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37-063-27403

Well Details

Well ID: 37-063-27403
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Burrell Township
Operator Name: MARTIN LEON M
Well Pad ID:
Farm/Lease Name: CO OF INDIANA/PINE RIDGE PARK 1
License Status: ABANDONED
Spud Date:
Permit Date: 1983-01-04
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.439545
Longitude: -79.199097

For data sources see[1][2][3]

Well History

Date Event
1983-01-04 New Permit Application
1983-01-19 Performed Spud Operation
1983-02-02 Drilling Completion
1983-02-02 Perforation
1983-02-11 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2001 ATLAS RESOURCES INC 0.00 0 0.00 0 0.00 0
2002 ATLAS RESOURCES INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1113845 Primary Facility 2002-03-27 Routine/Complete Inspection No Violations Noted Meas line to 2375. Clean out cellar. No 3 inch. Collar locator to 4100. 7 icnh to 2875. 950" of 10 inch.
1127247 Primary Facility 2002-05-23 Routine/Complete Inspection No Violations Noted Plg to 1060 & shut-in.Still leaking. Checked w/pkr test. Appears to be leaking @plug. Wil ck again & possibly drl out plugs.
1160814 Primary Facility 2002-03-27 Routine/Complete Inspection No Violations Noted Measure line to 2375'.Mobed rig.Clean out cellar w/back hoe.No 3" found. Only 10" swedged to 3".Titan ran collar locator to 4100. 7 inch to 2875. Open to 950. 10" 950 to surf. Will begin drop Zonite.
1160815 Primary Facility 2002-05-13 Routine/Complete Inspection No Violations Noted Plug may be leaking. Will run packer to determine where leaking.
1160816 Primary Facility 2002-05-23 Routine/Complete Inspection No Violations Noted Now plugged back to 1060' & shut in. Still leaking. Checked w/Pkr test. Appears to be leaking @plug. will recheck & poss. drill out as per Cliff Simon of Key.
1160817 Primary Facility 2002-06-18 Routine/Complete Inspection No Violations Noted Key installed pkr @845" at top of plug.Gas pressure on both sides of pkr. Will recommend. drl out & plug solid with mechanical plug @ producing formations.
1160818 Primary Facility 2002-06-21 Routine/Complete Inspection No Violations Noted Checked press. @ 4" csg/pkr. Found 90 psi. Checked press. @8 5/8 csg/outside pkr. 0 psi.
1161334 Primary Facility 2002-08-09 Routine/Complete Inspection No Violations Noted Install 1475 ft. of 4 in. to drop Zonite through plugged off. Romove 4 in. plugged back from 1475 to 1200 ft w/Zonite. Well again showing gas pressure.
1161949 Primary Facility 2002-08-16 Routine/Complete Inspection No Violations Noted Replugfrom 1470 ft. to surf. Well no longer leaks.

For data sources see[6]

References