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Well ID: 37-063-25140 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Cherryhill Township | |
Operator Name: HHR HOLDINGS | |
Well Pad ID: | |
Farm/Lease Name: ANNA SHANK DICK 1 | |
License Status: ACTIVE | |
Spud Date: 1979-12-11 | |
Permit Date: 1979-11-20 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.622821 | |
Longitude: -79.084689 |
Date | Event |
---|---|
1979-11-20 | New Permit Application |
1979-12-11 | Performed Spud Operation |
1979-12-15 | Drilling Completion |
1980-01-04 | Perforation |
1980-02-04 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1994 | TOM A LEEPER | 500.00 | 210 | 0.00 | 0 | 0.00 | 0 |
1995 | TOM A LEEPER | 920.00 | 300 | 0.00 | 0 | 0.00 | 0 |
1996 | TOM A LEEPER | 1127 | 300 | 0.00 | 0 | 0.00 | 0 |
1997 | TOM A LEEPER | 250 | 300 | 0.00 | 0 | 0.00 | 0 |
1998 | TOM A LEEPER | 627 | 300 | 0.00 | 0 | 0.00 | 0 |
1999 | TOM A LEEPER | 520 | 300 | 0.00 | 0 | 0.00 | 0 |
2000 | TOM A LEEPER | 458 | 300 | 0.00 | 0 | 0.00 | 0 |
2001 | TOM A LEEPER | 328 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | TOM A LEEPER | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | TOM A LEEPER | 228 | 340 | 0.00 | 0 | 0.00 | 0 |
2004 | TOM A LEEPER | 497 | 300 | 0.00 | 0 | 0.00 | 0 |
2006 | TOM A LEEPER | 683.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | TOM A LEEPER | 443.00 | 220 | 0.00 | 0 | 0.00 | 0 |
2008 | TOM A LEEPER | 514.00 | 180 | 0.00 | 0 | 0.00 | 0 |
2009 | TOM A LEEPER | 309.00 | 100 | 0.00 | 0 | 0.00 | 0 |
2014 | TOM A LEEPER | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | TOM A LEEPER | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | TOM A LEEPER | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | TOM A LEEPER | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | HHR HOLDINGS | 100.00 | 365 | 0.01 | 365 | 0.01 | 365 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2006 | TOM A LEEPER | Brine | 0.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2018 | HHR HOLDINGS | Other Oil & Gas Wastes | 0.01 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC003 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2420506 | Primary Facility | 2015-10-30 | Complaint Inspection | Violation(s) Noted | At the time of inspection, well appears to be abandoned. Production equipment still remains at site in poor condition. Approximately 30 bbl. of brine water present in brine tank. Stress vegetation occurs around brine tank. No well tag was present at the well head. According to records, no production reports or mechanical integrity reports have been submitted to DEP. The well is producing gas to a residential home |
2437993 | Primary Facility | 2015-11-04 | Compliance Evaluation | No Violations Noted | at the time of inspection, no activity was completed. |
2440004 | Primary Facility | 2016-01-11 | Compliance Evaluation | No Violations Noted | At the time of inspection, production equipment was painted. Brine tank was at full capacity. A well tag was installed on the separator. Production reports and mechanical testing reports were submitted to PADEP. However, the production and MIA reports are still missing from the package submitted to the PADEP. At the time of the inspection, gas from the well is being supplied to the landowner’s resident dwelling. |
2480745 | Primary Facility | 2016-04-28 | Complaint Inspection | No Violations Noted | DEP representatives (Paul Wyrwas, Jason Brannon and Ed Ritzer) performed an inspection of the site. Complaint made relative to the well causing leakage of gas to surrounding area. A well tag was installed on the separator. DEP used the 62S meter (last calibrated on April 20th using three point system) and try to determine if any gas reading located around the well. DEP noted a small crack in the 8 inch reducer fitting. The crack in metal was approximately 1/2” in length. No readings from the meter were recorded surrounding the production equipment and site pad. A reportable reading of 40 percent gas was detected at the small crack. The well is currently running at 2 psi of pressure at the well head. DEP called Thomas Leeper and informed him of the crack in the well reducer fitting. DEP is also concern with the full capacity of the brine tank. Mr. Leeper agreed to repair the leak and remove the brine water from the tank |
2517705 | Primary Facility | 2016-08-29 | Routine/Complete Inspection | In Compliance with Policy | At time of inspection access road vegetated, no E&S issues observed. Well site vegetated. Department observed an area of standing water near the SW side of brine tank. Soil probe reading of 0.09 mS/cm appears to indicate that the fluid is not brine. Brine tank appears structurally sound and does not appear to be leaking. Brine tank does not appear to have been emptied since OGI inspection of 4-28-16 (inspection record #2480745).
Well label present and legible. Previous inspection by OGI sites a small crack in the well head casing. As of this inspection the crack has not been fixed and the well appears to be leaking. This inspection is PENDING. Violations may be issued after further investigation of OGI and WQS. UPDATE 10-3-16: After further investigation it appears that, at this time, there are no adverse affects observed at the well site due to the operation of this oil and gas well. However, Department recommends Operator continue to monitor and maintain brine tank to avoid any potential pollution events |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2420506 | 738049 | 10/30/2015 | 2015-10-30 | OGA 3213(C) - Failure to install, in a permanent manner, registration number on well 60 days after issuance. | Administrative | |
2420506 | 738050 | 10/30/2015 | 2015-10-30 | OGA 3222(A) - Failure to submit annual conventional well production report. | Administrative | |
2420506 | 738051 | 10/30/2015 | 2015-10-30 | 78.88(a) - OPERATING WELLS - MECHANICAL INTEGRITY OF OPERATING WELLS - Operator failed to inspect each operating well quarterly for compliance with the well construction and operating requirements. | Administrative | |
2420506 | 738052 | 10/30/2015 | 2015-10-30 | OGA 3220(A) - Failure to plug the well upon abandoning it. | Environmental Health & Safety |
For data sources see[7]