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37-015-20865

Well Details

Well ID: 37-015-20865
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Country: United States
State: Pennsylvania
County: Bradford
Municipality: Orwell Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Well Pad ID: 149183
Farm/Lease Name: REXFORD 5H
License Status:
Spud Date:
Permit Date: 2010-05-06
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.877794
Longitude: -76.309322

For data sources see[1][2][3]

Well History

Date Event
2010-05-06 New Permit Application
2010-06-07 Performed Spud Operation
2010-10-08 Perforation
2014-02-14 DEVIATED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 CHESAPEAKE APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2011 CHESAPEAKE APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2012 CHESAPEAKE APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2013 CHESAPEAKE APPALACHIA LLC 233,209.00 90 0.00 0 0.00 0
2014 CHESAPEAKE APPALACHIA LLC 276,252.00 360 0.00 0 0.00 0
2015 CHESAPEAKE APPALACHIA LLC 108,221.00 354 0.00 0 0.00 0
2016 CHESAPEAKE APPALACHIA LLC 110,257.00 348 0.00 0 0.00 0
2017 CHESAPEAKE APPALACHIA LLC 131,829.00 340 0.00 0 0.00 0
2018 CHESAPEAKE APPALACHIA LLC 89,541.00 351 0.00 0 0.00 0
2019 CHESAPEAKE APPALACHIA LLC 68,812.00 364 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2012 CHESAPEAKE APPALACHIA LLC Produced Fluid 4,965.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 1,221.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC007
2013 CHESAPEAKE APPALACHIA LLC Fracing Fluid Waste 1,167.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC008
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 8,824.17 Bbl REUSE OTHER THAN ROAD SPREADING
2014 CHESAPEAKE APPALACHIA LLC Produced Fluid 100.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC010
2014 CHESAPEAKE APPALACHIA LLC Produced Fluid 4,893.62 Bbl REUSE OTHER THAN ROAD SPREADING
2014 CHESAPEAKE APPALACHIA LLC Produced Fluid 50.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC018
2015 CHESAPEAKE APPALACHIA LLC Produced Fluid 453.16 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 56.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 212.50 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC018
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 605.50 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 126.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC018
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 147.50 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NW011
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 58.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC010
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 5.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 58.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2017 CHESAPEAKE APPALACHIA LLC Produced Fluid 99.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2017 CHESAPEAKE APPALACHIA LLC Produced Fluid 382.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC018
2017 CHESAPEAKE APPALACHIA LLC Produced Fluid 55.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2017 CHESAPEAKE APPALACHIA LLC Produced Fluid 112.00 Bbl REUSE (AT WELL PAD)
2017 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 110.10 Bbl REUSE (AT WELL PAD)
2018 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 50.10 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008
2018 CHESAPEAKE APPALACHIA LLC Waste Water Treatment Sludge 0.40 Tons LANDFILL 301626

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1976895 Primary Facility 2011-05-18 Routine/Complete Inspection Violation(s) Noted 22% LEL combustible gas off of 13 5/8 vent port
1987627 Primary Facility 2011-07-14 Routine/Complete Inspection Outstanding Violations - No Viols Req'd 20 3 pressure on 13 3/8. 2 1/2% combustible gas being vented to atomosphere.
2001690 Primary Facility 2011-08-25 Routine/Complete Inspection Outstanding Violations - No Viols Req'd 40% combustible gas off of 13 3/8. 2% comb gas off of 9 5/8. Not vented to tank. No bubbles in cellar.
2024141 Primary Facility 2011-12-05 Routine/Complete Inspection No Violations Noted Visible bubbling in the cellar. Cannot determine where gas is coming from as cellar is filled with water. Bubbling may be from communication with the 2H.
2032643 Primary Facility 2012-01-05 Follow-up Inspection Outstanding Violations - No Viols Req'd 13 3/8' x 20' annulus leaking gas
2033422 Primary Facility 2012-01-11 Follow-up Inspection Outstanding Violations - No Viols Req'd drilling out frac plugs and are at 9606 at present
2049353 Primary Facility 2012-03-05 Drilling/Alteration No Violations Noted workover rig onsite. Crew onsite monitoring pressures
2049371 Primary Facility 2012-01-18 Drilling/Alteration No Violations Noted Flowback crew onsite monitoring pressures. Wireline run this AM. Logs run 1/17 and 1/18. Logs to be reviewed by engineers 1/19
2063654 Primary Facility 2012-03-12 Routine/Complete Inspection No Violations Noted 13 3/8 vent - 0% combustible gas, 0 psi
2098741 Primary Facility 2012-09-10 Routine/Complete Inspection No Violations Noted 13 3/8 casing pressure - gauge reads 0 psi, 0% combustible gas off of vent.
2098742 Primary Facility 2012-09-05 Routine/Complete Inspection No Violations Noted 13 3/8 casing pressure - gauge reads 0 psi, .5% combustible gas off of vent. Meter holds at
2098743 Primary Facility 2012-08-27 Routine/Complete Inspection No Violations Noted 13 3/8 casing pressure - gauge reads 0 psi, 1% combustible gas spike off of vent. Meter holds at .5% combustible gas
2098744 Primary Facility 2012-08-22 Routine/Complete Inspection No Violations Noted 13 3/8 casing pressure - gauge reads 0 psi, 1% combustible gas spike off of vent. Meter holds at .5% combustible gas
2098745 Primary Facility 2012-08-16 Routine/Complete Inspection No Violations Noted 13 3/8 X 9 5/8 casing pressure - gauge reads 0 psi, 0% combustible gas off of vent.
2098746 Primary Facility 2012-07-05 Routine/Complete Inspection No Violations Noted 13 3/8 X 9 5/8 casing pressure - gauge reads 0 psi, 0% combustible gas off of vent.
2120031 Primary Facility 2012-10-10 Routine/Complete Inspection No Violations Noted Back pressure vavle installed. Performing 48 hour shut-in tests. Well currently shut-in. 13 3/8 - 0 psi. 9 5/8 - 0 psi (pop-off valve installed). 5 1/2 - 275 psi.
2120677 Primary Facility 2012-10-03 Routine/Complete Inspection No Violations Noted 13 X 9 - 0 psi 0.2 %spike comb gas
2120685 Primary Facility 2012-09-25 Routine/Complete Inspection No Violations Noted 13 X 9 -(vented) - 0psi - 2% combustible gas spike
2194576 Primary Facility 2013-08-02 Routine/Complete Inspection No Violations Noted Inspection for 'Inactive Well Status".
2203364 Primary Facility 2013-09-04 Routine/Complete Inspection No Violations Noted
2239234 Primary Facility 2014-01-13 Routine/Complete Inspection No Violations Noted
2259257 Primary Facility 2014-04-02 Routine/Complete Inspection No Violations Noted
2265008 Primary Facility 2014-04-17 Routine/Complete Inspection No Violations Noted
2374247 Primary Facility 2015-05-28 Routine/Complete Inspection Outstanding Violations - No Viols Req'd
2493909 Primary Facility 2016-06-16 Follow-up Inspection Outstanding Violations - No Viols Req'd At time of inspection, arrived on site at 9:30a.m. On site to conclude the 72 hr. Pressure Build-up Test (PBUT) being performed on the 5H and the 2H as part of an ongoing migration investigation. I was accompanied by Eric Rooney (DEP Geologist), we met with Joel Mincer (lease operator for Chesapeake) and Tom Messing of Leidos. The wells were shut in on 6/13/16 at 10:15a.m. It was noticed that the pop off valves were still on the (28x20), (20x13¿), and (13¿x9¿) vent pipes on the 2H and on the (28x20) and (20x13¿) vent pipes on the 5H.

Tom called Charlie Olmsted of Chesapeake to let him know of the pop off valves and Charlie said the PBUT would be rescheduled for sometime in July. No gas samples or pressure reading were taken. I left the site at 10:50a.m.

2502272 Primary Facility 2016-07-18 Routine/Complete Inspection Outstanding Violations - No Viols Req'd At time of inspection, arrived on site at 13:10p.m. for a post 72hr pressure build up test (PBUT), the cellar was empty, I met with lease operators Joel Mincer and Joel Failie. They were setting up the wells for the 72hr PBUT, Joel Mincer had to go to the shop to get some connections, he returned about 15:00p.m. The production line was shut in at 15:30p.m. and the other annuli’s were shut in and set up with a digital recorder at 5:26p.m. The vent pipes from the 28" and 20" caps were set up with a 15lb pop off valve and they had a hose going to a plastic tank.

I left the site at 5:30p.m.

2503861 Primary Facility 2016-07-21 Follow-up Inspection Outstanding Violations - No Viols Req'd At time of inspection, arrived on site at 16:10p.m. to conclude the 72hr. Pressure Build-up Test (PBUT) being performed on the 2H and the 5H as part of an ongoing migration investigation. The cellar was empty. I met with Joel Mincer (lease operator for Chesapeake), Tom Messing and Shauna Erway of Leidos. The wells were shut in on 7/18/16 at 17:26,Tom used a Gas Explorer gas meter by Bascom Turner calibrated on 7/21/16 to check for gas show at all annuli’s, gas samples were taken if gas was detected. Pressures were taken from a 30psi pressure gauge for the 28" and 20" annuli’s, and from the SCADA digital pressure gauges on the wells for the rest of the annuli’s. The 28" and 20" annuli’s were set up with 15psi pop off valves and connected to poly tanks, there was no gas detected at the tanks. We started taking pressures at 17:25 on the 5H.

I left the site at 18:30p.m.

2575950 Primary Facility 2017-03-20 Routine/Complete Inspection No Violations Noted On March 20, 2017, the Department conducted a routine inspection at the Chesapeake Appalachia, LLC (Chesapeake) Rexford Location in Orwell Township, Bradford County. Andrew Hobbins, Water Quality Specialist, represented the Department. Nobody was present for Chesapeake.

The E&S plan, site sign and weekly inspection reports were on site and available for review. The site was mostly covered in about 8 inches of snow. PCSM has not been addressed at the site.

There were two well in production phase during the inspection. Both wells were labeled and no bubbling was observed in the well cellar. Two production tanks and two GPUs were on site. The production tanks were on secondary containment.

The ESGGP-2 permit expires 1/11/2021. A major modification was approved on January 12, 2016 to address PCSM. According to Department records, there are no active well permits for the Rexford Location. The well pad retains its original shape and has not been reduced in size. The Department recommends installi

2591654 Primary Facility 2017-05-08 Routine/Complete Inspection Outstanding Violations - Viols Req'd At time of inspection, arrived on site at 12:00p.m. for a pre-PBUT inspection.

The cellar was about half full of water with no bubbling noticed. The (28x20) annulus was set up with a pop off valve and a 60psi pressure gauge with 0psi on it. The (20x13) annulus was set up with a digital recorder and a 60psi pressure gauge with 0psi on it. The (13x9) annulus was set up with a SCADA digital pressure gauge with 0psi on it and the valve going to the production tank was closed. The (9x5) annulus was set up with a SCADA digital pressure gauge with 114psi on it and the valve going to the production tank was closed. The 5½ production casing was open and venting to the production tank with 0psi on the SCADA pressure gauge. There was 863psi on the production tubing. I left the site at 13:05 p.m.

2593893 Primary Facility 2017-05-11 Follow-up Inspection Outstanding Violations - Viols Req'd At time of inspection, arrived on site at 8:00a.m. to conclude the 72hr. Pressure Build-up Test (PBUT) being performed on the 2H and the 5H as part of an ongoing migration investigation. The cellar was about half full of water with no bubbling noticed. I met with Joel Fairlie of Chesapeake, Tom Messing and Shauna Erway of Leidos. The wells were shut in on 5/8/17 at 8:15a.m. Tom used a Gas Explorer gas meter by Bascom Turner to check for gas show at all annuli’s, gas samples were taken if gas was detected. Pressures were taken from SSI Technology Inc. pressure gauge for the 28" and 20" annuli’s, and from the SCADA digital pressure gauges on the wells for the rest of the annuli’s. The wells were still producing.

We started taking pressures at 8:20a.m. on the 5H. I left the site at 9:15a.m.

2756121 Primary Facility 2018-07-11 Routine/Complete Inspection Outstanding Violations - Viols Req'd Remarks: At time of inspection. On site to check for gas presence, gas flows and take samples from the annuli of the 2H and 5H wells. I was accompanied by DEP OGI Supervisor, Mike Panettieri and DEP OGI, David Schoonover. We met with Chesapeake Reps. Max Goff (Operations Engineer), Lester Peterson (Optimization Technician), Joe Riley (Well Tender) and Leidos Rep. Tom Messing.

- Lester used an Eco meter to check the fluid level in the (9x5) and (5/Prod) annuli on 7/5/18. Tom used a Gas Explorer gas meter (calibrated on 7/10/18) to check for gas shows at annuli and I used an Altair 5X gas meter (calibrated on 7/9/18) to confirm the results. Joe used a Digital Manometer 621 with a 1/4" orifice to check for any flow rates at annuli. There were no measurable gas flow rates detected at any annuli, cemented to surface, of the 2H or 5H wells at time of inspection. Both wells (28"x 20"), (20"x 13 3/8") and (13 3/8"x 9 5/8") annuli had been open and venting for several weeks prior to this inspection. The results of

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1976895 612379 05/18/2011 2011-05-18 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative
2591654 785122 2017-05-08 78a85(a)5 Environmental Health & Safety
2591654 785123 2017-05-08 78a86 Environmental Health & Safety
2593893 785660 2017-05-11 78a85(a)5 Environmental Health & Safety
2593893 785661 2017-05-11 78a86 Environmental Health & Safety
2756121 823278 2011-05-18 78a86 Environmental Health & Safety Originally cited on 5/18/11. Operator has performed remedial work on the 5H well between 1/21/12 - 2/20/12. (See attached well bore diagram for details). No gas flows were noted in cemented annuli of the 5H well at time of this inspection.
2756121 823279 2017-05-11 78a85(a)5 Environmental Health & Safety Originally cited on 5/8/17. No gas flows were noted in cemented annuli of the 5H well at time of this inspection.

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
612379 275910 NOV - Notice of Violation

For data sources see[7]

References