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Well ID: 37-033-27018 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Clearfield | |
Municipality: Karthaus Township | |
Operator Name: BKV OPR LLC | |
Well Pad ID: 145302 | |
Farm/Lease Name: RHP-A | |
License Status: Inactive | |
Spud Date: | |
Permit Date: 2011-04-19 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.141006 | |
Longitude: -78.097322 |
Date | Event |
---|---|
2011-04-19 | New Permit Application |
2011-10-18 | Performed Spud Operation |
2011-12-30 | Drilling Completion |
2012-11-06 | DEVIATED |
2019-04-22 | Inactive Well Request Granted |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2011 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2019 | BKV OPR LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 1,556.38 Tons | LANDFILL | 101397 |
2012 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 1,988.00 Tons | LANDFILL | 101397 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2023550 | Primary Facility | 2011-11-28 | Routine/Complete Inspection | No Violations Noted | |
2044962 | Primary Facility | 2012-02-24 | Routine/Complete Inspection | No Violations Noted | |
2053307 | Primary Facility | 2012-03-22 | Routine/Complete Inspection | No Violations Noted | |
2116208 | Primary Facility | 2012-11-16 | Routine/Complete Inspection | No Violations Noted | |
2240996 | Primary Facility | 2014-01-30 | Routine/Complete Inspection | No Violations Noted | |
2528441 | Primary Facility | 2016-10-17 | Site Restoration | No Violations Noted | |
2597819 | Primary Facility | 2017-05-25 | Routine/Complete Inspection | No Violations Noted | Routine inspection of the River Hill Power Marcellus well pad. Site is occupied by a single completed well, (RHP #1H 37-033-27018) which has been completed and flowed back, but has never been placed in an active production status. The Ceritas Midstream Partners-Karthaus West gathering pipeline originally planned to serve the site was cleared and grubbed, but was never built, and the pipeline ROW has been fully restored and pipeline ESCGP terminated, and the well remains shut in, in a regulatory inactive status.
The original ESCGP for this site was modified to upgrade the existing sediment traps into infiltration basins, and the post-construction pad footprint was approved at the original full buildout size. The location is built entirely on reclaimed bituminous mine spoils, and while ponded water may be present on the pad itself after a rain event, runoff off the aggregate pad quickly infiltrates into the surrounding vegetated spoil material. Site ID signage is posted at the access road entran |
2724297 | Primary Facility | 2018-04-27 | Routine/Complete Inspection | No Violations Noted | Department representative Sue Herzing conducted a routine site inspection at BKV Operating, LLC River Hill Power Pad on April 27, 2018 with environmental consultant Kevin Brady. There is one Marcellus well (033-27018) drilled on this pad. The well has been drilled and stimulated. This well is currently in regulatory inactive status and this status will expire on 4/22/19. The well head is tagged. Water was observed in the well cellar.
The well pad remains the original footprint size. All PCSMs are in place. The ESCGP (ESX11-033-0006) for the construction of the well pad and access road was terminated by Department staff on 10/25/16. In addition, a well site restoration report for this well was approved on 10/17/16 by Department staff. No production equipment is onsite. The pad and access road appear stable. No E&S issues were observed. No violations noted. |
2751194 | Primary Facility | 2018-07-03 | Routine/Complete Inspection | No Violations Noted | The weather is 70 Deg. F and sunny at time of inspection. Follow up inspection of BKV Operating, LLC., RHP-A Pad, well 5H on July 3, 2018.
There is 1 inactive and shut in well on this pad. Annulus vent (9-5/8" x 5-1/2") is open and vented at time of inspection. 0% combustible gas was detected at the annulus. Production casing pressure is 0 PSI, production tubing pressure is 0 PSI, backside casing pressure is 4950 PSI, annulus intermediate by production pressure is 0 PSI. All production equipment has been removed from the wellsite. No violations are noted at time of inspection. BKV Operating, LLC Representatives - Kevin J. Brady and Jesse Bonnice, Sr. Production Foreman. DEP Representative - Ulyana Trynovich, Oil and Gas Inspector. |
2845276 | Primary Facility | 2019-02-26 | Follow-up Inspection | No Violations Noted | The weather is 32 Deg. F and sunny at time of inspection. Follow up inspection of BKV Operating, LLC., RHP-A Pad, well 5H on Feb. 26, 2019.
There is 1 inactive and shut in well on this pad. Inactive Well Status expires on April 22, 2019. Annulus vent (9-5/8" x 5-1/2") is open and vented at time of inspection. 0% combustible gas was detected at the annulus. Production casing pressure is 0 PSI, production tubing pressure is 0 PSI, backside casing pressure is 4900 PSI, annulus intermediate by production pressure is 0 PSI. All production equipment has been removed from the wellsite. No violations are noted at time of inspection. BKV Operating, LLC Representatives - Kevin J. Brady, Hydrologist, Environmental Scientist, Wetland Delineator (WPIT) Whitetail Environmental Services, LLC; Matt Merculdo, Contractor Manager. DEP Representative - Ulyana Trynovich, Oil and Gas Inspector. |
For data sources see[7]