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Well ID: 37-007-20297 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Beaver | |
Municipality: Franklin Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: 149612 | |
Farm/Lease Name: YMCA 590433 | |
License Status: | |
Spud Date: | |
Permit Date: 2010-02-02 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 40.813922 | |
Longitude: -80.208025 |
Date | Event |
---|---|
2010-02-02 | New Permit Application |
2010-03-03 | Performed Spud Operation |
2010-03-15 | Drilling Completion |
2010-08-09 | DEVIATED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | EQT PROD CO | Drilling Fluid Waste | 1,410.00 Bbl | IDENTIFY METHOD IN COMMENTS | |
2010 | EQT PROD CO | Drilling Fluid Waste | 20.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2010 | EQT PROD CO | Drilling Fluid Waste | 870.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 301353 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1869545 | Primary Facility | 2010-03-10 | Drilling/Alteration | No Violations Noted | HIGHLANDS RIG 4 DRILLING TOP HOLE FOR THIS MARCELLUS WELL. |
1869551 | Primary Facility | 2010-03-04 | Drilling/Alteration | No Violations Noted | SUPERIOR CEMENTING 133/8" CASING. MARCELLUS WELL. |
1882760 | Primary Facility | 2010-03-29 | Drilling/Alteration | No Violations Noted | TOP HOLE COMPLETE. RIG AND SUPPORT EQUIPTMENT GONE. SITE, E&S, & ACCESS, OK. |
1882772 | Primary Facility | 2010-04-05 | Drilling/Alteration | No Violations Noted | SERVICE RIG IS UP. WELL WILL BE PERFED AT 5160'. HORIZONTAL PART OF WELL WILL NOT BE DRILLED. |
1882798 | Primary Facility | 2010-04-21 | Drilling/Alteration | No Violations Noted | DRILLING COMPLETE. WELL WILL REMAIN VERTICAL. PIT WAS DRAINED, SOLIDIFIED, AND BURIED. |
1883284 | Primary Facility | 2010-04-29 | Routine/Complete Inspection | No Violations Noted | On April 29, 2010 I visited this site as a routine inspection. The well was drilled but not yet in production. The well site appeared to be in compliance. A site ID sign and E&S plan were posted on site. The access road was in good condition. E&S controls were in place according to the plan on site. There was no evidence of spills or leaks and no accelerated erosion was observed at the time of inspection. The operator should continue to inspect the E&S controls routinely and after each runoff event until the site has reached uniform 70% vegetative cover. |
1913145 | Primary Facility | 2010-08-10 | Routine/Complete Inspection | No Violations Noted | THIS MARCELLUS SITE IS RESTORED, VEGETATED, AND FENCED. THE ACCESS IS STONED. |
1928579 | Primary Facility | 2010-10-06 | Routine/Complete Inspection | No Violations Noted | On October 6th, 2010 I visited this site as a routine inspection. The well was drilled but not yet in production. The well site appeared to be in compliance. A site ID sign and E&S plan were posted on site. The access road was in good condition. E&S controls were in place according to the plan on site. There was no evidence of spills or leaks and no accelerated erosion was observed at the time of inspection. The operator should continue to inspect the E&S controls routinely and after each runoff event until the site has reached uniform 70% vegetative cover. The site was well vegetated and surrounded by security fence. |
2016831 | Primary Facility | 2011-10-28 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | SERVICE RIG AND SUPPORT EQUIPTMENT SET UP, BUT THERE IS NO ACTIVITY. |
2016862 | Primary Facility | 2011-10-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | WELL IS TO BE PLUGGED. NO RIG OR EQUIPTMENT ON THE PAD. |
2018674 | Primary Facility | 2011-11-08 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | HYDROCARBON WELL SERVICES RUNNING TUBING TO SET CEMENT PLUGS. |
2023015 | Primary Facility | 2011-11-15 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | HYDROCARBON JACKING 4080' OF 5.5" CASING. THIS IS A VERTICLE MARCELLUS WELL. |
2064338 | Primary Facility | 2012-04-17 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | EXCAVATION AROUND WELL WAS FILLED WITH WATER AND NO BUBBLES CAN BE SEEN. |
2064347 | Primary Facility | 2012-04-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | WELL IS PLUGGED. MEETING WITH EQT AND YMCA TO DISCUSS THE FUTURE OF THE VENT . |
2064364 | Primary Facility | 2012-04-16 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | AT WELL WITH HYDROCARBON STEVE JONES TO TRY AND FIND SOURCE OF BUBBLES.THE WELL HEAD IS EXCAVATED TO HELP. |
2121625 | Primary Facility | 2012-12-05 | Routine/Complete Inspection | No Violations Noted | John Ley WQS, SWRO was on site to conduct a routine inspection. At the time of this inspection, the well sign was onsite. The well was drilled and there was a vent pipe on site. Bmp's installed were functioning. No accelerated erosion or sedimentation issues were noted on site or the access road. The hillsides had been stabilized and had good growth with at least 70% vegetation. |
2169316 | Primary Facility | 2013-05-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | WHEN WEL WAS PLUGGED IN 2011 GAS WAS DETECTED IN THE GROUND AROUND THE WELL. THE VENT WAS CHECKED FOR GAS FROM 5/4/12 TILL 7/20/12. % OF LEL RANGED FROM 6.0% TO 20.0%. ON THIS DAY THE % OF LEL WAS 9.0. THE SOURCE OF THE GAS HAS NOT BEEN DETERMINED. |
For data sources see[7]