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Well ID: 37-039-25624 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Crawford | |
Municipality: Woodcock Township | |
Operator Name: BOBCAT WELL & PIPELINE LLC | |
Well Pad ID: | |
Farm/Lease Name: CAMPBELL 13 | |
License Status: | |
Spud Date: | |
Permit Date: 2008-12-09 | |
Well Type: COMB. OIL&GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 41.692056 | |
Longitude: -80.147180 |
Date | Event |
---|---|
2008-12-09 | New Permit Application |
2009-02-24 | Performed Spud Operation |
2009-03-01 | Drilling Completion |
2009-03-12 | Perforation |
2009-04-14 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | D & L ENERGY INC | 1,961.10 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | D & L ENERGY INC | 3,487.30 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | D & L ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | D & L ENERGY INC | 933.6 | 365 | 0.01 | 365 | 0.00 | 0 |
2015 | BOBCAT WELL & PIPELINE LLC | 345.83 | 240 | 0.00 | 0 | 0.00 | 0 |
2016 | BOBCAT WELL & PIPELINE LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | BOBCAT WELL & PIPELINE LLC | 0.00 | 0 | 20.68 | 1 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | D & L ENERGY INC | Produced Fluid | 74.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 34-007-22038 |
2011 | D & L ENERGY INC | Produced Fluid | 62.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 34-099-23127 |
2012 | D & L ENERGY INC | Produced Fluid | 58.00 Bbl | INJECTION DISPOSAL WELL | 34-007-20919 |
2013 | D & L ENERGY INC | Produced Fluid | 9.00 Bbl | ROAD SPREADING | |
2017 | BOBCAT WELL & PIPELINE LLC | Produced Fluid | 50.00 Bbl | ROAD SPREADING |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1771775 | Primary Facility | 2009-02-25 | Drilling/Alteration | No Violations Noted | |
1773293 | Primary Facility | 2009-03-03 | Drilling/Alteration | No Violations Noted | |
1910541 | Primary Facility | 2010-09-02 | Routine/Complete Inspection | No Violations Noted | |
1913389 | Primary Facility | 2010-09-16 | Routine/Complete Inspection | No Violations Noted | |
1976783 | Primary Facility | 2011-05-31 | Complaint Inspection | No Violations Noted | Today's inspection was the result of a complaint re: the overflow of the steel stock tank inside the dike at this production site. Upon inspection I meet the complainant in-site, and found a producing well and the following production equipment. One steel stock tank at 99% capacity/ one poly tank nearly empty and valved off, one separator and an active production chart. The steel tank had apparently overflowed, with a small amount of oily substance flowing onto the limestone base inside the dike. The area impacted by the oil was approx. 2'x4'. The tank had some oil on it also. I contacted the comapany and asked them to remove the contaminated soil/stone and clean the tank. I also ask them to call me when the work is completed. I told the complainant I would let him know when the work was done. |
1981292 | Primary Facility | 2011-06-17 | Follow-up Inspection | No Violations Noted | Follow-up inspection to complaint recived 5/31/11 and inspection dated 5/31/11 to setermine if the required work was completed. Upon inxpection i found all oil on the tank and the ground had been cleaned up. I contacted the complaintant and told them complaince was met. No violations. |
2175685 | Primary Facility | 2013-06-12 | Routine/Partial Inspection | No Violations Noted | |
2546688 | Primary Facility | 2016-12-22 | Administrative/File Review | No Violations Noted | production report review |
For data sources see[7]