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37-047-00710

Well Details

Well ID: 37-047-00710
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Country: United States
State: Pennsylvania
County: Elk
Municipality: Millstone Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: GODFREY PARRETT 4712
License Status: Plugged and Abandoned
Spud Date: 1947-03-31
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.387577
Longitude: -78.999514

For data sources see[1][2][3]

Well History

Date Event
1947-06-03 Drilling Completion
2017-08-23 Begin Plugging
2017-11-16 Finished Plugging
2017-11-28 Old Well

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
SHOT 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 NATL FUEL GAS SUPPLY CORP 549.00 120 0.00 0 0.00 0
1992 NATL FUEL GAS SUPPLY CORP 0.00 0 0.00 0 0.00 0
1993 NATL FUEL GAS SUPPLY CORP 783.00 160 2.28 160 0.00 0
1994 NATL FUEL GAS SUPPLY CORP 1324.00 365 0.00 0 0.00 0
1995 SENECA RESOURCES CO LLC 798.00 365 0.00 0 0.00 0
1996 SENECA RESOURCES CO LLC 747 365 0.00 0 0.00 0
1997 SENECA RESOURCES CO LLC 399 364 0.00 0 0.00 0
1998 SENECA RESOURCES CO LLC 92 365 0.00 0 0.00 0
1999 SENECA RESOURCES CO LLC 84 365 0.00 0 0.00 0
2000 SENECA RESOURCES CO LLC 84 365 0.00 0 0.00 0
2001 SENECA RESOURCES CO LLC 84 365 0.00 0 0.00 0
2002 SENECA RESOURCES CO LLC 84 365 0.00 0 0.00 0
2003 SENECA RESOURCES CO LLC 124 365 0.00 0 0.00 0
2004 SENECA RESOURCES CO LLC 125 365 0.00 0 0.00 0
2006 SENECA RESOURCES CO LLC 119.00 365 0.00 0 0.00 0
2007 SENECA RESOURCES CO LLC 119.00 365 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 124.00 365 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 123.00 365 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2629166 Primary Facility 2017-08-25 Plugging(Includes Plugged/Mined Through) No Violations Noted No one here on my arrival. Rig setting at well and all equipment on site to plug this well.
2632010 Primary Facility 2017-09-05 Plugging(Includes Plugged/Mined Through) No Violations Noted Plugging this well. Currently at 100' fishing for 4" pipe that separated at 83'.
2638002 Primary Facility 2017-09-20 Plugging(Includes Plugged/Mined Through) No Violations Noted They are currently at 200' deep fishing rotted 4" out of the well. They are using a lined pit to contain all fluids and cuttings.
2640506 Primary Facility 2017-09-27 Plugging(Includes Plugged/Mined Through) No Violations Noted They made it to 1130' but the tools keep getting hung up on the 4" pipe they ran when pulling out of the well at 200'. They are continuing to try to get to TD. They have a lined pit for cutting and fluids that is empty at this time.
2651793 Primary Facility 2017-10-25 Plugging(Includes Plugged/Mined Through) No Violations Noted They were at 1805' and broke their drilling line off and lost the tools in the hole with 800' of drill line. Due to the condition of the production pipe being rotten they could not fish line and tools out. Decision was made to cement the well at 1745', cementing the tools in the well with 110 sacks (605')I approved the attainable bottom for this well. The top of the 41/2 pipe is at 200' where it parted. They plan to shoot production pipe off at around 1000' and then set the casing seat plug.

For data sources see[7]

References