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Well ID: 37-063-35961 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: White Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: M P WHITE 4 | |
License Status: ACTIVE | |
Spud Date: 2008-05-27 | |
Permit Date: 2008-04-23 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.648205 | |
Longitude: -79.120397 |
Date | Event |
---|---|
2008-04-23 | New Permit Application |
2008-05-23 | Performed Spud Operation |
2008-05-29 | Drilling Completion |
2008-06-04 | Perforation |
2009-06-26 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | CONSOL GAS CO | 10404.25 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 21103.61 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 13,280.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 14,515.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 9,435.17 | 365 | 11.99 | 30 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 9,316.01 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 6,066.48 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 6,490.22 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 5,226.13 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 2,946.52 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 706.00 | 151 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2008 | CONSOL GAS CO | Fracking Fluid | 200.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2008 | CONSOL GAS CO | Fracking Fluid | 110.00 Bbl | Reuse other than road spreading | 37-129-27352 |
2008 | CONSOL GAS CO | Brine | 95.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2008 | CONSOL GAS CO | Fracking Fluid | 1,200.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095443 |
2009 | CONSOL GAS CO | Brine | 80.00 Bbl | Municipal Sewage Treatment Plant | PA0026034 |
2009 | CONSOL GAS CO | Brine | 956.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009 | CONSOL GAS CO | Brine | 390.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2010 | CONSOL GAS CO | Produced Fluid | 304.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2010 | CONSOL GAS CO | Produced Fluid | 119.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026034 |
2010 | CONSOL GAS CO | Produced Fluid | 85.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2011 | CNX GAS CO LLC | Produced Fluid | 214.14 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 34-099-23127 |
2011 | CNX GAS CO LLC | Produced Fluid | 185.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2012 | CNX GAS CO LLC | Produced Fluid | 125.10 Bbl | INJECTION DISPOSAL WELL | 34-007-22038 |
2012 | CNX GAS CO LLC | Produced Fluid | 66.00 Bbl | INJECTION DISPOSAL WELL | 34-155-23584 |
2012 | CNX GAS CO LLC | Produced Fluid | 124.47 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2013 | CNX GAS CO LLC | Produced Fluid | 90.07 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2014 | CNX GAS CO LLC | Produced Fluid | 20.00 Bbl | INJECTION DISPOSAL WELL | 34-155-23795 |
2014 | CNX GAS CO LLC | Produced Fluid | 62.30 Bbl | INJECTION DISPOSAL WELL | PAS2D912BSOM |
2014 | CNX GAS CO LLC | Produced Fluid | 130.00 Bbl | INJECTION DISPOSAL WELL | 34-119-28776 |
2014 | CNX GAS CO LLC | Produced Fluid | 19.03 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2014 | CNX GAS CO LLC | Produced Fluid | 11.00 Bbl | INJECTION DISPOSAL WELL | 34-155-21893 |
2014 | CNX GAS CO LLC | Produced Fluid | 71.00 Bbl | INJECTION DISPOSAL WELL | 34-133-20525 |
2014 | CNX GAS CO LLC | Produced Fluid | 11.00 Bbl | INJECTION DISPOSAL WELL | 34-155-23203 |
2014 | CNX GAS CO LLC | Produced Fluid | 11.00 Bbl | INJECTION DISPOSAL WELL | 34-155-21894 |
2015 | CNX GAS CO LLC | Produced Fluid | 204.57 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2015 | CNX GAS CO LLC | Produced Fluid | 204.57 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1966863 | Primary Facility | 2011-04-14 | Complaint Inspection | No Violations Noted | |
2383605 | Primary Facility | 2015-06-24 | Administrative/File Review | In Compliance with Policy | SPILL. |
2383625 | Primary Facility | 2015-06-24 | Administrative/File Review | In Compliance with Policy | Admin inspt in response to inspt ID 2383605 for 6/24 reportable release of 20 bbl brine.Upon receipt of spill report, Dept contacted Opr rep Dick Mildren via phone at 1239.Mr. Mildren reported that “20 bbl brine water with a skim of oil on top” was released into a veg dike and fluids are contained w/in dike.Fluids are currently being hauled out now and well has been shut in.Spartan is collecting samples and excavation will begin after all fluids have been vac’d up.Dept recom'd that temp E&S BMPs are properly installed prior to the commencement of any earth disturbance activities.Per Mr. Mildren, the pumping unit kept running when it was supposed to stop, causing the fluids to overflow from the tank, resulting in the release.No waterways are reported to be impacted.Spill discovered by WT on 6/24 at 1123 and subsequently reported to the SWRO at 1202.Operator appears to be in compliance with current policy at this time. A follow-up inspection will be conducted to assess any environmental impact and/or issue any associated violations as necessary. |
2383888 | Primary Facility | 2015-06-26 | Incident- Response to Accident or Event | Violation(s) Noted | On-site inspt conducted in response to record 2383605 for 6/24 reportable release of 20 bbl brine water mixture.At time of inspt, excavation of impacted materials currently ongoing by Spartan.Spartan excavating down-gradient of dike, utilizing conductivity meter as guidance.Per Spartan rep, excavation began yesterday, more trucks are currently en route for disposal of excavated soils.Upon completion of excavation today, plastic will placed over exposed soils due to forecasted heavy rains until area can be temp stabilized w/seed/mulch.BT on-site, removed from veg dike, placed on plastic.Well label present. Dept recommends Opr ensure all temp E&S BMPs are properly installed down-gradient of excavation and cont’ to mon/maintain AR as necessary in order to prevent any add’l pollution events from occurring.A FUI will be conducted in the future to ensure site is properly remediated and restored.Viols are being issued for this reportable release of production fluids. |
2410701 | Primary Facility | 2015-09-22 | Compliance Evaluation | No Violations Noted | On-site CEI conducted in response to viols issued under inspection 2383888 (enf ID 325020) for reportable release of 20 bbl brine water/crude oil mixture.At time of inspt, area of excavation not yet backfilled.Plastic covering area of excavation.Roll-off boxes not on-site.On-site BT remains on plastic.In accordance w/Spill Policy, 15 day written response received by Dept on 7/6/15, notifying Dept that Opr will be utilizing attainment method of Alternative Remediation for remediation of release.Per this response, all contaminated soils excavated utilizing a conductivity meter as guidance and confirmatory soil samples collected for further analysis.As Opr has identified their intent for remediation and excavation of contaminated soils has commenced, viols issued under inspection 2383888 (enf ID 325020) have been corrected.A FUI is anticipated to be conducted to ensure site is properly restored per current regs.Viols may be forthcoming pending future inspts monitoring site restoration and permanent stabilization. |
2413900 | Primary Facility | 2015-09-28 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection ID 2383888 (enf ID 325020) for the reportable release of 20 bbl brine water/crude oil mixture. |
2429269 | Primary Facility | 2015-12-02 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection ID 2383888 (enf ID 325020) for the reportable release of 20 bbl brine water/crude oil mixture. |
2431715 | Primary Facility | 2015-12-03 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection ID 2383888 (enf ID 325020) for the reportable release of 20 bbl brine water/crude oil mixture. |
2454797 | Primary Facility | 2016-02-22 | Administrative/File Review | In Compliance with Policy | Admin inspection in response to violations issued under inspection ID 2383888 (enf ID 325020) for the reportable release of 20 bbl brine water/crude oil mixture.
Fifteen day written response previously received by Department on 7/6/2015, notifying the Department that the Operator will be utilizing the attainment method of Alternative Remediation for the remediation of this release. In accordance with the Spill Policy, Site Characterization & Final Report received by the ECB Program on 11/3/2015. The Site Characterization Report was approved by the Department on 1/14/2016. Operator appears to be in compliance with current policy at this time. |
2707409 | Primary Facility | 2018-03-20 | Routine/Complete Inspection | No Violations Noted | Well appears to be in production. Pump jack on site.
A 20 bbl release of brine occurred on site on 6-24-15. At the time of this inspection area of release is vegetated and all temporary BMPs have been removed. Site appears to be restored. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2383888 | 726737 | 06/24/2015 | 2015-06-24 | 78.54 - GENERAL REQUIREMENTS - Operator failed to control and dispose of fluids, residual waste and drill cuttings, including tophole water, brines, drilling fluids, drilling muds, stimulation fluids, well servicing fluids, oil, and production fluids | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
726737 | 325020 | NOV - Notice of Violation | |||||
726737 | 366525 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2018-07-20 | 2018-07-20 | $4,000.00 | $4,000.00 |
For data sources see[7]