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Well ID: 37-063-22887 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: East Mahoning Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: A F DEEMER 4953 | |
License Status: ACTIVE | |
Spud Date: 1975-03-05 | |
Permit Date: 1975-02-11 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.750366 | |
Longitude: -78.997440 |
Date | Event |
---|---|
1975-02-11 | New Permit Application |
1975-03-05 | Performed Spud Operation |
1975-03-10 | Drilling Completion |
1975-03-17 | Perforation |
1975-04-23 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | 3217.00 | 344 | 0.00 | 0 | 0.00 | 0 | |
1992 | 2420.00 | 370 | 0.00 | 0 | 0.00 | 0 | |
1993 | 2196.00 | 328 | 0.00 | 0 | 0.00 | 0 | |
1994 | 1736.00 | 230 | 0.00 | 0 | 0.00 | 0 | |
1995 | 671.00 | 241 | 0.00 | 0 | 0.00 | 0 | |
1996 | 671 | 365 | 0.00 | 0 | 0.00 | 0 | |
1998 | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 | |
1999 | CONSOL GAS CO | 1067 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | CONSOL GAS CO | 849 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | CONSOL GAS CO | 825 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | CONSOL GAS CO | 6164 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | CONSOL GAS CO | 5411 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | CONSOL GAS CO | 2927 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | CONSOL GAS CO | 2,557.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | CONSOL GAS CO | 2745.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | CONSOL GAS CO | 2393.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 2517.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 2,332.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 1,572.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 1,439.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 1,363.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 1,102.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 1,019.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 776.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 593.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 688.00 | 337 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2001 | CONSOL GAS CO | Brine | 625.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2002 | CONSOL GAS CO | Brine | 1,043.05 Bbl | Brine or Industrial Waste Treatment Plt | |
2002 | CONSOL GAS CO | Brine | 86.58 Bbl | Other | |
2003 | CONSOL GAS CO | Brine | 114.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2003 | CONSOL GAS CO | Brine | 192.00 Bbl | Injection Disposal Well | PAS2D912BSOM |
2003 | CONSOL GAS CO | Brine | 49.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2003 | CONSOL GAS CO | Brine | 396.00 Bbl | Other | |
2003 | CONSOL GAS CO | Brine | 159.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026034 |
2005 | CONSOL GAS CO | Brine | 200.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026034 |
2005 | CONSOL GAS CO | Brine | 350.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2005 | CONSOL GAS CO | Brine | 30.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2008 | CONSOL GAS CO | Brine | 300.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2008 | CONSOL GAS CO | Brine | 96.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026034 |
2008 | CONSOL GAS CO | Brine | 59.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009 | CONSOL GAS CO | Brine | 420.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2010 | CONSOL GAS CO | Produced Fluid | 175.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2010 | CONSOL GAS CO | Produced Fluid | 267.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2011 | CNX GAS CO LLC | Produced Fluid | 170.00 Bbl | Injection Disposal Well | 34-155-23584 |
2011 | CNX GAS CO LLC | Produced Fluid | 89.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2011 | CNX GAS CO LLC | Produced Fluid | 151.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 34-099-23127 |
2011 | CNX GAS CO LLC | Produced Fluid | 89.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2012 | CNX GAS CO LLC | Produced Fluid | 35.00 Bbl | Injection Disposal Well | 34-007-22038 |
2012 | CNX GAS CO LLC | Produced Fluid | 65.00 Bbl | Injection Disposal Well | 34-155-21447 |
2015 | CNX GAS CO LLC | Produced Fluid | 70 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2015 | CNX GAS CO LLC | Produced Fluid | 70.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2617225 | Primary Facility | 2017-07-20 | Routine/Complete Inspection | No Violations Noted | At time of inspection, well drilled and appears equipped for production. Pump jack installed on well. |
2715607 | Primary Facility | 2018-03-26 | Administrative/File Review | In Compliance with Policy | SPILL.
At 1020 on 3/26/18, operator representative Spencer Johnson reported a release of 30 gallons of brine water to the ground to SWRO representative Nicole Smith. The release reportedly occurred and/or was discovered on at 0930 on 3/26/18. No waterways are reported to be affected. |
2715628 | Primary Facility | 2018-03-26 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to release of 30 gallons brine water reported under inspection record 2715607.
Upon receipt of spill report, the Department contacted operator representative Spencer Johnson by phone. Per Mr. Johnson: The freeze/thaw cycle caused the valve to fail, resulting in a release of 30 gallons brine water to the ground. The release was discovered this morning at 0930 by the well-tender. The amount released was determined utilizing tank readings. This well is checked monthly. According to Mr. Johnson: There are no known nearby waterways. The release is confined to the area immediately by the brine tank. Visual clean-up will be performed in accordance with the Department's Spill Policy. Remediation is anticipated to commence today by a third-party contractor. Operator appears to be in compliance with current policy at this time. Violations may be forthcoming pending an on-site inspection to assess any environmental impact.
|
2715632 | Primary Facility | 2018-03-28 | Incident- Response to Accident or Event | Viol(s) Noted & Immediately Corrected | On-site inspection conducted in response to the reported release of 30 gallons brine water to the ground (inspection record 2715607).
At time of inspection, all visibly impacted soils appear to have been removed. Well drilled and appears equipped for production. Pump jack installed on well.
|
2742481 | Primary Facility | 2018-06-18 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued, noted as immediately corrected, under inspection record 2715632 for the reported release of 30 bbl brine water.
A written NOV response was requested. To date, it does not appear that this response was submitted and/or received by the Department. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2715632 | 813050 | 2018-03-28 | 2018-03-28 | 78.57(a) | Environmental Health & Safety | A violation is being issued for the reported release of 30 gallons brine water to the ground. This violation is being noted as immediately corrected as all visibly impacted soils appear to have been removed. |
2715632 | 813051 | 2018-03-28 | 2018-03-28 | 78.54 | Environmental Health & Safety | A violation is being issued for the reported release of 30 gallons brine water to the ground. This violation is being noted as immediately corrected as all visibly impacted soils appear to have been removed. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
813050 | 362950 | NOV - Notice of Violation | 2018-03-28 | ||||
813051 | 362950 | NOV - Notice of Violation | 2018-03-28 |
For data sources see[7]