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Well ID: 37-063-33248 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Armstrong Township | |
Operator Name: BLX INC | |
Well Pad ID: | |
Farm/Lease Name: ROBERTA B JONES 1 | |
License Status: ACTIVE | |
Spud Date: 2002-11-16 | |
Permit Date: 2002-11-05 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.620103 | |
Longitude: -79.336735 |
Date | Event |
---|---|
2002-11-05 | New Permit Application |
2002-11-16 | Performed Spud Operation |
2002-11-19 | Drilling Completion |
2002-11-26 | Perforation |
2003-04-17 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2003 | BLX INC | 14827.62 | 270 | 0.00 | 0 | 0.00 | 0 |
2005 | BLX INC | 12961.04 | 363 | 77.87 | 363 | 0.00 | 0 |
2006 | BLX INC | 10,064.00 | 342 | 0.00 | 0 | 0.00 | 0 |
2009 | BLX INC | 6855.00 | 268 | 0.00 | 0 | 0.00 | 0 |
2010 | BLX INC | 5,298.36 | 315 | 0.00 | 0 | 0.00 | 0 |
2011 | BLX INC | 5,088.74 | 345 | 0.00 | 0 | 0.00 | 0 |
2012 | BLX INC | 3,848.48 | 359 | 0.00 | 0 | 0.00 | 0 |
2013 | BLX INC | 3,474.86 | 337 | 20.47 | 337 | 0.00 | 0 |
2014 | BLX INC | 4,657.28 | 358 | 0.00 | 0 | 0.00 | 0 |
2015 | BLX INC | 4,113.34 | 337 | 0.00 | 0 | 0.00 | 0 |
2016 | BLX INC | 4,114.63 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | BLX INC | 3,360.21 | 360 | 0.00 | 0 | 0.00 | 0 |
2018 | BLX INC | 3,064.57 | 351 | 0.00 | 0 | 0.00 | 0 |
2019 | BLX INC | 2,128.59 | 356 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | BLX INC | Produced Fluid | 29.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095443 |
2014 | BLX INC | Produced Fluid | 17.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
2014 | BLX INC | Produced Fluid | 17 Bbl | CENT WASTE TRT FAC NPDES | PA0095443 |
2017 | BLX INC | Produced Fluid | 10.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2564345 | Primary Facility | 2017-02-15 | Routine/Complete Inspection | Violation(s) Noted | At time of inspection no E&S issues observed on access road. Site vegetated.
Well tag present and legible. Department observed fluid dripping from brine tank valve. Small patch (approx 15 inches X 15 inches) of stained gravel located under the valve. Department contacted Operator by phone from site to report findings and recommend well tender visit site. Operator stated well tender will be sent to site immediately. 12:00. Well tender Randy McCoy met Department at site. Mr. McCoy stated the valve appears to be broken. He also stated tank appears to be one-third full and was last emptied sometime last year. He visits this site once a week and was last on site 'a few days ago' and did not notice any leaking fluid at that time. Mr. McCoy stated he would excavate visibly impacted soils immediately and place a bucket under valve to catch dripping fluids until tank can be emptied and valve replaced. He will follow up with Department regarding further actions. 13:45. Mr. McCoy contacted Department by phone and s |
2565045 | Primary Facility | 2017-02-17 | Administrative/File Review | Outstanding Violations - Viols Req'd | Admin inspection to inspection record # 2564345 where violation issued for discharge of brine or other fluids on or into the ground or into waters of the Commonwealth.
Operator Rep Randy McCoy contacted Department by phone and left message. Mr. McCoy stated that the brine tank has been emptied and and the broken valve has been replaced. Mr. McCoy also stated that the amount of impacted soil was approximately half a 5 gal bucket. Department recommends Operator dispose of impacted soil by a method permitted by law. Previously issued violation still exists for this site. A follow up inspection will be conducted at a later date. |
2570205 | Primary Facility | 2017-03-09 | Administrative/File Review | Outstanding Violations - Viols Req'd | Admin inspection to inspection record # 2564345 where violation was issued for discharge of brine or other fluids on or into the ground or into waters of the Commonwealth.
Department received response to NOV from Operator. Operator states that freezing water damaged valve on brine tank. Operator also states that the impacted soil was removed on 2-15-17 and that the faulty valve was replaced on 2-16-17. Department recommends Operator dispose of impacted soil in a manner permitted by law. A follow up inspection will be conducted at a later date. Previously issued violation still exists for this site. |
2571456 | Primary Facility | 2017-03-13 | Compliance Evaluation | No Violations Noted | Compliance Evaluation Inspection to inspection record # 2564345 where a violation was issued for discharge of brine or other fluids on or into the ground or into waters of the Commonwealth.
At time of inspection it appears a new valve has been placed on the brine tank. The brine tank/valve appear structurally sound. Excavated area below valve has been rocked and appears pemanently stabilized. Previously issued violation (25 Pa. Code § 78.57(a)) for this site has been corrected. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2564345 | 779027 | 2017-02-15 | 2017-03-13 | 78.57(a) | Environmental Health & Safety | |
2565045 | 779223 | 2017-02-17 | 2017-03-13 | 78.57(a) | Environmental Health & Safety | |
2570205 | 780334 | 2017-03-09 | 2017-03-13 | 78.57(a) | Environmental Health & Safety | |
2570205 | 780335 | 2017-03-09 | 2017-03-13 | 78.57(a) | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
779027 | 351205 | NOV - Notice of Violation | 2017-03-27 | ||||
779223 | 351205 | NOV - Notice of Violation | 2017-03-27 | ||||
780334 | 351205 | NOV - Notice of Violation | 2017-03-27 | ||||
780335 | 351205 | NOV - Notice of Violation | 2017-03-27 |
For data sources see[7]