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Well ID: 37-033-20173 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Pennsylvania | |
County: Clearfield | |
Municipality: Huston Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: | |
Farm/Lease Name: STATE TRACT 66 N677 | |
License Status: ACTIVE | |
Spud Date: 1958-10-03 | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.231483 | |
Longitude: -78.595955 |
Date | Event |
---|---|
1958-10-03 | Performed Spud Operation |
1958-11-24 | Drilling Completion |
1959-01-01 | Fully Plugged |
2017-05-19 | Begin Plugging |
2017-06-23 | Finished Plugging |
For data sources see[4]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
Sand | 0 | 0 | 3,750 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1980 | NEW YORK NATURAL GAS CORP | 3,717.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1981 | NEW YORK NATURAL GAS CORP | 5,750.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1982 | NEW YORK NATURAL GAS CORP | 4,405.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1983 | NEW YORK NATURAL GAS CORP | 4,537.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1984 | NEW YORK NATURAL GAS CORP | 4,721.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1985 | NEW YORK NATURAL GAS CORP | 538.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1992 | DOMINION ENERGY TRANS INC | 1252.00 | ? | 0.00 | 0 | 0.00 | 0 |
1994 | DOMINION ENERGY TRANS INC | 1147.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | DOMINION ENERGY TRANS INC | 1097 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | AMER EXPLORATION CO | 1263 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | AMER EXPLORATION CO | 1259 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | AMER EXPLORATION CO | 2098 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | AMER EXPLORATION CO | 1,159.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | DOMINION ENERGY TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | AMER EXPLORATION CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | DOMINION ENERGY TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | DOMINION ENERGY TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | DOMINION ENERGY TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | EQT PROD CO | 443.00 | 184 | 0.00 | 0 | 0.00 | 0 |
2011 | EQT PROD CO | 1,379.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | EQT PROD CO | 900.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | EQT PROD CO | 677.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | EQT PROD CO | 750.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | EQT PROD CO | 862.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | EQT PROD CO | 291.00 | 183 | 0.00 | 0 | 0.00 | 0 |
2017 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
1998 | AMER EXPLORATION CO | Brine | 33.70 Bbl | Other | PA0101508 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2599378 | Primary Facility | 2017-05-31 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s State Tract 66 N677 well in Huston Twp. conducted May 31, 2017 at 10:30 am. Hydrocarbon Well Service is rigged up for plugging ops. Well is dead, the crew is tripping in hole with 2 3/8” hole tubing to attainable bottom. They are at 3800’ at time of inspection. No major issues observed. |
2599934 | Primary Facility | 2017-06-01 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s State Tract 66 N677 well in Huston Twp. conducted June 1, 2017 12 pm. Hydrocarbon Well Services are rigged up for plugging ops. Yesterday they tagged obstruction in 7” 6302’ (tools reportedly were lost in hole prior to P&A). Plan is to set CIBP in 7” at attainable bottom, run CBL on 7” and continue procedure. Checked the backside of the 7”, ~150 PSI. |
2601349 | Primary Facility | 2017-06-06 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s State Tract 66 N677 well in Huston Twp. conducted June 6, 2017 approximately 10 am . Hydrocarbon Well Services are rigged up for plugging ops. CIBP has been set in the 7” at 6275’ and 7” was logged. At the time of inspection, the rig was digging around well in preparation to rig up casing jacks to pull 7”. Casing appears to be recoverable at ~5500’ based on log interpretation but crew may need to move up hole if needed to successfully pull 7”. Well is dead and there was no pressure on the backside of 7” noted at time of inspection. No obvious issues were noted. |
2604420 | Primary Facility | 2017-06-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s State Tract 66 N677 well in Huston Twp. conducted June 13, 2017 approximately 10 am. Hydrocarbon Well Services are rigged up for plugging ops. CIBP is set in 7”, cellar dug out to rig up casing jacks, rig is running back in hole w/tubing. Backside of 7” was open and lined out to tank, no flow observed. Well is static. No issues. |
2606987 | Primary Facility | 2017-06-22 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s State Tract 66 N677 well in Huston Twp. conducted June 22, 2017 approximately 11 am. Hydrocarbon Well Services are rigged up for plugging ops. I spoke with the driller. Yesterday they squeezed the 7” and set a 300’ cement plug across where the cut was made in attempt to pull 7” at 5520’. Regarding the squeeze effort, they closed the backside of their 2 3/8” workstring, began pumping and put ~400 PSI on it, then the pressure dropped with a vent of gas to returns and were able to squeeze 2 bbls of cement this way, opened the backside of tubing and displaced balanced plug. They tagged TOC 10’ above calculated indicating no fallback. They will do the same procedure across the 2nd cut in 7” @2748’ and again (100’) below the surface casing shoe (1360’). That will be a 150’ plug after perf’ing 7” (1470’-1460’) and squeezing backside (no more than 4 bbls calc.). Displace balanced plug inside 7”, WOC, Tag plug, bail hole dry and put a vent on it. No issues. |
2609955 | Primary Facility | 2017-06-30 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s State Tract 66 N677 well in Huston Twp. conducted June 30, 2017 approximately 1:40 pm. The rig is off location following plugging ops. The crew erected a ~20’ vent pipe monument with marker to identify the well. No gas was detected in, at, or around the vent. No Violations. |
For data sources see[8]