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Well ID: 37-059-01532 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Greene | |
Municipality: Wayne Township | |
Operator Name: CONTURA PENNSYLVANIA LAND LLC | |
Well Pad ID: | |
Farm/Lease Name: T.L.J. GARRISON | |
License Status: Plugged and Abandoned | |
Spud Date: 1903-11-20 | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 39.798961 | |
Longitude: -80.226803 |
Date | Event |
---|---|
1904-01-25 | Drilling Completion |
1905-01-01 | OLD WELL |
2019-08-20 | Begin Plugging |
2019-11-19 | Finished Plugging |
2020-01-13 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1994 | ZAMA PETRO INC | 3238.42 | 365 | 0.00 | 0 | 0.00 | 0 |
1995 | ZAMA PETRO INC | 3126.42 | 334 | 0.00 | 0 | 0.00 | 0 |
1996 | ZAMA PETRO INC | 3182.42 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | ZAMA PETRO INC | 3654.67 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | ZAMA PETRO INC | 3800.83 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | ZAMA PETRO INC | 2945.83 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | ZAMA PETRO INC | 2627.25 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | ZAMA PETRO INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2005 | ZAMA PETRO INC | 2067.83 | 334 | 0.00 | 0 | 0.00 | 0 |
2006 | ZAMA PETRO INC | 1998.58 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | ZAMA PETRO INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | ZAMA PETRO INC | 2,411.27 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | ZAMA PETRO INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | ZAMA PETRO INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | ZAMA PETRO INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | PA LAND HOLDINGS COMPANY LLC | 100.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | PA LAND HOLDINGS COMPANY LLC | 100.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | PA LAND HOLDINGS COMPANY LLC | 100.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | PA LAND HOLDINGS COMPANY LLC | 100.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | PA LAND HOLDINGS COMPANY LLC | 100.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | PA LAND HOLDINGS COMPANY LLC | 100.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CONTURA PENNSYLVANIA LAND LLC | 100.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2646002 | Primary Facility | 2016-06-20 | Complaint Inspection | No Violations Noted | The Department conducted an inspection of the T.L.J Garrison 1 gas well on 6/20/16 in response to a complaint. The Department determined that a valve on an unused section of sales line was damaged while bailing hay allowing gas to escape from the unused portion of the sales line. The valve is located approximately 100 west of the gas wellhead. The well was not damaged. The well was shut in after gas was heard escaping from the damaged valve. The Department did not observe any gas leaking from the sales line or the T.L.J Garrison 1 gas well at the time of inspection. The Department contacted the well operator pertaining to the damaged sales valve. The operator responded to the well location to make repairs to the damaged valve/sales line and restore gas service to the complainant’s residence. The Department also requested that the operator verify the operation of emergency phone number posted on the T.L.J Garrison wellhead. |
For data sources see[6]