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Well ID: 37-063-23582 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Cherryhill Township | |
Operator Name: PENN VIEW EXPLORATION CORP | |
Well Pad ID: | |
Farm/Lease Name: JAMES & FRANK CAMPBELL 6 | |
License Status: ACTIVE | |
Spud Date: 1976-12-22 | |
Permit Date: 1976-12-07 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.601134 | |
Longitude: -79.066968 |
Date | Event |
---|---|
1976-12-07 | New Permit Application |
1976-12-22 | Performed Spud Operation |
1976-12-31 | Drilling Completion |
1977-01-21 | Perforation |
1977-03-14 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | EAST RESOURCES INC | 658.00 | 86 | 0.00 | 0 | 0.00 | 0 |
1994 | EAST RESOURCES INC | 4082.83 | 365 | 0.00 | 0 | 0.00 | 0 |
1995 | EAST RESOURCES INC | 219.81 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | EAST RESOURCES INC | 22998 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | EAST RESOURCES INC | 1,721.78 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | EAST RESOURCES INC | 300.17 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | EAST RESOURCES INC | 2352.44 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | EAST RESOURCES INC | 2338.89 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | EAST RESOURCES INC | 1902 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | EAST RESOURCES INC | 2262 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | EAST RESOURCES INC | 2764.67 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | WIND RIVER EXPLORATION INC | 1,800.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | PENN VIEW EXPLORATION CORP | 1438.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | PENN VIEW EXPLORATION CORP | 1837.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | PENN VIEW EXPLORATION CORP | 1,658.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | PENN VIEW EXPLORATION CORP | 893.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2017 | PENN VIEW EXPLORATION CORP | 1,065.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | PENN VIEW EXPLORATION CORP | 1,123.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
1994 | EAST RESOURCES INC | Brine | 71.33 Bbl | ||
1995 | EAST RESOURCES INC | Brine | 24.11 Bbl | ||
1997 | EAST RESOURCES INC | Brine | 71.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2004 | WIND RIVER EXPLORATION INC | Brine | 130.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2588622 | Primary Facility | 2017-04-26 | Routine/Complete Inspection | Violation(s) Noted | At time of inspection, well drilled and appears equipped for production. Well tag present, legible.
While on-site at 1009, Department called Operator representative Brad Little and left a message in regards to the above-noted observations. Mr. Little returned the Department's phone call at 1108. Mr. Little stated that he talked to the well-tender and per the well-tender, the tank only contained freshwater and that the well-tender had previously observed a "wet" area on the brine tank. The well-tender also sprays weedkiller around the tanks. Mr. Little stated that he would visit the location and that the Department's concerns will be addressed. The Department is requesting the operator provide the following information: the last time the tank was emptied, tank readings from a year prior to this date through today's date, the last time the well-tender visited the site, and the last time maintenance has been performed on this tank and the reason(s) why. Based upon the Department's observations and soil condu |
2589641 | Primary Facility | 2017-05-01 | Administrative/File Review | Outstanding Violations - Viols Req'd | Admin inspection conducted in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
At 0811, Operator representative Brad Little notified the Department via voicemail that the contractor is on-site today to remove the brine tank and remediate the site. |
2589659 | Primary Facility | 2017-05-02 | Administrative/File Review | Outstanding Violations - Viols Req'd | Admin inspection conducted in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
At 0837, Department spoke to operator representative Brad Little via phone. Mr. Little stated that the tank had a crack in it and has since been removed. The quantity released is unknown at this time, but Mr. Little believes this amount is "very minimal". The operator intends to remediate this release in accordance with the Department's Spill Policy. |
2598009 | Primary Facility | 2017-05-15 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
At 0841, operator representative Brad Little notified the Department via voicemail that the contaminated soils at this site have been excavated and a report will be submitted to the Department. A follow-up inspection will be conducted at the site to further evaluate compliance. |
2598231 | Primary Facility | 2017-05-23 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Documentation in response to release submitted via e-mail by operator consultant. Violations remain outstanding at this time. |
2601329 | Primary Facility | 2017-05-26 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Department requested several clarifications by phone on documentation previously submitted in response to this release. Operator consultant is to provide revised documentation to the Department on the operator's behalf. |
2601331 | Primary Facility | 2017-05-26 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Documentation previously submitted in response to violations has been revised and re-submitted to the Department via e-mail. |
2601474 | Primary Facility | 2017-05-26 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Revised documentation in response to violations was previously re-submitted to the Department. Upon review, the Department requested additional clarifications from the operator via email, including an accurate quantity of fluids released. The Department's Spill Policy was also provided to the operator. |
2601599 | Primary Facility | 2017-06-07 | Follow-up Inspection | Outstanding Violations - Viols Req'd | On-site FUI in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
At time of inspection, former area of visible impact is exhibiting greater than 70% uniform and adequate vegetative growth. The brine tank has been removed from the location. Well tag present, legible. Violations previously issued for this reportable release remain outstanding as the Operator has not yet provided an accurate quantity of brine released in order for the Department to determine whether the Operator remediated this release in accordance with the Department's Spill Policy. |
2604551 | Primary Facility | 2017-05-30 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Documentation in response to release received by Department. Violations remain outstanding at this time. |
2604552 | Primary Facility | 2017-05-30 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Revised documentation in response to release received by Department. Violations remain outstanding at this time. |
2615695 | Primary Facility | 2017-07-05 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Revised documentation in response to violations was previously re-submitted to the Department. Upon review, the Department previously requested additional clarifications from the operator via email, including an accurate quantity of fluids released (inspection record 2601474). As no response as yet been received, the Department again requested additional clarifications from the operator via email, including an accurate quantity of fluids released. |
2620940 | Primary Facility | 2017-07-24 | Compliance Evaluation | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
E-mail submitted by operator consultant providing clarifications in response to release. An accurate quantity of brine released was also provided as previously requested by the Department; the quantity reported to be released is 40 gallons. Therefore, based on the reported quantity and the Department's follow-up on-site inspection (inspection record 2601599), it appears that this release was remediated in accordance with the Department's Spill Policy. Violations issued under inspection record 2588622 have been corrected. No new violations are being noted at this time. The Department is requesting that the disposal records/manifests are submitted to the attention of S. Foulk at the provided address upon disposal of the wastes excavated in response to this release. |
2622501 | Primary Facility | 2017-07-25 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Soil sample results and additional documentation provided by operator consultant via email. Violations were previously corrected under inspection record 2620940. |
2649071 | Primary Facility | 2017-10-06 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection record 2588622 (enf ID 352965) for failure to properly control and dispose of production fluids.
Voicemail received from operator consultant notifying Department that sampling for the removal of the wastes from the location is ongoing. Violations were previously corrected under inspection record 2620940. |
2752780 | Primary Facility | 2018-07-10 | Routine/Complete Inspection | No Violations Noted | Well appears equipped for production. It appears excavated soil from a release on 5-1-17 (inspection record #2588622) have been removed from site. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2588622 | 784492 | 2017-04-26 | 2017-07-24 | 78.54 | Environmental Health & Safety | Violations are being issued for a release of production fluids. |
2588622 | 784493 | 2017-04-26 | 2017-07-24 | 78.57(a) | Environmental Health & Safety | Violations are being issued for a release of production fluids. |
2589641 | 785160 | 2017-05-01 | 2017-07-24 | 78.54 | Environmental Health & Safety | Violations remain outstanding. |
2589641 | 785161 | 2017-05-01 | 2017-07-24 | 78.57(a) | Environmental Health & Safety | Violations remain outstanding. |
2589659 | 785162 | 2017-05-02 | 2017-07-24 | 78.54 | Environmental Health & Safety | Violations remain outstanding. |
2589659 | 785163 | 2017-05-02 | 2017-07-24 | 78.57(a) | Environmental Health & Safety | Violations remain outstanding. |
2601599 | 787581 | 2017-06-07 | 2017-07-24 | 78.54 | Environmental Health & Safety | This violation remains outstanding. |
2601599 | 787582 | 2017-06-07 | 2017-07-24 | 78.57(a) | Environmental Health & Safety | This violation remains outstanding. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
784492 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
784493 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
785160 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
785161 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
785162 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
785163 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
787581 | 352965 | NOV - Notice of Violation | 2019-01-28 | ||||
787582 | 352965 | NOV - Notice of Violation | 2019-01-28 |
For data sources see[7]