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37-059-01574

Well Details

Well ID: 37-059-01574
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Country: United States
State: Pennsylvania
County: Greene
Municipality: Richhill Township
Operator Name: LEATHERWOOD INC
Well Pad ID:
Farm/Lease Name: MASON SCOTT 1
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 39.870692
Longitude: -80.395608

For data sources see[1][2][3]

Well History

Date Event
1898-11-04 Drilling Completion
1901-01-01 Old Well
2016-06-15 Begin Plugging
2016-07-12 Finished Plugging

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 GREENRIDGE OIL CO INC 0.00 0 74.00 365 0.00 0
1997 MTN ENERGY 0.00 0 131 365 0.00 0
1998 MTN ENERGY 0.00 0 118 365 0.00 0
1999 MTN ENERGY 0.00 0 123 365 0.00 0
2001 MTN ENERGY 0.00 0 87 365 0.00 0
2002 MTN ENERGY 0.00 0 170 365 0.00 0
2003 MTN ENERGY 0.00 0 84 365 0.00 0
2004 MTN ENERGY 0.00 0 167 365 0.00 0
2008 MTN ENERGY 0.00 0 0.00 0 0.00 0
2009 LEATHERWOOD INC 0.00 0 60.00 117 0.00 0
2010 LEATHERWOOD INC 380.00 365 137.00 156 0.00 0
2011 LEATHERWOOD INC 548.00 356 90.00 156 0.00 0
2012 LEATHERWOOD INC 439.00 365 25.00 156 0.00 0
2013 LEATHERWOOD INC 199.00 365 80.00 156 0.00 0
2014 LEATHERWOOD INC 481.00 365 123.00 156 0.00 0
2015 LEATHERWOOD INC 78.00 365 48.00 84 0.00 0
2016 LEATHERWOOD INC 206.00 150 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2498164 Primary Facility 2016-06-24 Plugging(Includes Plugged/Mined Through) No Violations Noted Coastal Rig. Pulled 2,889’ of sucker rods. Pulled 2,910’ of 2” tubing. Pulled 2,248’ of 5 ½” casing and packer @ 2,248’. Bottom hole plug set from 2,910’ to 1,950’. Conduct site inspection.
536651 Primary Facility 1989-01-12 Routine/Complete Inspection No Violations Noted E&S OK; TANK

For data sources see[6]

References