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37-049-24806

Well Details

Well ID: 37-049-24806
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Country: United States
State: Pennsylvania
County: Erie
Municipality: Venango Township
Operator Name: STEDMAN ENERGY INC
Well Pad ID:
Farm/Lease Name: FRED DEAN 1
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date: 1986-11-20
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 42.019440
Longitude: -79.820602

For data sources see[1][2][3]

Well History

Date Event
1986-11-20 New Permit Application
1987-01-05 Performed Spud Operation
1987-01-14 Drilling Completion
1987-01-30 Perforation
1987-03-27 Performed Stimulation
1987-10-21 NEWLY DRILLED
2006-08-02 Drilling Completion
2007-03-14 FULLY PLUGGED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1987-03-27 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
1996 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
1997 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
1998 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
1999 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
2000 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
2001 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
2002 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
2004 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
2005 VINEYARD OIL & GAS CO 0.00 0 0.00 0 0.00 0
2006 STEDMAN ENERGY INC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1991 VINEYARD OIL & GAS CO Brine 70.00 Bbl

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1554153 Primary Facility 2006-07-01 Plugging(Includes Plugged/Mined Through) No Violations Noted Had previously been unable to pull 4 1/2. Hooked on this morning circulated and it popped off at 619 feet. Casing seat plug set.
373367 Primary Facility 1993-02-25 Routine/Complete Inspection No Violations Noted
386458 Primary Facility 1998-12-15 Routine/Complete Inspection No Violations Noted

For data sources see[8]

References