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Well ID: 37-063-35598 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Cherryhill Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: 147237 | |
Farm/Lease Name: CARL BLOSE 1 | |
License Status: | |
Spud Date: 2008-08-21 | |
Permit Date: 2007-08-21 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 40.641055 | |
Longitude: -79.021905 |
Date | Event |
---|---|
2007-08-21 | New Permit Application |
2008-12-26 | Performed Spud Operation |
2009-01-23 | Drilling Completion |
2009-08-17 | Perforation |
2010-09-23 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2006 | POWER GAS MKT & TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | POWER GAS MKT & TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | POWER GAS MKT & TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | EXCO RESOURCES PA INC | 8687.00 | 100 | 0.00 | 0 | 0.00 | 0 |
2010 | EXCO RESOURCES PA INC | 19,109.00 | 323 | 0.00 | 0 | 0.00 | 0 |
2011 | EXCO RESOURCES PA INC | 4,797.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | EXCO RESOURCES PA LLC | 3,545.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | EXCO RESOURCES PA LLC | 2,633.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | EXCO RESOURCES PA LLC | 2,330.00 | 300 | 0.00 | 0 | 0.00 | 0 |
2015 | EXCO RESOURCES PA LLC | 2,641.00 | 356 | 0.00 | 0 | 0.00 | 0 |
2016 | ALLIANCE PETRO CO LLC | 2,890.00 | 355 | 0.00 | 0 | 0.00 | 0 |
2017 | ALLIANCE PETRO CO LLC | 2,876.30 | 357 | 0.00 | 0 | 0.00 | 0 |
2018 | ALLIANCE PETRO CO LLC | 1,841.00 | 363 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 2,130.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2009 | EXCO RESOURCES PA INC | Fracking Fluid | 100.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2010 | EXCO RESOURCES PA INC | Fracing Fluid Waste | 50.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2015 | EXCO RESOURCES PA LLC | Produced Fluid | 10.00 Bbl | INJECTION DISPOSAL WELL | PAS2D205BCLE |
2016 | ALLIANCE PETRO CO LLC | Produced Fluid | 16.00 Bbl | INJECTION DISPOSAL WELL | 2D0830792 |
2016 | ALLIANCE PETRO CO LLC | Produced Fluid | 16.00 Bbl | STORAGE PENDING DISPOSAL OR REUSE | |
2017 | ALLIANCE PETRO CO LLC | Produced Fluid | 17.00 Bbl | STORAGE PENDING DISPOSAL OR REUSE | |
2018 | ALLIANCE PETRO CO LLC | Waste comment only | 0.00 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1766340 | Primary Facility | 2008-12-31 | Drilling/Alteration | No Violations Noted | Dusting @ 1900' pit & E&S OK |
1794022 | Primary Facility | 2009-04-23 | Routine/Complete Inspection | No Violations Noted | id & e/s plan on site, drilling complete, rough graded, no open pits |
1794089 | Primary Facility | 2009-04-14 | Complaint Inspection | Violation(s) Noted | Drilling is complete. Crews are preparing to frac the well. There is evidence of a spill near the frac tanks. Oil went on the ground. The spill was approximately 50 gallons. Crews responded quickly and area was diked off before the oil could spread. It appears that all spillage was contained within the dike. The contaminated area was covered with absorptive material (Gator). Discussed options with operator representative Bryan Nelson and it was decided that the contaminated soil will be excavated and disposed of. |
1794107 | Primary Facility | 2009-04-22 | Compliance Evaluation | Outstanding Violations - No Viols Req'd | Performed a Field View as a follow-up to a previously issued Violation for an oil spill. |
1804192 | Primary Facility | 2009-05-19 | Compliance Evaluation | Outstanding Violations - No Viols Req'd | Performed a Field View as a follow-up to a previously issued Violation for an oil spill. |
2235284 | Primary Facility | 2014-01-09 | Routine/Complete Inspection | No Violations Noted | Marcellus. At time of inspection, well drilled and equipped for production. According to records, drilling occurred 8/21/2008-1/23/2009. Wellhead surrounded by gate. Well tag present. Two brine tanks on-site, both sound, located within vegetative dike. Gas odor noted. |
2262959 | Primary Facility | 2014-04-15 | Administrative/File Review | In Compliance with Policy | SPILL.Admin inspt in response to reported release of 2 bbl brine into earthen dike from prod tank.Release reported to SWRO at 1615 on 4/14/14 by Opr rep Doug Byers.At time of call, leak contained and stopped.No waterways affected.Dept spoke to Mr. Byers via phone in response to this release.Mr. Byers stated that spill was discovered on 4/14/14 at approximately 1530.Pinhole leak in steel 210 bbl tank resulted in brine spraying out of tank into unlined earthen dike.At this time, hole has a temp patch, water has been vac'd out of dike and tank, and Opr is currently delineating area for excavation. Samples being collected and upon receipt, Opr will submit to Dept.Per the spill policy, Opr will be utilizing the attainment method of alternative remediation by remediating this release under the background or Statewide health standard.It appears Operator is handling situation according to policy and a follow-up inspection will be conducted in future to assess any environmental impacts of release and/or issue any associated violations as necessary. |
2263038 | Primary Facility | 2014-04-15 | Incident- Response to Accident or Event | Violation(s) Noted | On-site inspt as follow-up to admin inspt 2262959 for the 4/14/14 reportable release of 2 bbl brine water into earthen dike.Two 210 bbl steel prod tanks w/in earthen dike.Brine water previously vac'd out of dike.Small puddle remains in b/w 2 tanks in which Dept collected conductivity readings of 1460 umHos/cm utilizing a conductivity meter.Excavation of contaminated materials not yet commenced.Dept unable to identify "temporary patch" (record 2262959) on pinhole leak.Dept contacted Opr rep Doug Byers via phone to obtain aid in identifying patch.Mr. Byers stated that temp patch is a "stick stuck into the hole" & water levels in tank were pumped below hole.WT's last check was on 4/1/14 & leak was discovered on 4/14/14; hence, leak dev at some pt w/in this time pd.Dept rec'd Opr commence excavation activities ASAP.Mr. Byers stated that source samples, soil samples, and bkgd samples collected earlier today & excavation will begin upon receipt of sample results.Add'l comments on paper copy. |
2263596 | Primary Facility | 2014-04-17 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On-site FUI for violations issued under inspection record 2263038 for the 4/14/2014 reportable release of 2 bbl brine water into earthen dike. |
2296859 | Primary Facility | 2014-08-20 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On-site FUI for violations issued under inspection record 2263038 (enf ID 309888) for the 4/14/2014 reportable release of 2 bbl brine water into earthen dike. |
2362161 | Primary Facility | 2015-04-07 | Compliance Evaluation | No Violations Noted | On-site FUI in response to violations issued under inspection record 2263038, enf ID 309888 for the reportable release of 2 bbl brine to the ground.At time of inspection, well appears equipped for production.WT present, legible.Well surrounded by fence.Single BT located w/in veg dike with gravel base.Site remediated and properly restored with >70% uniform and adequate veg growth.Dept recommends Opr cont' to monitor/maintain AR and well pad as needed in order to prevent any potential pollution events from occurring.Site ID present, in compliance with Act 9 standards, however attachment to posts is compromised; Dept recommends sign is re-affixed to posts.ERP on-site.Site characterization report approved by Dept on 2/25/15.As approval of the site characterization report has been received and site is restored, viols issued under record 2263038 and enf ID 309888 have been corrected.No new viols noted at this time.Environmental Trainee Cindy Witham present during inspection. |
2627767 | Primary Facility | 2017-08-22 | Routine/Complete Inspection | Violation(s) Noted | At time of inspection, well drilled and appears equipped for production. |
2637083 | Primary Facility | 2017-09-18 | Administrative/File Review | Outstanding Violations - Viols Req'd | Admin inspection conducted in response to violations issued under inspection record 2627767 (enf ID 357599).
The Department requested a written NOV response by 9/14/17. To date, this requested written NOV response has not been received. Violations remain outstanding. |
2643585 | Primary Facility | 2017-10-02 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to violations issued under inspection record 2627767 (enf ID 357599).
The requested NOV written response has been received by the Department. |
2643595 | Primary Facility | 2017-10-04 | Compliance Evaluation | No Violations Noted | Compliance evaluation inspection conducted in response to violations issued under inspection record 2627767 (enf ID 357599).
At the time of this inspection, the Site ID appears to have been repaired. Violations issued under 78a.55(i)4ii have been corrected. |
2724773 | Primary Facility | 2018-05-01 | Routine/Complete Inspection | No Violations Noted | |
2826614 | Primary Facility | 2019-01-11 | Routine/Complete Inspection | No Violations Noted | On 1/11/19 at 1400 hrs., I conducted a routine inspection of Alliance Petroleum, Corp.'s Carl Blose 1 well (API 063-35598) in Cherryhill Twp., Indiana Co. Snow cover prevented proper evaluation of site stabilization. The well pad appears to be restored and permanently stabilized. The well is properly labeled and equipped for production. A site ID sign is posted and a well tag is present at the well head. The production fluid tank is located within secondary containment. There are no violations noted for this inspection. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1794089 | 561714 | 04/14/2009 | 2009-04-14 | 401 CSL - Discharge of pollultional material to waters of Commonwealth. | Environmental Health & Safety | |
2263038 | 693404 | 04/15/2014 | 2014-04-15 | 78.57 - Failure to post pit approval number | Administrative | 78.57A: A violation is being issued for Operator's failure to properly collect and not discharge brine and other fluids on or into the ground or into the waters of the Commonwealth. |
2627767 | 795105 | 2017-08-22 | 2017-10-04 | 78a55(i)4ii | Administrative | A violation is being issued for the operator's failure to comply with 78a55(i)4ii. |
2637083 | 797531 | 2017-09-18 | 2017-10-04 | 78a55(i)4ii | Administrative | This violation remains outstanding. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
561714 | 245473 | NOV - Notice of Violation | Comply/Closed | 2009-06-12 | |||
693404 | 309888 | NOV - Notice of Violation | Superseded | 2017-12-08 | |||
693404 | 360241 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2017-12-08 | 2017-12-08 | $27,000.00 | $27,000.00 |
795105 | 357599 | NOV - Notice of Violation | 2017-10-04 |
For data sources see[7]