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Well ID: 37-039-22409 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Crawford | |
Municipality: Wayne Township | |
Operator Name: RANGE RESOURCES APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: L LEGNOSKY 1 | |
License Status: Plugged and Abandoned | |
Spud Date: 1985-05-05 | |
Permit Date: 1985-05-08 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 41.554386 | |
Longitude: -79.945836 |
Date | Event |
---|---|
1985-05-08 | New Permit Application |
1985-05-15 | Drilling Completion |
1986-04-28 | NEWLY DRILLED |
2018-09-04 | Begin Plugging |
2018-09-20 | Finished Plugging |
2018-10-04 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1986 | MARK RESOURCES CORP | 14,807.00 | 271 | 0.00 | 0 | 0.00 | 0 |
1987 | MARK RESOURCES CORP | 10,823.00 | 226 | 0.00 | 0 | 0.00 | 0 |
1988 | MARK RESOURCES CORP | 19,101.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1989 | MARK RESOURCES CORP | 10,814.00 | 363 | 0.00 | 0 | 0.00 | 0 |
1990 | MARK RESOURCES CORP | 10236.00 | 341 | 0.00 | 0 | 0.00 | 0 |
1991 | MARK RESOURCES CORP | 8821.00 | 312 | 0.00 | 0 | 0.00 | 0 |
1992 | MARK RESOURCES CORP | 9233.00 | 355 | 0.00 | 0 | 0.00 | 0 |
1993 | RANGE OPR CO | 9036.00 | 360 | 0.00 | 0 | 0.00 | 0 |
1994 | RANGE OPR CO | 7126.00 | 341 | 0.00 | 0 | 0.00 | 0 |
1995 | RANGE OPR CO | 5946.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | RANGE OPR CO | 7333 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | RANGE OPR CO | 6409 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | RANGE OPR CO | 6423 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | RANGE OPR CO | 4359 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | RANGE RESOURCES APPALACHIA LLC | 4609 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | RANGE RESOURCES APPALACHIA LLC | 4021 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | RANGE RESOURCES APPALACHIA LLC | 3523 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | RANGE RESOURCES APPALACHIA LLC | 2973.23 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | RANGE RESOURCES APPALACHIA LLC | 2705.56 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | RANGE RESOURCES APPALACHIA LLC | 2701.36 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | RANGE RESOURCES APPALACHIA LLC | 2678.12 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | RANGE RESOURCES APPALACHIA LLC | 2432 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | RANGE RESOURCES APPALACHIA LLC | 2357.75 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | RANGE RESOURCES APPALACHIA LLC | 2295.45 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | RANGE RESOURCES APPALACHIA LLC | 1,755.59 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | RANGE RESOURCES APPALACHIA LLC | 1,385.97 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | RANGE RESOURCES APPALACHIA LLC | 398.89 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | RANGE RESOURCES APPALACHIA LLC | 304.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | RANGE RESOURCES APPALACHIA LLC | 1,251.86 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | RANGE RESOURCES APPALACHIA LLC | 638.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
1997 | RANGE OPR CO | Brine | 70.00 Bbl | Road Spreading | OIL CREEK TWP. |
1999 | RANGE OPR CO | Brine | 75.00 Bbl | Injection Disposal Well | 2585201 |
2004 | RANGE RESOURCES APPALACHIA LLC | Brine | 75.00 Bbl | Road Spreading | |
2006 | RANGE RESOURCES APPALACHIA LLC | Brine | 75.00 Bbl | Road Spreading | |
2008 | RANGE RESOURCES APPALACHIA LLC | Brine | 30.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2012 | RANGE RESOURCES APPALACHIA LLC | Produced Fluid | 35.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2018 | RANGE RESOURCES APPALACHIA LLC | Produced Fluid | 300.00 Bbl | Injection Disposal Well | 34-007-21847 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2468855 | Primary Facility | 2016-03-29 | Routine/Partial Inspection | No Violations Noted | |
2772021 | Primary Facility | 2018-09-07 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspected location, rig and supporting plugging equipment have been setup, crew is getting ready to rig up hot water to pump down on 1 1/2 inch tubing to try to flush out a salt bridge at 3000 feet. |
2773145 | Primary Facility | 2018-09-11 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspected location, rig crew was pulling out tubing at time of inspection, they flushed out salt bridge, wireline will be on location 9/12/18 to cut casing and begin cementing operations. |
2774431 | Primary Facility | 2018-09-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspected location, cement crew was pumping bottom plug with 130 sacks of cement, after cement crew pumped cement and flushed lines crew then rigged down to start pulling work string and pipe became stuck in hole, rig crew worked the string for approx 45 minutes and was not able to get work string free, after consulting with company official they are going to let the pipe sit over night then come in with wireline run a bond log then shoot the work string at top of cement then set top plug. |
2775021 | Primary Facility | 2018-09-14 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspected location, when arrived wireline crew was setting up to run bond log, could not get down below 3100', wireline then pulled out and put cutter on and ran down too 3060' and then cut casing then pulled out of hole and rigged down, rig crew then made sure that the pipe was free by pulling up on joint, cement crew then broke circulation and then spotted 100' stub plug, rig crew then pulled up hole and finished setting remaining plugs. |
357489 | Primary Facility | 1988-04-11 | Routine/Complete Inspection | No Violations Noted | |
357490 | Primary Facility | 1989-05-09 | Routine/Complete Inspection | No Violations Noted | |
357491 | Primary Facility | 1989-06-29 | Routine/Complete Inspection | No Violations Noted | |
357492 | Primary Facility | 1989-07-31 | Routine/Complete Inspection | No Violations Noted |
For data sources see[7]