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37-023-20044

Well Details

Well ID: 37-023-20044
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Country: United States
State: Pennsylvania
County: Cameron
Municipality: Portage Township
Operator Name:
Well Pad ID:
Farm/Lease Name: EMPORIUM WATER CO
License Status: PLUGGED & ABANDONED
Spud Date: 1972-09-17
Permit Date: 1972-07-21
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.551222
Longitude: -78.165909

For data sources see[1][2][3]

Well History

Date Event
1972-07-21 New Permit Application
1972-09-17 Performed Spud Operation
1972-10-19 Drilling Completion
1972-10-19 Perforation
1972-10-19 Performed Stimulation
1973-08-02 Perforation
1973-08-02 Performed Stage 1 of Stimulation
1973-08-02 Performed Stage 2 of Stimulation
1973-08-02 Performed Stage 3 of Stimulation
1973-08-02 Performed Stage 4 of Stimulation
1974-01-01 NEWLY DRILLED
1974-01-01 PARTIALLY PLUGGED
2019-07-18 Begin Plugging
2019-08-29 Finished Plugging
2020-01-13 Fully Plugged

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1973-08-02 1 sand 0 0 0
1973-08-02 2 sand 0 0 0
1973-08-02 3 sand 0 0 0
1973-08-02 4 sand 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1999 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2000 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2004 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2005 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2006 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2007 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2008 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2009 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2010 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2011 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2012 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2013 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2014 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2015 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2016 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2017 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2018 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2760858 Primary Facility 2018-07-31 Routine/Complete Inspection No Violations Noted At the time of this inspection this well was not in production. This well was drilled in September of 1972(drilling started 9-17-72 as indicated on the well record). The well record indicates no date as to when drilling was completed but does indicate well completion as 8-4-73. This well had 13 3/8" casing(39') installed on 9-18-72, 9 5/8" casing(835') installed on 9-22-72, 7" production casing(6,470') installed on 10-5-72 and 4 1/2" production pipe(2,153') installed on 7-30-73. This well was never put into production or connected to a production sales line. At the time of this inspection this well was observed to be bubbling out of one side of the approximate 5"x2"x2" tee style wellhead assembly fitting. Combustible gas was detected with a Altair 5x multi- gas meter at this inspection. The operator,Dominion Energy Trans Inc. Will sample the gas to determine the source and origin of gas detected and then propose a plan of action to correct the bubbling observed at this inspection. Future inspection(s) of thi
903596 Primary Facility 1999-12-15 Plugging(Includes Plugged/Mined Through) No Violations Noted

For data sources see[7]

References