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Well ID: 37-063-35567 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Black Lick Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: JAMES E HILL 3 | |
License Status: ACTIVE | |
Spud Date: 2007-11-07 | |
Permit Date: 2007-08-13 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.495852 | |
Longitude: -79.255574 |
Date | Event |
---|---|
2007-08-13 | New Permit Application |
2007-11-07 | Performed Spud Operation |
2007-11-13 | Drilling Completion |
2007-11-19 | Perforation |
2008-01-15 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | PHILLIPS EXPLORATION INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | PHILLIPS EXPLORATION INC | 15048.00 | 254 | 0.00 | 0 | 0.00 | 0 |
2009 | PHILLIPS EXPLORATION INC | 17416.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | PHILLIPS EXPLORATION INC | 10,724.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | PHILLIPS EXPLORATION INC | 9,327.00 | 363 | 0.00 | 0 | 0.00 | 0 |
2012 | XTO ENERGY INC | 7,777.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | XTO ENERGY INC | 6,512.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | XTO ENERGY INC | 3,989.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | XTO ENERGY INC | 3,978.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | XTO ENERGY INC | 1,154.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | ALLIANCE PETRO CO LLC | 1,956.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2018 | ALLIANCE PETRO CO LLC | 2,556.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2012 | XTO ENERGY INC | Produced Fluid | 19.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2013 | XTO ENERGY INC | Produced Fluid | 43.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0020346 |
2013 | XTO ENERGY INC | Produced Fluid | 14 Bbl | CENT WASTE TRT FAC NPDES | PA0095443 |
2013 | XTO ENERGY INC | Produced Fluid | 14.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1843587 | Primary Facility | 2009-11-05 | Routine/Complete Inspection | Violation(s) Noted | PC (Phillips Exploration) had reported a brine release/fire (~500gals) on11-5-09 which occurred 11- 04-09 at approx. 9:00am at this site. At the time of inspection, the site had been secured, well was in production. The brine tank was replaced, as well as any production equipment that was destroyed by the fire. The release remnants were placed (contaminated soils/absorbent materials and brine tank) into a lined pit surrounded by a drainage ditch. All disturbed areas had been fertilized and reseeded. PC had plans to place the contaminants in a lined dumpster until permanent disposal could be conducted. the spill/fire was contained and restoration measures were taken,but violations will be issued for failure to report release in required timeframe, as well as discharge of brine. According to PC, the fire and release were caused by static electricity that produced a spark during dumping of the well separator which ignited the brine tank and well regulator causing an explosion/fire. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1843587 | 575832 | 11/05/2009 | 2009-11-05 | 91.33A - Failure to notify DEP of pollution incident. No phone call made forthwith | Administrative | |
1843587 | 575833 | 11/05/2009 | 2009-11-05 | 401 CSL - Discharge of pollultional material to waters of Commonwealth. | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
575832 | 252498 | NOV - Notice of Violation | Comply/Closed | 2009-12-03 | |||
575833 | 252498 | NOV - Notice of Violation | Comply/Closed | 2009-12-03 |
For data sources see[7]