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37-049-24685

Well Details

Well ID: 37-049-24685
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Country: United States
State: Pennsylvania
County: Erie
Municipality: Amity Township
Operator Name:
Well Pad ID:
Farm/Lease Name: ROSE 1
License Status:
Spud Date:
Permit Date: 1985-12-10
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.970966
Longitude: -79.785789

For data sources see[1][2][3]

Well History

Date Event
1985-12-10 New Permit Application
1985-12-17 Performed Spud Operation
1985-12-21 Drilling Completion
1986-01-02 Perforation
1986-01-03 Performed Stimulation
1986-07-12 NEWLY DRILLED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1986-01-03 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2012 MITCH WELL ENERGY INC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1838244 Primary Facility 2009-09-17 Routine/Complete Inspection No Violations Noted
1963875 Primary Facility 2011-04-04 Routine/Complete Inspection Violation(s) Noted Inspection of the well revealed the production equipment and wellhead have been removed. The only remaining equipment is a short section of pipeline protruding up about 6ft out of the ground beside the 15" well casing ; this casing has a flat steel plate covering the casing opening. The plate is laying on the casing, not fastened. the landowner indicated he was told the well was plugged. DEP has not received a plugging certificate.
2064871 Primary Facility 2012-05-02 Follow-up Inspection Outstanding Violations - No Viols Req'd
2118597 Primary Facility 2012-11-20 Follow-up Inspection Outstanding Violations - No Viols Req'd
2162556 Primary Facility 2013-04-29 Follow-up Inspection Outstanding Violations - No Viols Req'd
363055 Primary Facility 1988-05-27 Plugging(Includes Plugged/Mined Through) No Violations Noted PLUGGED
363056 Primary Facility 1988-11-15 Routine/Complete Inspection No Violations Noted DID NOT LOCATE

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1963875 608283 04/04/2011 2011-04-04 210UNPLUG - Failure to plug a well upon abandonment Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
608283 269756 NOV - Notice of Violation Superseded 2013-01-29
608283 292029 ADORD - Administrative Order Superseded 2013-01-29
608283 294448 ADORD - Administrative Order

For data sources see[7]

References