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| Well ID: 37-063-27403 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Indiana | |
| Municipality: Burrell Township | |
| Operator Name: MARTIN LEON M | |
| Well Pad ID: | |
| Farm/Lease Name: CO OF INDIANA/PINE RIDGE PARK 1 | |
| License Status: ABANDONED | |
| Spud Date: | |
| Permit Date: 1983-01-04 | |
| Well Type: GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: No | |
| Latitude: 40.439545 | |
| Longitude: -79.199097 |
| Date | Event |
|---|---|
| 1983-01-04 | New Permit Application |
| 1983-01-19 | Performed Spud Operation |
| 1983-02-02 | Drilling Completion |
| 1983-02-02 | Perforation |
| 1983-02-11 | NEWLY DRILLED |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 2001 | ATLAS RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2002 | ATLAS RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 1113845 | Primary Facility | 2002-03-27 | Routine/Complete Inspection | No Violations Noted | Meas line to 2375. Clean out cellar. No 3 inch. Collar locator to 4100. 7 icnh to 2875. 950" of 10 inch. |
| 1127247 | Primary Facility | 2002-05-23 | Routine/Complete Inspection | No Violations Noted | Plg to 1060 & shut-in.Still leaking. Checked w/pkr test. Appears to be leaking @plug. Wil ck again & possibly drl out plugs. |
| 1160814 | Primary Facility | 2002-03-27 | Routine/Complete Inspection | No Violations Noted | Measure line to 2375'.Mobed rig.Clean out cellar w/back hoe.No 3" found. Only 10" swedged to 3".Titan ran collar locator to 4100. 7 inch to 2875. Open to 950. 10" 950 to surf. Will begin drop Zonite. |
| 1160815 | Primary Facility | 2002-05-13 | Routine/Complete Inspection | No Violations Noted | Plug may be leaking. Will run packer to determine where leaking. |
| 1160816 | Primary Facility | 2002-05-23 | Routine/Complete Inspection | No Violations Noted | Now plugged back to 1060' & shut in. Still leaking. Checked w/Pkr test. Appears to be leaking @plug. will recheck & poss. drill out as per Cliff Simon of Key. |
| 1160817 | Primary Facility | 2002-06-18 | Routine/Complete Inspection | No Violations Noted | Key installed pkr @845" at top of plug.Gas pressure on both sides of pkr. Will recommend. drl out & plug solid with mechanical plug @ producing formations. |
| 1160818 | Primary Facility | 2002-06-21 | Routine/Complete Inspection | No Violations Noted | Checked press. @ 4" csg/pkr. Found 90 psi. Checked press. @8 5/8 csg/outside pkr. 0 psi. |
| 1161334 | Primary Facility | 2002-08-09 | Routine/Complete Inspection | No Violations Noted | Install 1475 ft. of 4 in. to drop Zonite through plugged off. Romove 4 in. plugged back from 1475 to 1200 ft w/Zonite. Well again showing gas pressure. |
| 1161949 | Primary Facility | 2002-08-16 | Routine/Complete Inspection | No Violations Noted | Replugfrom 1470 ft. to surf. Well no longer leaks. |
For data sources see[6]