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Well ID: 37-063-33593 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: East Mahoning Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: LAURA ALLISON 21 | |
License Status: ACTIVE | |
Spud Date: 2004-05-25 | |
Permit Date: 2003-12-03 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.808370 | |
Longitude: -79.086862 |
Date | Event |
---|---|
2003-12-03 | New Permit Application |
2004-05-25 | Performed Spud Operation |
2004-06-02 | Drilling Completion |
2004-06-09 | Perforation |
2004-09-08 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2004 | PHILLIPS EXPLORATION INC | 10986 | 131 | 0.00 | 0 | 0.00 | 0 |
2005 | PHILLIPS EXPLORATION INC | 18142 | 352 | 0.00 | 0 | 0.00 | 0 |
2006 | PHILLIPS EXPLORATION INC | 12,570.00 | 364 | 0.00 | 0 | 0.00 | 0 |
2007 | PHILLIPS EXPLORATION INC | 7890.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | PHILLIPS EXPLORATION INC | 8485.00 | 360 | 0.00 | 0 | 0.00 | 0 |
2009 | PHILLIPS EXPLORATION INC | 6713.00 | 359 | 0.00 | 0 | 0.00 | 0 |
2010 | PHILLIPS EXPLORATION INC | 5,292.00 | 283 | 0.00 | 0 | 0.00 | 0 |
2011 | PHILLIPS EXPLORATION INC | 4,209.00 | 363 | 0.00 | 0 | 0.00 | 0 |
2012 | XTO ENERGY INC | 3,841.00 | 246 | 0.00 | 0 | 0.00 | 0 |
2013 | XTO ENERGY INC | 2,950.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | XTO ENERGY INC | 2,300.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | XTO ENERGY INC | 2,867.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | XTO ENERGY INC | 1,777.00 | 204 | 0.00 | 0 | 0.00 | 0 |
2017 | ALLIANCE PETRO CO LLC | 3,423.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2018 | ALLIANCE PETRO CO LLC | 2,344.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2004 | PHILLIPS EXPLORATION INC | Brine | 572.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2005 | PHILLIPS EXPLORATION INC | Brine | 890.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026310 |
2006 | PHILLIPS EXPLORATION INC | Brine | 505.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2008 | PHILLIPS EXPLORATION INC | Brine | 375.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 27.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026310 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 24.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095443 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 1.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0020346 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 31.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 1.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026034 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 9.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2010 | PHILLIPS EXPLORATION INC | Produced Fluid | 199.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 301353 |
2011 | PHILLIPS EXPLORATION INC | Produced Fluid | 38.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2011 | PHILLIPS EXPLORATION INC | Produced Fluid | 38.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 301353 |
2011 | PHILLIPS EXPLORATION INC | Produced Fluid | 37.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026310 |
2011 | PHILLIPS EXPLORATION INC | Produced Fluid | 37.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095443 |
2012 | XTO ENERGY INC | Produced Fluid | 97.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095443 |
2013 | XTO ENERGY INC | Produced Fluid | 205.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2013 | XTO ENERGY INC | Produced Fluid | 205 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2014 | XTO ENERGY INC | Produced Fluid | 172 Bbl | CENT WASTE TRT FAC NPDES | PA0095443 |
2014 | XTO ENERGY INC | Produced Fluid | 172.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
2015 | XTO ENERGY INC | Produced Fluid | 134.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2015 | XTO ENERGY INC | Produced Fluid | 47.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
2015 | XTO ENERGY INC | Produced Fluid | 47 Bbl | CENT WASTE TRT FAC NPDES | PA0095443 |
2015 | XTO ENERGY INC | Produced Fluid | 134 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2016 | XTO ENERGY INC | Soil Contaminated by Oil & Gas Related Spills | 54.01 Tons | RESIDUAL WASTE PROCESSING FACILITY | 101674 |
2016 | XTO ENERGY INC | Produced Fluid | 112 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2016 | XTO ENERGY INC | Produced Fluid | 112.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2016 | XTO ENERGY INC | Soil Contaminated by Oil | 54.01 Tons | RESIDUAL WASTE PROCESSING FACILITY | 101674 |
2017 | ALLIANCE PETRO CO LLC | Produced Fluid | 155.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2018 | ALLIANCE PETRO CO LLC | Produced Fluid | 165.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2019 | ALLIANCE PETRO CO LLC | Produced Fluid | 85.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028207 |
2019 | ALLIANCE PETRO CO LLC | Produced Fluid | 161.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1547179 | Primary Facility | 2006-06-22 | Complaint Inspection | No Violations Noted | PROD GS/TAG/TANK & E&S OK |
2507217 | Primary Facility | 2016-07-29 | Incident- Response to Accident or Event | Violation(s) Noted | |
2513398 | Primary Facility | 2016-08-25 | Compliance Evaluation | No Violations Noted | Requested follow-up documentation and 15-day response documentation received from the operator related to the spil reported on 07/28/16. The operator has elected to utilize the ACT 2 process for site remediation. This documentation was reviewed and the operator was found to be in compliance with the Department's Oil & Gas Program's Spill Policy. |
2530985 | Primary Facility | 2016-10-25 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to violations issued under inspection record 2507017 (enf ID 345824) for the 7/28/2016 reported release of 11.5 bbl brine. The violations were subsequently closed under inspection ID 2513398.
In accordance with the Spill Policy, the 15 day written response was received by the Department on 8/25/2016 notifying the Department that the Operator will be utilizing Act 2 for the remediation of this release (inspection ID 2513398). The Final Report was received by the ECB program on 10/21/2016. Operator appears to be in compliance with current policy at this time. |
2538665 | Primary Facility | 2016-11-22 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to violations issued under inspection record 2507017 (enf ID 345824) for the 7/28/2016 reported release of 11.5 bbl brine. The violations were subsequently closed under inspection ID 2513398.
In accordance with the Spill Policy, the 15 day written response was received by the Department on 8/25/2016 notifying the Department that the Operator will be utilizing Act 2 for the remediation of this release (inspection ID 2513398). The Final Report was received by the ECB program on 10/21/2016 and approved on 11/21/2016. Operator appears to be in compliance with current policy at this time. |
2553896 | Primary Facility | 2017-01-17 | Routine/Complete Inspection | No Violations Noted | On-site inspection conducted to monitor site remediation as a reportable release of brine previously occurred at this site. Violations were issued for this reportable release under inspection record 2507017 (enf ID 345824) and subsequently corrected under inspection record 2513398.
At time of inspection, what appears to have been the area of excavation is backfilled, seeded and mulched with minimal vegetative growth observed. Temporary BMPs installed down-gradient of this area and surrounded by fence. Well tag present, legible. Brine tank on-site, not connected to well. Access road appears to be shared. Site located within pasture. In accordance with the Spill Policy, the 15 day written response was received by the Department on 8/25/2016 notifying the Department that the Operator will be utilizing Act 2 for the remediation of this release (inspection ID 2513398). The Final Report was received by the ECB program on 10/21/2016 and approved on 11/21/2016. A follow-up inspection is anticipated to be conducted |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2507217 | 765186 | 2016-07-29 | 2016-08-25 | 78.54 | Environmental Health & Safety | Chapter 78.57(a) |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
765186 | 345824 | NOV - Notice of Violation | 2018-04-30 | ||||
765186 | 363720 | CPA - Civil Penalty Assessment | COMP - Completed | 2018-06-06 | 2018-06-06 | $70,000.00 | $70,000.00 |
For data sources see[7]