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Well ID: 37-063-32130 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Burrell Township | |
Operator Name: FATE VENTURES LLC | |
Well Pad ID: | |
Farm/Lease Name: BONARRIGO 3 | |
License Status: ACTIVE | |
Spud Date: 1998-11-13 | |
Permit Date: 1998-08-20 | |
Well Type: COALBED METHANE | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.456389 | |
Longitude: -79.229873 |
Date | Event |
---|---|
1998-08-20 | New Permit Application |
1998-11-11 | Performed Spud Operation |
1998-11-16 | Drilling Completion |
1999-05-04 | Perforation |
1999-08-31 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1999 | BELDEN & BLAKE CORP | 3434 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | BELDEN & BLAKE CORP | 11612 | 366 | 0.00 | 0 | 0.00 | 0 |
2001 | BELDEN & BLAKE CORP | 10491 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | BELDEN & BLAKE CORP | 9206 | 365 | 0 | 0 | 0.00 | 0 |
2003 | BELDEN & BLAKE CORP | 7356 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | BELDEN & BLAKE CORP | 7180 | 366 | 0.00 | 0 | 0.00 | 0 |
2005 | BELDEN & BLAKE CORP | 6507 | 365 | 0 | 365 | 0.00 | 0 |
2006 | BELDEN & BLAKE CORP | 4,958.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | BELDEN & BLAKE CORP | 3,743.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | BELDEN & BLAKE CORP | 6,636.79 | 366 | 0.00 | 0 | 0.00 | 0 |
2009 | BELDEN & BLAKE CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | KEYROCK ENERGY LLC | 2,535.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | KEYROCK ENERGY LLC | 1,751.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | KEYROCK ENERGY LLC | 3,187.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | KEYROCK ENERGY LLC | 79.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | KEYROCK ENERGY LLC | 2,222.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | KEYROCK ENERGY LLC | 1,915.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | KEYROCK ENERGY LLC | 962.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | KEYROCK ENERGY LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2002 | BELDEN & BLAKE CORP | Brine | 7,812.00 Bbl | Treated On-Site, NPDES Discharge | |
2003 | BELDEN & BLAKE CORP | Brine | 8,184.00 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
2004 | BELDEN & BLAKE CORP | Brine | 6,436.86 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
2005 | BELDEN & BLAKE CORP | Brine | 7,810.00 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
2006 | BELDEN & BLAKE CORP | Brine | 8,451.00 Bbl | Treated On-Site, NPDES Discharge | PA0206075 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1823419 | Primary Facility | 2009-08-19 | Routine/Complete Inspection | No Violations Noted | Well drilled on 11/13/98 to depth of 1,204 ft. Well Record Report submitted to the DEP on 6/8/99. Well designed for Coal Bed Methane collection. Well head consisted of 4 ¿pipe reduced to 2¿ production. Dual data logger showed 15 psi/ 5 psi readings. Pump jack located at the well and was not running during the inspection. At the time of the inspection, no water discharged from top of pump jack well rod. Slight vegetation growth stress located hydraulically down gradient of the well head. No E&S issues at the site. |
2851448 | Primary Facility | 2019-03-11 | Administrative/File Review | No Violations Noted |
For data sources see[7]