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Well ID: 37-063-28509 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Canoe Township | |
Operator Name: R & R OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: VANCE C MCCORMICK 1 | |
License Status: ACTIVE | |
Spud Date: 1985-03-08 | |
Permit Date: 1984-12-28 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.887202 | |
Longitude: -78.961354 |
Date | Event |
---|---|
1984-12-28 | New Permit Application |
1985-03-08 | Performed Spud Operation |
1985-03-13 | Drilling Completion |
1985-03-21 | Perforation |
1985-10-18 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | EMAX OIL CO | 7619.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | EMAX OIL CO | 3241 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | EMAX OIL CO | 2702 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | EMAX OIL CO | 2459 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | EMAX OIL CO | 4,221.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | EMAX OIL CO | 5349.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | EMAX OIL CO | 1088.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | EMAX OIL CO | 2750.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | EMAX OIL CO | 217.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | EMAX OIL CO | 2,187.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | EMAX OIL CO | 2,139.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | EMAX OIL CO | 1,937.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | EMAX OIL CO | 1,994.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | EMAX OIL CO | 1,935.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | EMAX OIL CO | 1,763.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | R & R OIL & GAS LLC | 1,737.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2368760 | Primary Facility | 2015-04-30 | Administrative/File Review | Viol(s) Noted & Immediately Corrected | Admin inspection.Department notified on 4/29 via e-mail of spill by NWRO WQS Brian Shank. Spill was reported to B.Shank by Operator representative Rusty Kraft.At 0807 on 4/30, Department contacted Mr. Kraft via phone. Per Mr. Kraft, a disconnected brine tank was on the well site waiting to be hauled away for proper disposal. At 2030 on 4/28, a resident notified Mr. Kraft of crude oil spilling out from the top of the tank. Mr. Kraft estimates of release of ¼ bbl crude oil and stated that he immediately attempted to contact Mr. Shank via phone and text message to notify him of the release.Upon notification of the release, Mr. Kraft stated that he immediately placed barriers around the release to contain the fluids and placed absorbent pads on the impacted materials. A water truck emptied the tank that night. *ADD'L COMMENTS ON PAPER SAIR* |
2368837 | Primary Facility | 2015-05-01 | Incident- Response to Accident or Event | Violation(s) Noted | On-site inspt conducted in response to inspection record 2368760 for the release of ¼ bbl crude oil.At time of inspt, all visibly impacted materials appear removed.Area of excavation approx 25’x40’ in size and backfilled, seeded, mulched.No roll-off box on-site.BT remains on-site adjacent to AR.WT present, legible. Well head and associated equipment appears rusty.Drilling occurred 3/8/1985-3/13/1985.Faint gas odor noted.AR vegetated.Environ'l Trainee Cindy Witham present during inspt.A FUI will be conducted to ensure site is properly remediated and restored.Viols are being issued under 78.54 & 78.57(a) for this reportable release of residual fluids.Following this inspt, Dept contacted Opr rep R.Kraft via phone.Dept recommended Opr re-install E&S BMPs down-gradient of excavation and ensure any contaminants that remain on brine tank are prevented from reaching the ground in order to prevent any additional pollution events from occurring.Mr. Kraft agreed to immediately implement the Dept’s recommendations. |
2390785 | Primary Facility | 2015-07-15 | Compliance Evaluation | No Violations Noted | On-site CEI conducted in response to violations issued under inspection record 2368837 (enf ID 323093) for the 4/28/15 reported release of ¼ bbl crude oil to the ground. |
2392401 | Primary Facility | 2015-07-16 | Administrative/File Review | In Compliance with Policy | Admin insp conducted in response to viols issued under record 2368837 (enf ID 323093) for the 4/28 reported release of ¼ bbl crude oil.At 1414, Dept spoke to Opr rep J.Haskins via phone in response to the submittal of the disposal manifest for the fluids removed from the BT.Per the initial reporting of the incident, no brine was reported to have been in the brine tank; however, the invoice lists the fluids as “brine water” while the manifest reports “0% salt” in the fluids.Mr. Haskins infers that the use of “brine water” is standard on the invoices and that only freshwater was hauled.Mr. Haskins believes that someone put freshwater and/or freshwater with oil in their empty BT which resulted in the overflow. Mr. Haskins believes that the fluids emptied from the BT were “not produced fluids from their well”.The Dept inquired about status of disposal manifests for materials excavated from site during spill remediation efforts.Mr. Haskins believes records have just been received and will submit them to the Dept. |
783278 | Primary Facility | 1985-04-24 | Unspecified Inspection | Violation(s) Noted |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2368760 | 722342 | 04/28/2015 | 2015-04-28 | 78.66(a) - REPORTING RELEASES - Owner or operator failed to comply with the reporting and corrective action requirements of 25 Pa. Code Section 91.33 when a release of a substance caused or threatened pollution to the Waters of the Commonwealth. | Environmental Health & Safety | |
2368760 | 722343 | 04/28/2015 | 2015-04-28 | 91.33A - Failure to notify DEP of pollution incident. No phone call made forthwith | Administrative | |
2368837 | 722374 | 04/28/2015 | 2015-04-28 | 78.54 - GENERAL REQUIREMENTS - Operator failed to control and dispose of fluids, residual waste and drill cuttings, including tophole water, brines, drilling fluids, drilling muds, stimulation fluids, well servicing fluids, oil, and production fluids | Environmental Health & Safety | |
2368837 | 722375 | 04/28/2015 | 2015-04-28 | 78.57(a) - CONTROL, STORAGE AND DISPOSAL OF PRODUCTION FLUIDS - Operator failed to collect the brine and other fluids produced during operation, service and plugging of the well in a tank, pit or a series of pits or tanks, or other device approved by | Environmental Health & Safety | |
783278 | 86030 | 04/24/1985 | 1985-04-24 | 301307 - Unpermitted discharge of IW (brine, drill cuttings, & oil spills) | Environmental Health & Safety | DRILL FLUID DISCHARGE |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
722342 | 323085 | NOV - Notice of Violation | Comply/Closed | 2015-10-13 | |||
722343 | 323085 | NOV - Notice of Violation | Comply/Closed | 2015-10-13 | |||
722374 | 323093 | NOV - Notice of Violation | Comply/Closed | 2015-10-13 | |||
722375 | 323093 | NOV - Notice of Violation | Comply/Closed | 2015-10-13 | |||
86030 | 33526 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 1988-02-19 | $1,250.00 |
For data sources see[6]