL AFTER FRAC. WELL FLOWED BACK ON ITS OWN. WILL TREAT NEXT ZONE ON 11/20/07 AND 3RD ZONE ON 12/5/07 |
1671695 | Primary Facility | 2007-09-06 | Drilling/Alteration | No Violations Noted | 11033' OUT OF HOLE CHANGE BIT. RUNNING HARDER BIT #9 - FORMATION IS DRILLING VERY HARD - HAULING WATER FROM PIT TOOK OUT 17 LOADS |
2187554 | Primary Facility | 2013-07-10 | Routine/Complete Inspection | No Violations Noted | THIS WELL WAS TRANSFERED TO CHESAPEAKE. ASSET MANAGER SAID THE PAPERWORK IS BEING PREPARED TO PLUG THIS WELL. |
2286187 | Primary Facility | 2014-07-01 | Routine/Complete Inspection | No Violations Noted | THIS WELL AND IT'S SURFACE EQUIPTMENT APPEAR TO BE IN GOOD CONDITION. CHESAPEAKE HAS NO PLANS TO PRODUCE THIS WELL ,AND IT WILL BE PLUGGED. |
2378964 | Primary Facility | 2015-05-08 | Routine/Complete Inspection | No Violations Noted | THIS WELL WAS DRILLED BY ERGON IN 2007 AND TRANSFERED TO CHESAPEAKE IN 2010. THE WELL NEVER WAS PUT INTO PRODUCTION. CHESAPEAKE WILL PLUG THE WELL IN JUNE. |
2378966 | Primary Facility | 2015-05-13 | Routine/Complete Inspection | No Violations Noted | INSPECTED WELL AND PAD WITH WQS TO FIND CULVERT PIPES LOCATED UNDER THE PAD. THIS WELL IS TO BE PLUGGED. |
2439750 | Primary Facility | 2015-12-04 | Routine/Complete Inspection | No Violations Noted | CHESAPEAKE'S LOCK HAS BEEN REMOVED FROM THE ACCESS ROAD GATE. CHESAPEAKE PROMISED TO PLUG THIS WELL IN JUNE 2015. IN MAY I WAS TOLD THIER ATTORNEYS FOUND THAT THE WELL WAS SOLD TO ERGON IN 2010. THE WELL WAS THEN TO BE SOLD TO A PRIVATE OWNER, BUT THE BUYER BBACKED OUT OF THE DEAL. CHESAPEAKE PUT A TRANSFER INTO THE STATE BUT IT WAS NOT SIGNED BY ERGON. CHESAPEAKE AND THE STATE HAVE TRIED TO CONTACT ERGON BUT THEY HAVE NOT RETURNED CALLS. STATE RECORDS SHOW THAT CHESAPEAKE IS THE OWNER. |
2447247 | Primary Facility | 2016-02-01 | Routine/Complete Inspection | Violation(s) Noted | |
2521331 | Primary Facility | 2016-08-03 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | MERCER CUT AND BEGAN PULLING 95/8" CASING. |
2521333 | Primary Facility | 2016-07-15 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | THE PAD AROUND THE WELL IS COVERED. FRAC TANKS ARE SET.
NO ACTIVITY. |
2521337 | Primary Facility | 2016-07-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | THE TUBING IN THE WELL FAILED A PRESSURE TEST AND WILL BE PULLED TO LOCATE THE HOLE.
THE SITE IS OK. |
2521343 | Primary Facility | 2016-07-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | 7/19/16 THE TUBING WAS PULLED AND MERCER RIG IS RUNNING IT BACK IN.
7/20/16 THE PLUG FAILED AND A CIBP WAS SET AT 9,988'. |
2521348 | Primary Facility | 2016-07-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | CIBP WAS SET AT 10,025'. CEMENT PLUG FROM 10,025' TO 9,837'. 5.5" CASING WAS CUT AT 9,700'. CASING JACKS LIFTED WITH 400,000# AND THE CASING DID NOT RELEASE. CASING WAS PERFED EVERY 50" TO 8,692'. CASING HAD BEEN CUT AT9,132' AND PULLED WITH 340,000#. |
2521354 | Primary Facility | 2016-07-27 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | A CEMENT PLUG WAS SET ON A GELL SPACER FROM 9,111' TO 8,282'. MERSER PULLED TUBING ABOVE THE PLUG AND LEFT THE SITE. |
2534283 | Primary Facility | 2016-10-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | A NEW WELLHEAD HAS BEEN INSTALLED ON THIS LEAKING WELL. WASTE CONTAINERS ARE ON THE PAD.
THE SITE IS IN GOOD CONDITION. |
2547208 | Primary Facility | 2016-09-21 | Plugging(Includes Plugged/Mined Through) | Pending | AFTER PLUGGING WAS COMPLETED THE WELL WAS STILL LEAKING. CHESAPEAKE WAS NOTIFIED AND THEY ARE WORKING ON THE NEXT STEP TO STOP THE FLOW OF GAS. |
2563400 | Primary Facility | 2017-01-05 | Plugging(Includes Plugged/Mined Through) | Pending | STONE DRILLING IS SET UP TO DRILL OUT CEMENT PLUG IN AND BELOW 133/8" CASING. THEY WILL TRY TO LOCATE SOURCE OF LEAKING GAS. |
2563405 | Primary Facility | 2017-01-12 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | STONE DRILLING DRILLED TO 1,100'. THIS DEPTH IS 27' BELOW THE 133/8" CASING. OVER 500 BBL'S OF CLEAN WATER WAS USED TO FLUSH OUT THE CASING. WHEN A CAMERA WAS RUN THE WATER WAS CLEAR TILL IT NEARED THE BOTTOM. THIS MAY BE WHERE THE GAS IS ENTERING THE WELL. |
2565027 | Primary Facility | 2016-11-16 | Plugging(Includes Plugged/Mined Through) | Pending | A VAC TRUCK REMOVED THE WATER FROM THE CELLAR AND CASING. GAS WAS SEEN TO BE COMING FROM INSIDE THE 133/8" CASING. |
2565031 | Primary Facility | 2016-11-16 | Plugging(Includes Plugged/Mined Through) | Pending | A HYDRO EXCAVATOR IS SUCKING THE PEA GRAVEL FROM THE 133/8" CASING. THEY HAVE REACHED A DEPTH OF 500'. THEY WILL KEEP GOING TO 795' WHICH IS THE DEPTH OF THE 1ST PLUG. |
2701747 | Primary Facility | 2018-03-06 | Routine/Complete Inspection | Violation(s) Noted | At the direction of Oil & Gas Southwest District management WQS Higgins conducted an onsite inspection of the site. The site was constructed in 2007 by Ergon Exploration. In 2010 the site and well were purchased by Chesapeake Appalachia. In 2016 Chesapeake began the process of plugging the well, work that is still ongoing at the time of the inspection. According to Department documents plugging was completed in January 2017, therefore putting the restoration by deadline to November 2017. In conjunction with plugging the well Chesapeake submitted an ESCGP for the site restoration earthwork that would be necessary. In this submittal Chesapeake outlined stream encroachments that were unpermitted by the original operator, Ergon, and how Chesapeake was proposing to restore the site and address the stream encroachments. |
2817347 | Primary Facility | 2018-12-19 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well is plugged but the site has not been restored. The well appears to be in good condition and not leaking. After the site has been restored the well will need to be lowered. With an Altair 5X I did not detect any gas or H2S. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2447247 | 745143 | 2016-02-01 | 2016-08-11 | OGA3220(A) | Environmental Health & Safety | Well was plugged 8/11/2016 |
2701747 | 810699 | 2018-03-06 | 105.11(a) | Environmental Health & Safety | ||
2701747 | 810700 | 2016-02-01 | OGA3220(A) | Environmental Health & Safety | ||
2701747 | 810701 | 2018-03-06 | 78a65(a)2 | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
745143 | 334242 | NOV - Notice of Violation | 2016-08-11 | ||||
745143 | 362343 | NOV - Notice of Violation | |||||
810699 | 362343 | NOV - Notice of Violation | |||||
810700 | 362343 | NOV - Notice of Violation | |||||
810701 | 362343 | NOV - Notice of Violation |
For data sources see[7]