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| Well ID: 37-007-20284 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Beaver | |
| Municipality: Ohioville Borough | |
| Operator Name: CHESAPEAKE APPALACHIA LLC | |
| Well Pad ID: | |
| Farm/Lease Name: THARP 1 | |
| License Status: Plugged and Abandoned | |
| Spud Date: | |
| Permit Date: 2007-04-09 | |
| Well Type: COMB. OIL&GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: Yes | |
| Latitude: 40.726450 | |
| Longitude: -80.512392 |
| Date | Event |
|---|---|
| 2007-04-09 | New Permit Application |
| 2008-02-24 | Performed Spud Operation |
| 2013-09-25 | Begin Plugging |
| 2013-10-01 | Finished Plugging |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 2007 | PETRO EVALUATION SVC INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2008 | PETRO EVALUATION SVC INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2010 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2011 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2012 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2013 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2014 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2015 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 1943162 | Primary Facility | 2011-01-05 | Routine/Complete Inspection | No Violations Noted | On January 5th, 2011 I conducted a routine inspection of the above site. Drilling was completed however the well was not in production. The access road was in good condition. A well tag was present. No spills, leaks, or accelerated erosion were observed at the time of the inspection. The site was well vegetated. |
| 1955502 | Primary Facility | 2011-01-05 | Routine/Complete Inspection | No Violations Noted | 95/8" CASING STICKING UP. VALVE IS CLOSED.
WELL IS TO BE PLUGGED AND A NEW WELL DRILLED. |
| 2078709 | Primary Facility | 2012-06-21 | Routine/Complete Inspection | No Violations Noted | John Ley WQS, SWRO was on site to conduct a routine inspection. At the time of this inspection, the well sign, E&S plan, PPC plan, ESCGP-1 were onsite. The site wsa gated for security. The Well was drilled. Bmp's installed were functioning according to the E&S plan. No accelerated erosion or sedimentation issues were noted with site or access road. No industrial waste issues were present. |
| 2187557 | Primary Facility | 2013-07-10 | Routine/Complete Inspection | No Violations Noted | THIS WELL WAS TRANSFERED TO CHESAPEAKE. ASSET MANAGER SAID THE PAPERWORK IS BEING PREPARED TO PLUG THIS WELL. |
| 2206062 | Primary Facility | 2013-09-05 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | CHESAPEAKE PLANS TO PLUG THIS WELL. THERE ARE BUBBLES COMINIG FROM INSIDE AND OUTSIDE THE CONDUCTOR. A NEW ACCESS HAS BEEN BUILT FROM THE JAMES THARP 3H PAD. |
| 2208033 | Primary Facility | 2013-09-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | A MEASURING LINE HIT AN OBSTRUCTION AT 5,445'. EQUIPTMENT BEING SET UP WITH A RIG COMING LATER IN THE DAY. |
| 2210168 | Primary Facility | 2013-10-01 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | WELL HAS CEMENT PLUGS UP TO 782'. TOP OF THE WELL WILL BE FILLED WITH PEA GRAVEL, AND A MARKER INSTALLED. |
| 2213892 | Primary Facility | 2013-10-11 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | WELL IS PLUGGED. DEP SPEC'S WERE MET. ALL EQUIPTMENT HAS BEEN REMOVED. |
| 2567662 | Primary Facility | 2017-03-01 | Routine/Complete Inspection | No Violations Noted | ON 3/1/17 I MET WITH CHESAPEAKE PERSONEL ALONG WITH GEO PETRO PERSONEL AFTER A REPORT OF BUBBLES NEAR THIS PLUGGED WELL. WE COULD SEE BUBBLES BUT I COULD NOT DETECT ANY GAS WITH A MSA 62S. ON THIS DAY THERE WAS ASTEADY RAIN SO I WILL RE-INSPECT WHEN THERE IS BETTER WEATHER. |
For data sources see[6]