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Well ID: 37-015-20952 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Bradford | |
Municipality: Herrick Township | |
Operator Name: SWN PROD CO LLC | |
Well Pad ID: 148327 | |
Farm/Lease Name: GREENZWEIG 7H | |
License Status: | |
Spud Date: | |
Permit Date: 2010-06-09 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.772244 | |
Longitude: -76.225436 |
Date | Event |
---|---|
2010-06-09 | New Permit Application |
2011-08-02 | New Permit Application |
2012-04-23 | Performed Spud Operation |
2012-08-13 | Perforation |
2013-06-17 | DEVIATED |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2012-08-09 | 2012-08-09 | 6,438 | 5,563,614 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | AI-250 | Clearwater International | Acid Inhibitor | Isopropanol | 67-63-0 | 40.00 | 0.00077000 | |
Propargyl alcohol | 107-19-7 | 40.00 | 0.00077000 | |||||
2-Butoxyethanol | 111-76-2 | 40.00 | 0.00077000 | |||||
Southwestern Energy | Sand | |||||||
Southwestern Energy | Water/Produced Water | Quartz | 14808-60-7 | 100.00 | 8.04 | |||
H2O + Disolved Salts | 100.00 | 91.05 | ||||||
K-Bec | Biocide | Polyethylene glycol | 25322-68-3 | 60.00 | 0.02 | |||
2,2-Dibromo-3-nitrilopropionamide | 10222-01-2 | 20.00 | 0.00765000 | |||||
StimLube | Southwestern Energy | Friction Reducer | Distillates, petroleum, hydrotreated light | 64742-47-8 | 30.00 | 0.02 | ||
15 HCl | Acid | Hydrochloric acid | 7647-01-0 | 15.00 | 0.11 | |||
SI-112 | Clearwater International | Scale Inhibitor | Ethylene glycol | 107-21-1 | 40.00 | 0.00418000 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | SOUTHWESTERN ENERGY PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | SOUTHWESTERN ENERGY PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | SOUTHWESTERN ENERGY PROD CO | 353,859.00 | 100 | 0.00 | 0 | 0.00 | 0 |
2013 | SOUTHWESTERN ENERGY PROD CO | 994,428.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SOUTHWESTERN ENERGY PROD CO | 752,874.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SWN PROD CO LLC | 611,288.00 | 363 | 0.00 | 0 | 0.00 | 0 |
2016 | SWN PROD CO LLC | 520,111.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | SWN PROD CO LLC | 425,378.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | SWN PROD CO LLC | 352,547.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | SWN PROD CO LLC | 262,202.00 | 361 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2012 | SOUTHWESTERN ENERGY PROD CO | Drill Cuttings | 1,090.69 Tons | LANDFILL | 101247 |
2012 | SOUTHWESTERN ENERGY PROD CO | Fracing Fluid Waste | 40.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2013 | SOUTHWESTERN ENERGY PROD CO | Produced Fluid | 4,513.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2013 | SOUTHWESTERN ENERGY PROD CO | Fracturing Fluid Waste | 41.58 Tons | LANDFILL | 101247 |
2014 | SOUTHWESTERN ENERGY PROD CO | Produced Fluid | 1,720.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2015 | SWN PROD CO LLC | Produced Fluid | 723.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | SWN PROD CO LLC | Produced Fluid | 196.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2016 | SWN PROD CO LLC | Produced Fluid | 215.40 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2017 | SWN PROD CO LLC | Produced Fluid | 36.00 Bbl | SURFACE IMPOUNDMENT | 826342 |
2017 | SWN PROD CO LLC | Other Oil & Gas Wastes | 10.00 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2017 | SWN PROD CO LLC | Produced Fluid | 87.33 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2017 | SWN PROD CO LLC | Produced Fluid | 18.33 Bbl | REUSE (AT WELL PAD) | |
2017 | SWN PROD CO LLC | Other Oil & Gas Wastes | 17.83 Bbl | SURFACE IMPOUNDMENT | 826342 |
2018 | SWN PROD CO LLC | Other Oil & Gas Wastes | 18.33 Bbl | REUSE (AT WELL PAD) | |
2018 | SWN PROD CO LLC | Produced Fluid | 57.17 Bbl | SURFACE IMPOUNDMENT | 826342 |
2018 | SWN PROD CO LLC | Produced Fluid | 80.33 Bbl | REUSE (AT WELL PAD) | |
2018 | SWN PROD CO LLC | Produced Fluid | 212.32 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2019 | SWN PROD CO LLC | Produced Fluid | 18.33 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC035 |
2019 | SWN PROD CO LLC | Produced Fluid | 93.00 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2019 | SWN PROD CO LLC | Other Oil & Gas Wastes | 35.42 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2019 | SWN PROD CO LLC | Produced Fluid | 70.66 Bbl | SURFACE IMPOUNDMENT | 826342 |
2019 | SWN PROD CO LLC | Other Oil & Gas Wastes | 11.00 Bbl | SURFACE IMPOUNDMENT | 826342 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2081987 | Primary Facility | 2012-05-22 | Drilling/Alteration | No Violations Noted | 20 set at 40' |
2089196 | Primary Facility | 2012-08-02 | Incident- Response to Accident or Event | Violation(s) Noted | Arrived at the site at 10:20 AM in response to a release of flowback fluid that was discovered at 10:05 on 8/1/12. Jason Petlock of SWN reported the release to the Department on 8-1-12. The initial report indicated the amount of flowback fluid released was determined to be (100-5,000) gallons. The report indicates that while SWN was in a preparation to frac a well at the site, blended water (treated flowback and freshwater from the Greenzweig large impoundment transported to the site via underground lines) overflowed the working tanks and secondary containment. The fluid exited the Well Pad and traveled under the Pad berm. SWM reported conductivity readings of (2,500) microSiemens/cm in a seep at the toe of the fill slope. A sump has been constructed in this area with a pump located on a liner to recover the fluid. During the inspection on 8-2-12, SWN indicated to the Department they have determined the out of containment and off the Well Pad release to be between 90-100 bbls (barrels) also equivalent to (4,000 to 4,200 gallons). |
2100606 | Primary Facility | 2012-09-11 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | I used an Extech, ExStik (2) pH, Conductivity, Salinty and TDS meter to field screen areas of ponded water both on and off the Well Pad. Conductivity readings recorded on the meter indicated less than (200) microSiemens/cm on the secondary containment liner near the frac tank storing fluid from Sump#1 at the bottom of the fill slope. Conductivity readings inside the lined pit for sump# 1 indicated a range between (1,000-1,200) microSiemens/cm. In areas of ponded and slow moving water outside this sump conductivity readings revealed levels in between (800-900) microSiemens/cm. Water was observed seeping from the ground in several areas at the toe of the fill slope. The water flows into Sump#1 and is periodically pumped through a line up the embankment into a frac tank located on secondary containment on the Well Pad. Sump #2 indicated conductivity readings between (1,100-1,200) microSiemens/cm. This was inside the sump pit, which is located at the edge of the wooded area. |
2180789 | Primary Facility | 2013-07-01 | Routine/Complete Inspection | No Violations Noted | |
2337369 | Primary Facility | 2015-01-20 | Incident- Response to Accident or Event | No Violations Noted | |
2343513 | Primary Facility | 2015-02-11 | Routine/Complete Inspection | No Violations Noted | Arrived onsite @ 12:25, sunny, temperature > freezing, pad snow-covered. There were 6 wells in production on the pad. The Ferguson-Keisling GU #1, Heckman-Hiduk GU #1, and Heckman-Camp GU #1 were in one row. The cellars on these wells were open. There were 3 digital Scada gauges on annuli for each of these well. The lowermost labeled, “Surface”, measured the pressure in the 9-5/8” x 5-1/2” casing. Higher on the wellhead, the “Casing” gauge measured the 5-1/2 x 2-3/8” annular pressure. The gauge on the top of the well head measured the tubing pressure, according to production superintendent Gary Dutton. The production units for these wells were near the western corner of the pad. The other three wells were also in a line but offset from the previous 3: Greenzweig 7H, Greenzweig 8H, and Heckman-Hiduk #2. |
2677985 | Primary Facility | 2017-12-05 | Routine/Complete Inspection | No Violations Noted | On December 5, 2017, the Department conducted a routine inspection at the SWN Production Company LLC, GU-G-Pad in Herrick Township, Bradford County. The Department was represented by Andrew Hobbins. Tracy Gregory was present for SWN.
The site sign, E & S plan and weekly inspection logs were on site and available for review. The site was well vegetated, and no E & S issues were observed during the inspection. The well pad has been reduced in size. A Notice of Termination was approved by the Department in November of 2015. Six wells were in production during the inspection. The wells were labeled and no bubbling was observed in the well cellars. Two production tanks and six GPUs were also on site. Puddles on the pad were low in specific conductivity and no staining was observed on the well pad surface. No violations were observed during this inspection. |
2817053 | Primary Facility | 2018-12-18 | Site Restoration | No Violations Noted | The DEP conducted a RESTORATION inspection of SWN's Heckman Camp G pad in Herrick Twp, Bradford County on 12/18/2018 at 1230 hours. The inspection was conducted in response to a Well Site Restoration Report received by the DEP.
This site has 6 producing wells onsite with two production tanks. The site is very well vegetated and steep slopes of the pad appear stabilized. All PCSM BMPs appeared to be in place and no temporary E&S BMPs were observed. This Well Site Restoration Report is accepted. No violations noted today, I departed the site at 1255. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2089196 | 645802 | 08/02/2012 | 2012-08-02 | 307CSL - Discharge of industrial waste to waters of Commonwealth without a permit. | Environmental Health & Safety | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
2089196 | 645803 | 08/02/2012 | 2012-08-02 | 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances. | Administrative | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
2089196 | 645804 | 08/02/2012 | 2012-08-02 | SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. | Environmental Health & Safety | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
2089196 | 645861 | 08/02/2012 | 2012-08-02 | 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | Environmental Health & Safety | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
2089196 | 645862 | 08/02/2012 | 2012-08-02 | 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt | Environmental Health & Safety | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
2089196 | 645863 | 08/02/2012 | 2012-08-02 | 401 CSL - Discharge of pollultional material to waters of Commonwealth. | Environmental Health & Safety | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
2089196 | 645864 | 08/02/2012 | 2012-08-02 | 91.34A - Failure to take all necessary measures to prevent spill. Inadequate diking, potential pollution | Environmental Health & Safety | NCRO EC&B case closure 8/3/13, MBC data clean-up 5/8/15, closed. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
645802 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 | |||
645803 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 | |||
645804 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 | |||
645861 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 | |||
645862 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 | |||
645863 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 | |||
645864 | 286936 | NOV - Notice of Violation | Administrative Close Out | 2013-08-03 |
For data sources see[8]