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Well ID: 37-037-20001 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Columbia | |
Municipality: Sugarloaf Township | |
Operator Name: XPR RESOURCES LLC | |
Well Pad ID: 147019 | |
Farm/Lease Name: M MARTIN 1H | |
License Status: PLUGGED & ABANDONED | |
Spud Date: | |
Permit Date: 2009-07-22 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: Yes | |
Latitude: 41.236861 | |
Longitude: -76.366367 |
Date | Event |
---|---|
2009-07-22 | New Permit Application |
2010-07-07 | Permit Renewal Application |
2010-08-31 | Performed Spud Operation |
2011-02-04 | New Permit Application |
2011-04-05 | Drilling Completion |
2011-06-15 | Perforation |
2011-09-07 | DEVIATED |
2015-05-18 | Drilling Completion |
2015-07-01 | FULLY PLUGGED |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2011-06-16 | 2011-06-16 | 6,763 | 4,070,106 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Sand- Silica Sand | Halliburton Energy Services | Proppant | Quartz | 14808-60-7 | 100.00 | 13.79 | |
BE-9M | Halliburton Energy Services | Biocide | Methanol | 67-56-1 | 30.00 | 0.00320000 | ||
Tri-n-butyl tetradecyl phosphonium chloride | 81741-28-8 | 10.00 | 0.00107000 | |||||
GBW-30 Breaker | Halliburton Energy Services | Breaker | Hemicellulase enzyme | 9012-54-8 | 15.00 | 0.00005000 | ||
Carbohydrates | 95.00 | 0.00033000 | ||||||
Water | Carrier/Base Fluid | Water | 100.00 | 86.04 | ||||
Hydrochloric Acid | Halliburton Energy Services | Acid | Hydrochloric acid | 7647-01-0 | 30.00 | 0.10 | ||
Cla-Web | Halliburton Energy Services | Clay Control | ||||||
0.02 | ||||||||
Proprietary | 60.00 | |||||||
SP Breaker | Halliburton Energy Services | Breaker | Sodium persulfate | 7775-27-1 | 100.00 | 0.00035000 | ||
LP-65 | Halliburton Energy Services | Scale Inhibitor | Ammonium chloride | 12125-02-9 | 10.00 | 0.00407000 | ||
FR-66 Friction Reducer | Halliburton Energy Services | Friction Reducer | Distillates, petroleum, hydrotreated light | 64742-47-8 | 30.00 | 0.01 | ||
WG-36 Gelling Agent | Halliburton Energy Services | Gel | Guar gum | 9000-30-0 | 100.00 | 0.00145000 | ||
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | XPR RESOURCES LLC | Drilling Fluid Waste | 12,857.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0008451 |
2010 | XPR RESOURCES LLC | Drilling Fluid Waste | 143.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 301353 |
2011 | XPR RESOURCES LLC | Drilling Fluid Waste | 2,612.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0008451 |
2011 | XPR RESOURCES LLC | Fracing Fluid Waste | 54,025.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC006 |
2011 | XPR RESOURCES LLC | Drilling Fluid Waste | 2,512.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC006 |
2012 | XPR RESOURCES LLC | Fracing Fluid Waste | 350.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC006 |
2012 | XPR RESOURCES LLC | Drilling Fluid Waste | 70.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC006 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1842705 | Primary Facility | 2009-11-06 | Routine/Complete Inspection | No Violations Noted | |
1850555 | Primary Facility | 2009-12-16 | Compliance Evaluation | No Violations Noted | |
1851078 | Primary Facility | 2009-12-03 | Routine/Complete Inspection | No Violations Noted | |
1919154 | Primary Facility | 2010-10-04 | Drilling/Alteration | No Violations Noted | 37 ft 20" conductor-- ran 440 ft 13 3/8 casing 20 bbl cement return to surface-- ran 1525 ft 9 5/8 casing 10 bbl cement return to surface |
1920110 | Primary Facility | 2010-09-13 | Drilling/Alteration | No Violations Noted | rig @ 3411 ft deep. set 37 ft 20" conductor cemented with 21 yards concrete. ran 440 ft 13 3/8 casing cemented to surface with 20 bbl cement return to surface. ran 1525 ft 9 5/8 casing cemented to surface with 10 bbl cement returned to surface. |
1947219 | Primary Facility | 2011-02-03 | Drilling/Alteration | No Violations Noted | |
1956771 | Primary Facility | 2011-03-10 | Drilling/Alteration | No Violations Noted | |
1958074 | Primary Facility | 2011-03-17 | Drilling/Alteration | No Violations Noted | |
1964248 | Primary Facility | 2011-04-06 | Routine/Partial Inspection | Violation(s) Noted | |
1966839 | Primary Facility | 2011-04-19 | Routine/Complete Inspection | No Violations Noted | |
1981581 | Primary Facility | 2011-06-16 | Follow-up Inspection | No Violations Noted | |
2003899 | Primary Facility | 2011-09-20 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
2012677 | Primary Facility | 2011-10-19 | Drilling/Alteration | Outstanding Violations - No Viols Req'd | |
2021307 | Primary Facility | 2011-11-22 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
2072440 | Primary Facility | 2012-05-30 | Routine/Complete Inspection | No Violations Noted | |
2089838 | Primary Facility | 2012-08-08 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
2154684 | Primary Facility | 2013-04-08 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
2303236 | Primary Facility | 2014-08-26 | Routine/Complete Inspection | No Violations Noted | |
2347788 | Primary Facility | 2015-02-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This inspection occurred prior to the mobilization of plugging equipment. Arrived @16:40 on 2/18/15. Containment has been laid down on the pad and there are two Baker tanks on site. Tubing pressure was ~ 1550 psi as measured by a 10,000 psi water-filled gauge. The cellar was frozen, ice and snow were directly adjacent to the well. There were no other annular vents visible at the time of my inspection. Left location @ 17:00. |
2347797 | Primary Facility | 2015-02-24 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | : This inspection took place during plug and abandon operations. Arrived on site @12:30. On location were WPX petroleum engineer Kent Knapschaefer and landman Jeff Volinas, Jason Nicholas with Nick’s Well Plugging. The service rig was up when I arrived. When I arrived the well head was frozen. Once thawed out, the well blew down quickly. Fresh water was pumped down the tubing and annulus to kill the well. 90 bbl were pumped with 10 bbl circulated out to the flowback tank. Left location @17:00. |
2347805 | Primary Facility | 2015-02-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Plugging operations continue. Arrived @ 12:30, sunny, warmer than previous frigid temps. Onsite were: WPX pet. engineer Kent Knapschaefer, Jason Nicholas and crew with Nick’s Well Plugging, Team Services rig crew, and Baker Hughes wireline services led by Cliff Smarr. BOPs were installed and 2-3/8” tubing was pulled before I arrived. Wireline services were preparing to gauge the 5-1/2” production casing when I arrived. Cast Iron Bridge Plug (CIBP) set at 5809’ in the 5-1/2” casing, as per the plugging procedure. Left location at 16:00 |
2347858 | Primary Facility | 2015-02-26 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Plugging operations continued. Arrived @11:30 cloudy, warmer. Operations were delayed due to difficulties freeing the production casing from the slips. Casing jacks were brought onsite and needed 310,000 lbf to free the casing. At the time the Baker Hughes crew noted that there was very little casing stretch visible at the surface. The plan was then to run a free point tool to find the casing free point (anticipated to be below 4000’ based on a previous CBL). The free point tool was checked at numerous depths but the casing free point was not observed. A radial cement bond log on the 5-1/2” casing was run. I left the location at 16:00. Results of the CBL available later indicated a cement top at 3490’ with some cement at 1760’ to 1810’. Even this log was not consistent with the failure to obtain tension on the pipe. It was decided that we would monitor for methane the next day and modify the plugging procedure accordingly. |
2347883 | Primary Facility | 2015-02-27 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Plugging operations continued. Arrived @08:00 with DEP OGI Bruce Jankura, sunny, very cold. Onsite were WPX’s Kent, Team Services’s Stacy, Baker Hughes’ Cliff, and Nick’s Well Plugging’s Jason with their attendant crews. Using the Altair 5, we monitored for gas in the surface to intermediate casing annulus and the production casing. Since there was no gas detected we agreed to the following: set a 200’ cement plug (5800’ to 5600’) using 15.6 ppg, Class A cement, 1.18 ft3/sk. Pump a gel spacer from 5600’ – 1800’ (~84 bbls). Pump a cement plug from ~ 1800’ to surface. The plan was to do this in three stages: 1800’ to 800’, 800’ to 200’ and 200’ to surface. Discussed requirements monument requirements with Kent. Left location at ~11:00. |
2351873 | Primary Facility | 2015-03-10 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Time 1600. weather: rain, cloudy, and warm. On- site to verify report of bubbling at the recently plugged gas well. Bubbles (diameter ~ 1”) were emerging intermittently from near the center of the water-filled depression around the well. There appeared to be ~6 bubbles in close succession and then a gap. I confined some of the gas and used the MSA 60 meter to verify that this was combustible gas. I used the Altair 5 and found no methane, carbon monoxide, or hydrogen sulfide at the vent. Informed WPX Petroleum Engineer Kent Knapschaefer of these findings and requested updates on WPX’s plans. I aslso requested a local contact. There are no violations at this time. |
2352825 | Primary Facility | 2015-03-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Time 11:50, windy with sun. Met with Williams’ staff Bob Goodwin and Kent Knapscheafer to investigate source of bubbling at the recently plugged well. The water had been removed from the cellar which was approximately 4’ deep with a muddy floor. The conductor was exposed and there was solid cement emerging from the conductor. The cement obscured the casing tops. The steel plate centered about the center of the well also obscured the top of the well. It was not possible to ID the bubble source.Williams plans to have the steel plate removed and then try the soap solution again, or perhaps enough water to just cover the cement. Once the source has been identified the short-term plan is to leave water in the cellar so that the situation can be monitored pending further investigation and a long-term plan. Left at 12:30. There are no violations at this time. |
2361125 | Primary Facility | 2015-04-07 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Arrived at 11:40, cloudy, warm, intermittent rain. At the time of my inspection subcontractors from ROC and United Rentals had already excavated around the cellar. Ground water was infiltrating the excavation. A pump arrived shortly after I did. Subcontractors pumped out the water, made a cut down the length of the cellar, scrapped away the lip of cement at the cellar’s base, and peeled the cellar off with a track hoe. When I left the location at 14:20, contractors were waiting on a jack hammer attachment to remove the cement and cut the cement and annuli. The next day, 4/8/15, I received a report containing photos and video from Kent Knapschaefer (WPX petroleum engineer) showing bubbling on the 9-5/8” x 5-1/2” annulus. The contractors installed a new cap and vent. WPX installed a pressure gauge and shut the vent in to build pressure and obtain a sample for stable isotopic analysis. |
2367506 | Primary Facility | 2015-04-29 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Arrived at 13:00. Met company man Matt Wilson. Drilling rig was onsite, Wilson was making preparations for staring on 4/30/15. Operations near the well head made precluded a measurement of combustible gas at the 9-5/8” x 5-1/2”. But Wilson had observed 45 psi on the gauge following shut in. This pressure blew down in seconds, he said. Discussed the replug prog. The plan, to the first decision point, was to weld casing head onto the 9-5/8” casing, spear the 5-1/2” bring it up and in slips, install BOPs and start to drill out the cement plug down to ~ 1750’, then try to cut and pull casing. Wilson said it was unwise to estimate how long it would take to drill out the plug. Left at 14:00 |
2368548 | Primary Facility | 2015-05-11 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Stopped at location to discuss plugging activity. Site quiet. Also investigated complaint related to equipment on containment. Containment was in place at the time of my inspection and equipment was on containment. Conducted a thorough inspection of the site. Did not observe any discoloration or other indications of leaks or spills. The location was appropriately protected at the time of my inspection. |
2370915 | Primary Facility | 2015-05-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Arrived @7:30. Company man Jon Short has replaced Matt Wilson on site. Rig on location, quiet at the time of my inspection, following success in cutting window and placing rock-to-rock plug as per the 5/13/15 revised prog: |
2454749 | Primary Facility | 2016-02-22 | Routine/Complete Inspection | No Violations Noted | |
2619611 | Primary Facility | 2017-07-07 | Site Restoration | No Violations Noted | On July 7, 2017, the Department conducted a site restoration inspection at the WPX Energy Appalachia, LLC (WPX) Martin 1V Well Pad in Sugarloaf Township, Columbia County. Andrew Hobbins, Water Quality Specialist represented the Department. Nobody was present for WPX. The Department received a Notice of Termination (NOT) from WPX on June 27, 2017.
The well pad has not been completely restored, but has been reduced in size. PCSM has not been addressed at the site. The restored area has been returned to approximate original contours. Vegetation was observed to be greater than 70%. The well that was on site was plugged in 2015. Section 3216(d) of the Oil and Gas Act states "Within nine months after plugging a well, the owner or operator shall remove all production or storage facilities, supplies and equipment and restore the well site." The Department recommends restoring the remain pad surface to approximate original contours. Chapter 78a.65(3) also states "Within 60 days after the restoration of t |
2620345 | Primary Facility | 2017-07-07 | Site Restoration | No Violations Noted | On July 7, 2017, the Department conducted a site restoration inspection at the WPX Energy Appalachia, LLC (WPX) Martin 1V Well Pad in Sugarloaf Township, Columbia County. Andrew Hobbins, Water Quality Specialist represented the Department. Nobody was present for WPX. The Department received a Notice of Termination (NOT) from WPX on June 27, 2017.
The well pad has not been completely restored, but has been reduced in size. PCSM has not been addressed at the site. The restored area has been returned to approximate original contours. Vegetation was observed to be greater than 70%. The well that was on site was plugged in 2015. Section 3216(d) of the Oil and Gas Act states "Within nine months after plugging a well, the owner or operator shall remove all production or storage facilities, supplies and equipment and restore the well site." The Department recommends restoring the remain pad surface to approximate original contours. Chapter 78a.65(3) also states "Within 60 days after the restoration of t |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1964248 | 608356 | 04/06/2011 | 2011-04-06 | 201G - Failure to post permit number, operator name, address, telephone number in a conspicuous manner at the site during drilling | Administrative |
For data sources see[8]